diff --git "a/processed/ddr/15_9_F_10_activities.csv" "b/processed/ddr/15_9_F_10_activities.csv" new file mode 100644--- /dev/null +++ "b/processed/ddr/15_9_F_10_activities.csv" @@ -0,0 +1,1132 @@ +file,well_name,wellbore_name,report_start,report_end,act_start,act_end,md_m,md_uom,phase,activity_code,state,state_detail,comments,duration_hours +15_9_F_10_2009_04_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-06T00:00:00+02:00,2009-04-07T00:00:00+02:00,2009-04-06 04:00:00+00:00,2009-04-06 05:00:00+00:00,0.0,m,fixed,drilling -- drill,ok,success,"Removed hatch for F-10. +Meanwhile :Ran foxhole and secured same.",1.0 +15_9_F_10_2009_04_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-06T00:00:00+02:00,2009-04-07T00:00:00+02:00,2009-04-06 05:00:00+00:00,2009-04-06 10:00:00+00:00,142.9,m,fixed,drilling -- drill,ok,success,"Held toolbox meeting. M/U 36"" BHA. Ran in and entered template at 142,4 m. Tagged seabed at 142,9 m.",5.0 +15_9_F_10_2009_04_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-06T00:00:00+02:00,2009-04-07T00:00:00+02:00,2009-04-06 10:00:00+00:00,2009-04-06 12:00:00+00:00,144.7,m,fixed,drilling -- drill,ok,success,"Started to wash down at 600 - 1000 lpm, taking weight straight away. Started to rotate 20 RPM. worked pipe between 142,9 m - 144,7 m. Pulled back to 143,4 m and held 20 RPM and 1000 lpm. Stopped rotation and stopped pumps. ROV checked bit position.",2.0 +15_9_F_10_2009_04_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-06T00:00:00+02:00,2009-04-07T00:00:00+02:00,2009-04-06 12:00:00+00:00,2009-04-06 14:00:00+00:00,148.1,m,fixed,drilling -- drill,ok,success,"Drilled back down to 144,9 m. Stopped rotation and pumps. ROV moved into template to observe position of bit. Continued to drill, worked 26""/36"" HO into slot. Drilled from 144,9 m to 148,1 m. 1000 lpm - 2300 lpm, 20 RPM.",2.0 +15_9_F_10_2009_04_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-06T00:00:00+02:00,2009-04-07T00:00:00+02:00,2009-04-06 14:00:00+00:00,2009-04-06 17:00:00+00:00,151.0,m,fixed,drilling -- drill,ok,success,"Stopped rotation and pumps. ROV moved into template to observe position of centralizer drill bushing. Continued to drill from 148,1 m to 151 m. 1000 lpm, 20 RPM.",3.0 +15_9_F_10_2009_04_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-06T00:00:00+02:00,2009-04-07T00:00:00+02:00,2009-04-06 17:00:00+00:00,2009-04-06 22:00:00+00:00,165.0,m,fixed,drilling -- drill,ok,success,"Drilled 36"" hole from 151 m to 165 m. 80 RPM, 4 -5 ton WOB, 3000 lpm, trq 3 kNm, Took survey at 160 m. Inclination 0,28 deg. Pumped HIVIS pills as per program.",5.0 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-06 22:00:00+00:00,2009-04-07 03:00:00+00:00,207.0,m,fixed,drilling -- drill,ok,success,"Drilled 36"" hole from 165 m to 207 m (17 1/2"" bit depth). 90-100 RPM, 5 ton WOB, 4000-4450 lpm, 3,7 kNm, ROP 5-20 m/hr. Pumped HIVIS pills as per program. +Took survey at 170 m: Inclination 0,27 deg. +Took survey at 180 m: Inclination 0,17 deg. +Took survey at 190 m: Inclination 0,21 deg. +Took survey at 206 m: Inclination 0,15 deg.",5.0 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 03:00:00+00:00,2009-04-07 03:30:00+00:00,207.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated 1,5 bottoms up with seawater. Pumped 40 m3 HIVIS pill at 4500 lpm. Displaced well to 1,40 sg WBM at 4500 lpm / SPP 128 bar, 10 RPM.",0.5 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 03:30:00+00:00,2009-04-07 04:00:00+00:00,167.0,m,fixed,drilling -- trip,ok,success,"POOH with 36"" BHA to 167 m.",0.5 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 04:00:00+00:00,2009-04-07 05:00:00+00:00,121.0,m,fixed,drilling -- trip,ok,success,"POOH with 36"" BHA to 147 m. Topped up hole with 1,40 sg WBM. POOH to 121 m.",1.0 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 05:00:00+00:00,2009-04-07 07:00:00+00:00,36.0,m,fixed,drilling -- trip,ok,success,"POOH with 36"" BHA to 36 m.",2.0 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 07:00:00+00:00,2009-04-07 07:45:00+00:00,36.0,m,fixed,interruption -- maintain,ok,equipment failure,Investigated and repaired leak on AFT Iron roughneck.,0.75 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 08:00:00+00:00,2009-04-07 10:15:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"POOH with 36"" BHA to 8 m. Held Toolbox talk prior to remove bushings with low block height. Pulled Holeopener through rotary and laid out same.",2.25 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 10:00:00+00:00,2009-04-07 11:30:00+00:00,0.0,m,fixed,drilling -- other,ok,success,Performed full derrick and top drive inspection.,1.5 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 11:30:00+00:00,2009-04-07 14:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Held tool box talk- Rigged to run 30"" conductor.",2.5 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 14:00:00+00:00,2009-04-07 15:00:00+00:00,0.0,m,fixed,drilling -- wait,ok,success,Waited on crane / deck crew to unload boat.,1.0 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 15:00:00+00:00,2009-04-07 17:00:00+00:00,12.0,m,fixed,drilling -- casing,ok,success,"Held toolbox talk with deck crew and 3rd partys prior to pick up an run 30"" Conductor. +P/U and ran 30"" Conductor shoe joint to 12 m. Filled shoe joint to check ball valve.",2.0 +15_9_F_10_2009_04_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-07T00:00:00+02:00,2009-04-08T00:00:00+02:00,2009-04-07 17:00:00+00:00,2009-04-07 22:00:00+00:00,49.0,m,fixed,drilling -- casing,ok,success,"Held toolbox talk. P/U and ran 2 x 30"" intermediate joints and 1 30"" X-over joint. Changed out casing handling gear. Installed elevator rotator and M/U kevlar belt tongs. P/U 30"" Conductor housing joint.",5.0 +15_9_F_10_2009_04_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-08T00:00:00+02:00,2009-04-09T00:00:00+02:00,2009-04-07 22:00:00+00:00,2009-04-08 00:00:00+00:00,45.0,m,fixed,drilling -- casing,ok,success,"M/U 30"" Conductor housing joint. Ran carefully into splash zone with 30"" Conductor. Waves and current was too high to continue operation and risk damaging adjacent production risers. Pulled up with 30"" Conductor to above sea-level and double-secured same. Significant wave height 1,6 m. Max wave height 2,5 m.",2.0 +15_9_F_10_2009_04_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-08T00:00:00+02:00,2009-04-09T00:00:00+02:00,2009-04-08 00:00:00+00:00,2009-04-08 04:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,"Waiting on weather to run 30"" Conductor. Notified Maersk Production to bean up wells. +While waiting on weather cleared rig floor. Removed frame and cage from HTS. Picked up cement stand. Started to pressure test BOP.",4.0 +15_9_F_10_2009_04_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-08T00:00:00+02:00,2009-04-09T00:00:00+02:00,2009-04-08 04:00:00+00:00,2009-04-08 05:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,Waiting on weather. Meanwhile pressure tested BOP to 1035 bar (15000 psi).,1.0 +15_9_F_10_2009_04_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-08T00:00:00+02:00,2009-04-09T00:00:00+02:00,2009-04-08 05:00:00+00:00,2009-04-08 07:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,Waiting on weather. Meanwhile continued to make up cement stand.,2.0 +15_9_F_10_2009_04_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-08T00:00:00+02:00,2009-04-09T00:00:00+02:00,2009-04-08 07:00:00+00:00,2009-04-08 09:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,Waiting on weather. Meanwhile repaired leak on FWD PRS top jaw.,2.0 +15_9_F_10_2009_04_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-08T00:00:00+02:00,2009-04-09T00:00:00+02:00,2009-04-08 09:00:00+00:00,2009-04-08 11:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,Waiting on weather. Meanwhile calibrated FWD PRS. Lined up to test lower pipe ram (LPR) on BOP.,2.0 +15_9_F_10_2009_04_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-08T00:00:00+02:00,2009-04-09T00:00:00+02:00,2009-04-08 11:00:00+00:00,2009-04-08 17:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,"Waiting on weather. Meanwhile rigged up and laid out MWD and 2 x 9 1/2"" drill collars from derrick. Pressure tested LPR on BOP to 20 bar / 5 minutes and 1035 bar / 15 minutes. Prepared 26"" BHA. Started to lay out 8 1/4"" jar.",6.0 +15_9_F_10_2009_04_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-08T00:00:00+02:00,2009-04-09T00:00:00+02:00,2009-04-08 17:00:00+00:00,2009-04-08 20:30:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,"Waiting on weather. Meanwhile held Toolbox talk with new crew. Continued to lay out 8 1/4"" drill collars. Pressure tested stand pipe manifoil to 1035 bar (15000 psi). L/D 8 1/4"" jar. Started to lift up last tension cylinder in moon pool.",3.5 +15_9_F_10_2009_04_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-08T00:00:00+02:00,2009-04-09T00:00:00+02:00,2009-04-08 20:30:00+00:00,2009-04-08 22:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,"Waiting on weather. Meanwhile picked up 8 1/4"" DC and racked in set back. Continued to install tension cylinder in moon pool.",1.5 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-08 22:00:00+00:00,2009-04-09 01:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,"Waiting on weather. Meanwhile P/U 8 1/4"" drill collars and racked back in set back. Installed last tension cylinder in moon pool.",3.0 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 01:00:00+00:00,2009-04-09 02:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,"Waiting on weather. Meanwhile rearranged collar fingerboard to rack back BHA and lay out 6 1/2"" jar.",1.0 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 02:00:00+00:00,2009-04-09 04:00:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,"Waiting on weather. Meanwhile laid out 6 1/4"" jar and 5"" HWDP.",2.0 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 04:00:00+00:00,2009-04-09 06:45:00+00:00,45.0,m,fixed,interruption -- waiting on weather,ok,success,Waited on weather. Issued notice to shut in adjacent wells at 06:45. Meanwhile removed end stops on HTS. Made up aluminium inner string on HTS.,2.75 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 06:45:00+00:00,2009-04-09 07:15:00+00:00,62.0,m,fixed,drilling -- casing,ok,success,"Removed dog collar and pulled slips. Ran 30"" conductor from 45 to 62 m MD.",0.5 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 07:15:00+00:00,2009-04-09 07:30:00+00:00,62.0,m,fixed,drilling -- casing,ok,success,Installed C-plate in rotary. Hung off conductor housing in C-plate. Removed CART handling tool. Filled conductor with SW.,0.25 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 07:30:00+00:00,2009-04-09 08:45:00+00:00,62.0,m,fixed,drilling -- casing,ok,success,"Installed C-plate on top of 30"" housing. Picked up and ran 2 ea premade lengths of aluminium stinger to 46 m inside 30"" conductor. Made up x-over to pup below CART.",1.25 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 08:45:00+00:00,2009-04-09 09:15:00+00:00,62.0,m,fixed,drilling -- casing,ok,success,"Lowered CART and made up to 30"" coductor housing with 5 counterclockwise turns. Installed inclinometer and valve handle on CART.",0.5 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 09:15:00+00:00,2009-04-09 09:45:00+00:00,65.0,m,fixed,drilling -- casing,ok,success,Removed C-plate from RT. Ran conductor housing through RT. Installed master bushing.,0.5 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 09:45:00+00:00,2009-04-09 11:00:00+00:00,196.0,m,fixed,drilling -- casing,ok,success,"RIH with 30"" conductor on 5 1/2"" HWDP landing string from 65 m to 196 m MD. Marked pipe at 112,9 m to obtain relative distance top of conductor housing to Centralizer deck. Observed with ROV when comming through template.",1.25 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 11:00:00+00:00,2009-04-09 11:45:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,"Laid out 5 1/2"" HWDP single. Made up cementing single with side entry and FOSV. Made up TDS. RIH with 30"" Conductor to 201,7 m MD and adjusted setting depth according to marking on pipe releative to Centralizer deck.",0.75 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 11:45:00+00:00,2009-04-09 12:45:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,"Performed elevation check releative to F-15 using ROV and digiquartz, 18 mm deviation - ok. Recorded x/y inclinometer readings 0,0/0,2.",1.0 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 12:45:00+00:00,2009-04-09 13:00:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,Made up cement hose to pump in sub. Flushed lines. Performed line test agianst lo-torque valve to 200 bar / 5 min - ok.,0.25 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 13:00:00+00:00,2009-04-09 13:30:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,Circulated 28 m3 SW at 1500 lpm / SPP 0 bar.,0.5 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 13:30:00+00:00,2009-04-09 14:15:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,"Pumped indicator pill (LCM). Not able to suck effectively from pit. Changed mudpump, but problems prevailing. Mudpump strainers plugged by LCM. Total LCM pill pumped 3,5 m3. Displaced LCM pill to string by pumping 3,6 m3 seawater.",0.75 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 14:15:00+00:00,2009-04-09 15:30:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,"Lined up to cement unit. Mixed and pumped 55 m3 1,54 sg xlite cement slurry at 920 lpm / CUP 21 bar. Observed cement return at seabead with ROV. Block weight declined from 101 MT to 97 MT during cementing.",1.25 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 15:30:00+00:00,2009-04-09 16:00:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,"Displaced cement with 6,2 m3 SW at 480 lpm / FCP 19 bar. Bled off pressure on cement unit - no backflow observed.",0.5 +15_9_F_10_2009_04_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-09T00:00:00+02:00,2009-04-10T00:00:00+02:00,2009-04-09 16:00:00+00:00,2009-04-09 22:00:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,"Waited on cement to set up. At 22:00, checked inclinometer x/y readings 0,2/0,12. Weight in block 97 MT. Issued notice for shut in of adjacent wells at 23:30.",6.0 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-09 22:00:00+00:00,2009-04-09 22:45:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,Waited on cement to set up. Meanwhile performed toolbox talk for disconnecting landing string. Checked cement sample - ok.,0.75 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-09 22:45:00+00:00,2009-04-10 00:00:00+00:00,202.0,m,fixed,drilling -- casing,ok,success,"Slacked off weight to neutral, i.e. 80 MT. Checked inclinometer x/y readings 0,02/0,13. Opened ball valve on CART. Bled off pressure above upper FOSV. Relased CART with 5 clockwise turns while observing conductor housing with ROV. Broke and laid down cementing stand. Picked up and made up 5 1/2"" HWDP single, inserted sponge ball and made up single.",1.25 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 00:00:00+00:00,2009-04-10 00:15:00+00:00,188.0,m,fixed,drilling -- casing,ok,success,Pumped sponge ball at 2000 lpm to clean string. Confirmed adjacent wells de-pressurized at 02:00.,0.25 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 00:15:00+00:00,2009-04-10 01:15:00+00:00,50.0,m,fixed,drilling -- casing,ok,success,"POOH with CART/stinger on 5 1/2"" HWDP from 188 m to 50 m MD. Meanwhile installed CTS pump/funnel on conductor housing using aft crane and ROV.",1.0 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 01:15:00+00:00,2009-04-10 02:15:00+00:00,48.0,m,fixed,drilling -- casing,ok,success,"Pulled master bushing. Pulled CART through RT. Installed master bushing. Set down CART on master bushing. Removed inclinometer. Screwed out 5 1/2"" HWDP single on top of CART. Rigged up C-plate in rotary, and hung off aluminium string on clamp. Broke and laid out CART.",1.0 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 02:15:00+00:00,2009-04-10 04:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"POOH with 5 ea aluminium singles using clamps, C-plate, tugger and chain tongs. Rigged down C-plate. Cleared drillfloor.",1.75 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 04:00:00+00:00,2009-04-10 04:15:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Cleared drillfloor. Put aluminium pipe in basket.,0.25 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 04:15:00+00:00,2009-04-10 05:00:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Held toolbox talk for making up BHA. Laid 26"" bit/stab/motor on HTS.",0.75 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 05:00:00+00:00,2009-04-10 05:15:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,Held toolbox talk/handover meeting.,0.25 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 05:15:00+00:00,2009-04-10 09:15:00+00:00,136.0,m,fixed,drilling -- trip,ok,success,"Made up 26"" drilling BHA comprising of 26"" bit/stab/motor, GWD and powerpulse. Established scribeline from bent sub to MWD and recorded correction. Made up UBHO and adjusted landing sub as required. Made 8 1/4"" DC stand and DC/jar stand. Recessed operation for TDS service/repair.",4.0 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 09:15:00+00:00,2009-04-10 17:30:00+00:00,136.0,m,fixed,interruption -- other,ok,equipment failure,"Changed around stabilizing liners on TDS due to observed wear on drillpipe couplings. Observed rear liner crest more worn than front liner crest. Discussed options. Carried out rig repair of worn liner, i.e. clad welding. Installed modified liner crests on TDS. Comment : New stabilizer liners ordered from rig 30/1-09. Order sendt from Maersk office in town to supplier 8/4-09.",8.25 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 17:30:00+00:00,2009-04-10 19:15:00+00:00,175.0,m,fixed,drilling -- drill,ok,success,"Moved diverter away from setback. RIH and stabbed 26"" BHA into 30"" conductor assissted by ROV. RIH to 175 m MD. ROV hooked up to CTS hose.",1.75 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 19:15:00+00:00,2009-04-10 20:15:00+00:00,175.0,m,fixed,interruption -- other,ok,equipment failure,Made up TDS to test modified stabilizing liner on TDS. Observed scores on DP coupling when rotating pipe. Discussed situation. Opened IBOP and rotated pipe - observed no contact between dies and DP coupling. Decided to continue operation without repair/modifications.,1.0 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 20:15:00+00:00,2009-04-10 21:15:00+00:00,201.0,m,fixed,drilling -- drill,ok,success,"Removed masterbushing and installed auto slips. Staged up pumps for washing down inside 30"" conductor. Observed large shocks in drillstring. Ran ROV to observation position by CTS. RIH to 180 m MD, no hang ups observed. Staged up pumps to 3500 lpm and commenced rotation at 60 rpm. Washed down and tagged shoe/top of cement at 201 m MD.",1.0 +15_9_F_10_2009_04_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-10T00:00:00+02:00,2009-04-11T00:00:00+02:00,2009-04-10 21:15:00+00:00,2009-04-10 22:00:00+00:00,207.0,m,fixed,drilling -- casing,ok,success,"Drilled cement and shoe. Parameters : Flow 2300-3500 lpm / SPP 48-95 bar / 40 RPM / WOB < 1 MT / Torque 2-3 kNm. Broke through shoe at ~203 m MD. Cleaned out rathole down to 207 m MD, reamed back every 2 m drilled.",0.75 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-10 22:00:00+00:00,2009-04-10 22:30:00+00:00,207.0,m,fixed,drilling -- casing,ok,success,Reciprocated across rathole and shoe 4 times. Swept hole with 20 m3 hivis pill.,0.5 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-10 22:30:00+00:00,2009-04-10 23:45:00+00:00,217.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole from 207 m to 217 m MD. Drilling parameters : Flow 3500 lpm / SPP 98 bar / 40 RPM / WOB < 1 MT / Torque 2-3 kNm. Secured string on Centralizer deck. Performed gMWD survey - out of specification. Continuos MWD survey 0-0,57 deg.",1.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-10 23:45:00+00:00,2009-04-11 01:45:00+00:00,228.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole from 217 m to 228 m MD. Drilling parameters : Flow 3500 lpm / SPP 48-95 bar / 40 RPM / WOB < 1 MT / Torque 2-3 kNm. Observed erratic string and torque peaks of 6-7 kNm at 227 m MD. Secured string on Centralizer deck. Performed gmWD survey - out of specification. MWD survey inclination 0,21 deg.",2.0 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 01:45:00+00:00,2009-04-11 02:00:00+00:00,231.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole from 228 m to 231 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 1-2 MT / Torque 2-3 kNm. Observed lose guide on automatic slips. Picked off bottom and stopped drilling.",0.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 02:00:00+00:00,2009-04-11 02:15:00+00:00,231.0,m,fixed,interruption -- other,ok,equipment failure,Removed automatic slips from rotary for repair. Continued operation with manual slips.,0.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 02:15:00+00:00,2009-04-11 03:00:00+00:00,233.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole from 231 m to 233 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 1-2 MT / Torque 2-3 kNm. Secured string on Centralizer deck. Performed gMWD survey - out of specification. MWD survey inclination 0,26 deg.",0.75 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 03:00:00+00:00,2009-04-11 04:00:00+00:00,239.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole from 233 m to 239 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 3-5 MT / Torque 2-4 kNm.",1.0 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 04:00:00+00:00,2009-04-11 05:15:00+00:00,245.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole from 239 to 245 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 3-5 MT / Torque 2-4 kNm. Secured DP at Centralizer deck. Performed gMWD survey - accepted (inc 0,24 / azi 238 deg).",1.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 05:15:00+00:00,2009-04-11 05:30:00+00:00,245.0,m,fixed,drilling -- drill,ok,success,Reamed interval 230-246 m MD in order to reduce inclination. Parameters : Flow 3500 lpm / SPP 97 bar / 40 RPM / Torque 2-4 kNm.,0.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 05:30:00+00:00,2009-04-11 06:00:00+00:00,244.0,m,fixed,drilling -- drill,ok,success,Rigged up WL for performing singel shot survey.,0.5 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 06:00:00+00:00,2009-04-11 06:45:00+00:00,244.0,m,fixed,drilling -- drill,ok,success,Ran singel shot survey. Landed gyro in UBHO at 208 m MD and performed survey. POOH with WL.,0.75 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 06:45:00+00:00,2009-04-11 07:00:00+00:00,244.0,m,fixed,drilling -- drill,ok,success,Rigged down WL equipment.,0.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 07:00:00+00:00,2009-04-11 09:15:00+00:00,246.0,m,fixed,drilling -- drill,ok,success,"Reamed interval 222-246 m MD in order to reduce inclination. Parameters : Flow 3500 lpm / SPP 95 bar / 140 RPM / Torque 2-4 kNm. Pumped 2 x 10 m3 hivis pills. Reduced iclination from 0,53 deg to 0,16 deg.",2.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 09:15:00+00:00,2009-04-11 11:30:00+00:00,257.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole from 246 m to 257 m MD. Drilling parameters : Flow 3500 lpm / SPP 100 bar / 40 RPM / WOB 3-5 MT / Torque 2-4 kNm. Secured DP at Centralizer deck. Performed gMWD survey - accepted. Pumped 10 m3 hivis pill.",2.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 11:30:00+00:00,2009-04-11 12:15:00+00:00,257.0,m,fixed,interruption -- other,ok,equipment failure,Changed to slimmer type dies in TDS pipe handler in order to minimize scoring of DP couplings.,0.75 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 12:15:00+00:00,2009-04-11 18:15:00+00:00,298.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole from 257 m to 298 m MD. Flow 3100-3500 lpm / SPP ~100 bar / 40 RPM / WOB 2-3 MT / Torque 2-4 kNm. Secured DP at Centralizer deck and performed gMWD survey every singel drilled. Pumped hivs every singel.",6.0 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 18:15:00+00:00,2009-04-11 18:45:00+00:00,298.0,m,fixed,drilling -- drill,ok,success,Rigged up WL for performing singel shot survey. Marked pipe and rotary for tooface orientation.,0.5 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 18:45:00+00:00,2009-04-11 19:15:00+00:00,298.0,m,fixed,drilling -- drill,ok,success,Ran singel shot survey. Landed gyro in UBHO at 256 m MD and performed survey. Adjusted toolface to ~132 deg and repeated surveys as required. POOH with WL.,0.5 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 19:15:00+00:00,2009-04-11 19:45:00+00:00,298.0,m,fixed,drilling -- drill,ok,success,Rigged down WL equipment. Made up TDS and performed gMWD survey.,0.5 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 19:45:00+00:00,2009-04-11 20:00:00+00:00,298.0,m,fixed,interruption -- other,ok,equipment failure,Inserted automatic slips (after repair job).,0.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 20:00:00+00:00,2009-04-11 20:15:00+00:00,298.0,m,fixed,drilling -- drill,ok,success,Perfomed gMWD survey. Staged up pumps to 3000 lpm for sliding.,0.25 +15_9_F_10_2009_04_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-11T00:00:00+02:00,2009-04-12T00:00:00+02:00,2009-04-11 20:15:00+00:00,2009-04-11 22:00:00+00:00,328.0,m,fixed,drilling -- drill,ok,success,Initiated kick off according to DDs instructions. Drilled/slided from 298 m to 328 m MD. Drilling parameters : Flow 3000 lpm / SPP ~75 bar / 87-121 RPM / WOB 2-10 MT / Torque 1-4 kNm. Performed gMWD survey at 316 m MD.,1.75 +15_9_F_10_2009_04_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-12T00:00:00+02:00,2009-04-13T00:00:00+02:00,2009-04-11 22:00:00+00:00,2009-04-12 00:00:00+00:00,338.0,m,fixed,drilling -- drill,ok,success,"Took 2 gMWD surveys at 328 m MD. Drilled 26"" hole / slided from 328 m to 338 m MD. Drilling parameters : Flow 3000 lpm / SPP ~82 bar / 83 RPM / WOB 5-7 MT / Torque 3 kNm. Perfomed 3 gMWD surveys at 338 m MD. Obtained survey within specification on 3rd attempt.",2.0 +15_9_F_10_2009_04_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-12T00:00:00+02:00,2009-04-13T00:00:00+02:00,2009-04-12 00:00:00+00:00,2009-04-12 01:15:00+00:00,354.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 338 m to 354 m MD. Drilling parameters : Flow 3000 lpm / SPP ~75 bar / ~85 RPM / WOB 5-6 MT / Torque 3-5 kNm. Secured DP at Centralizer deck and took gMWD survey at 354 m MD - ok.",1.25 +15_9_F_10_2009_04_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-12T00:00:00+02:00,2009-04-13T00:00:00+02:00,2009-04-12 01:15:00+00:00,2009-04-12 04:00:00+00:00,390.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 354 m to 390 m MD. Drilling parameters : Flow 3000 lpm / SPP 50-105 bar / 90-180 RPM / WOB 5-10 MT / Torque 4-8 kNm. Secured DP at Centralizer deck and took gMWD survey as instructed by DD.",2.75 +15_9_F_10_2009_04_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-12T00:00:00+02:00,2009-04-13T00:00:00+02:00,2009-04-12 04:00:00+00:00,2009-04-12 08:30:00+00:00,459.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 390 m to 459 m MD. Drilling parameters : Flow 3500 lpm / SPP 50-112 bar / 90-180 RPM / WOB 5-10 MT / Torque 4-7 kNm / ROP 40 m/hr. Pumped 2-3 hivis pills per stand.",4.5 +15_9_F_10_2009_04_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-12T00:00:00+02:00,2009-04-13T00:00:00+02:00,2009-04-12 08:30:00+00:00,2009-04-12 08:45:00+00:00,459.0,m,fixed,drilling -- drill,ok,success,Rigged up WL equipment to run gyro.,0.25 +15_9_F_10_2009_04_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-12T00:00:00+02:00,2009-04-13T00:00:00+02:00,2009-04-12 08:45:00+00:00,2009-04-12 10:15:00+00:00,459.0,m,fixed,drilling -- drill,ok,success,"Ran WL gyro. Landed gyro in UBHO at 420 m MD and performed survey. Experienced noise interference downhole. POOH with WL gyro and changed setting from North seeking to line of sight. RIH with gyro and landed in UBHO. Perfomed survey. POOH with WL gyro, performed contiunous survey on way out.",1.5 +15_9_F_10_2009_04_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-12T00:00:00+02:00,2009-04-13T00:00:00+02:00,2009-04-12 10:15:00+00:00,2009-04-12 10:30:00+00:00,459.0,m,fixed,drilling -- drill,ok,success,Rigged down WL equipment.,0.25 +15_9_F_10_2009_04_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-12T00:00:00+02:00,2009-04-13T00:00:00+02:00,2009-04-12 10:30:00+00:00,2009-04-12 20:30:00+00:00,620.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 459 m to 620 m MD. Drilling parameters Flow 3100-4500 lpm / SPP 85-177 bar/ 130-220 rpm / WOB 4-15 MT / Torque 5-12 kNm / ROP 30-60 m/hr. Performed gMWD/MWD survey on every single. Pumped 2-3 hivis pills per stand.",10.0 +15_9_F_10_2009_04_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-12T00:00:00+02:00,2009-04-13T00:00:00+02:00,2009-04-12 20:30:00+00:00,2009-04-12 22:00:00+00:00,660.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 620 m to 660 m MD. Drilling parameters Flow 3100-4500 lpm / SPP 95-180 bar/ 130-220 RPM / WOB 4-15 MT / Torque 5-12 kNm / ROP 30-50 m/hr. Performed gMWD/MWD on every connection. Pumped 2-3 hivis pills per stand.",1.5 +15_9_F_10_2009_04_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-13T00:00:00+02:00,2009-04-14T00:00:00+02:00,2009-04-12 22:00:00+00:00,2009-04-13 01:45:00+00:00,742.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 660 m to 742 m MD. Drilling parameters Flow 3100-4500 lpm / SPP 90-200 bar/ 130-220 RPM / WOB 15-20 MT / Torque 12-15 kNm / ROP 20-40 m/hr. Performed gMWD/MWD on every connection. Obtained 3rd consecutive quality survey MWD versus gMWD. Pumped 2-3 hivis pills per stand.",3.75 +15_9_F_10_2009_04_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-13T00:00:00+02:00,2009-04-14T00:00:00+02:00,2009-04-13 01:45:00+00:00,2009-04-13 04:00:00+00:00,798.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 742 m to 798 m MD. Drilling parameters Flow 3100-4500 lpm / SPP 105-200 bar/ 130-220 RPM / WOB 15-20 MT / Torque 12-15 kNm / ROP 15-25 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand.",2.25 +15_9_F_10_2009_04_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-13T00:00:00+02:00,2009-04-14T00:00:00+02:00,2009-04-13 04:00:00+00:00,2009-04-13 07:15:00+00:00,862.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 798 m to 862 m MD. Drilling parameters : Flow 3100-4500 lpm / SPP 105-200 bar/ 130-220 RPM / WOB 15-20 MT / Torque 12-15 kNm / ROP 15-35 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand.",3.25 +15_9_F_10_2009_04_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-13T00:00:00+02:00,2009-04-14T00:00:00+02:00,2009-04-13 07:15:00+00:00,2009-04-13 08:45:00+00:00,862.0,m,fixed,drilling -- drill,ok,success,Reamed/reciprocated last stand 3 times in order to clean hole before entering Utsira. Pumped 15 m3 hivs pill. Parameters : Flow 4000-4500 lpm / SPP 137-174 bar/ 140-170 RPM / Torque 3-5 kNm.,1.5 +15_9_F_10_2009_04_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-13T00:00:00+02:00,2009-04-14T00:00:00+02:00,2009-04-13 08:45:00+00:00,2009-04-13 11:00:00+00:00,893.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 862 m to 893 m MD. Drilling parameters : Flow 4500 lpm / SPP ~190 bar/ 130 RPM / WOB 10-20 MT / Torque 3-5 kNm / ROP 10-20 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand. Encountered top of Utsira at 892 m MD observed by drilling break.",2.25 +15_9_F_10_2009_04_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-13T00:00:00+02:00,2009-04-14T00:00:00+02:00,2009-04-13 11:00:00+00:00,2009-04-13 16:15:00+00:00,1090.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 893 m to 1090 m MD. Drilling parameters : Flow 3500 lpm / SPP 110-130 bar/ 100 RPM / WOB 5-10 MT / Torque 0-4 kNm / ROP 50-130 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand.",5.25 +15_9_F_10_2009_04_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-13T00:00:00+02:00,2009-04-14T00:00:00+02:00,2009-04-13 16:15:00+00:00,2009-04-13 22:00:00+00:00,1148.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 1090 to 1148 m MD. Drilling parameters : Flow 4000-4500 lpm / SPP 150-190 bar/ 130-220 RPM / WOB 10-20 MT / Torque 0-20 kNm / ROP 10-20 m/hr. Performed MWD survey on every connection. Pumped 2-3 hivis pills per stand. Encountered hard stringers at 1116, 1124 and 1134 m MD",5.75 +15_9_F_10_2009_04_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-14T00:00:00+02:00,2009-04-15T00:00:00+02:00,2009-04-13 22:00:00+00:00,2009-04-14 04:00:00+00:00,1265.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 1148 m to 1265 m MD. Drilling parameters : Flow 3000-4000 lpm / SPP 150-180 bar/ 115-200 RPM / WOB 8-20 MT / Torque 5-15 kNm / ROP 10-20 m/hr. Reamed 2 last stands drilled in order to cater for drilling the Skade formation. Pumped 2-3 hivis pills per stand.",6.0 +15_9_F_10_2009_04_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-14T00:00:00+02:00,2009-04-15T00:00:00+02:00,2009-04-14 04:00:00+00:00,2009-04-14 10:15:00+00:00,1400.0,m,fixed,drilling -- drill,ok,success,"Drilled 26"" hole / slided from 1265 m to section TD at1400 m MD. Drilling parameters : Flow 3500-4500 lpm / SPP 130-190 bar/ 100-170 RPM / WOB 5-20 MT / Torque 5-20 kNm / ROP 40-150 m/hr. Pumped 2-3 x 30 m3 hivis pills per stand. Perfomed MWD survey on every connection. Maintained toolface highside when drilling Skade sand. Top Skade at 1234 m MD and base Skade at 1364 m MD.",6.25 +15_9_F_10_2009_04_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-14T00:00:00+02:00,2009-04-15T00:00:00+02:00,2009-04-14 10:15:00+00:00,2009-04-14 12:30:00+00:00,1400.0,m,fixed,drilling -- circulating conditioning,ok,success,Circulated hole clean. Pumped 2 x 30 m3 hivis pills. Reciprocated stand between 1400 m and 1384 m MD. Parameters : Flow 4500 lpm / SPP 180-190 bar / 170-220 RPM / Torque 9-14 k Nm.,2.25 +15_9_F_10_2009_04_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-14T00:00:00+02:00,2009-04-15T00:00:00+02:00,2009-04-14 12:30:00+00:00,2009-04-14 13:45:00+00:00,1400.0,m,fixed,drilling -- circulating conditioning,ok,success,"Displaced well partly to put 1,40 sg KCl mud to above Utsira formation. Pumped a total of 252 m3 KCl mud. Parameters : Flow 4500 lpm / SPP 205-215 bar / 170 RPM / Torque 7-14 kNm.",1.25 +15_9_F_10_2009_04_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-14T00:00:00+02:00,2009-04-15T00:00:00+02:00,2009-04-14 13:45:00+00:00,2009-04-14 17:30:00+00:00,1223.0,m,fixed,drilling -- trip,ok,success,"POOH with 26"" drilling BHA from 1400 m to 1223 m MD. Took 30-50 MT overpull when pulling through Skade sand. Worked string with rotation/flow as limited by torque and overpull. Paramaters : Flow 200-1000 lpm / SPP 2-5 bar / 20-30 RPM / Torque 10-35 kNm. String free with normal weight when bit above Skade sand.",3.75 +15_9_F_10_2009_04_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-14T00:00:00+02:00,2009-04-15T00:00:00+02:00,2009-04-14 17:30:00+00:00,2009-04-14 18:30:00+00:00,958.0,m,fixed,drilling -- trip,ok,success,"POOH with 26"" drlling BHA from 1223 to 958 m MD.",1.0 +15_9_F_10_2009_04_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-14T00:00:00+02:00,2009-04-15T00:00:00+02:00,2009-04-14 18:30:00+00:00,2009-04-14 22:00:00+00:00,916.0,m,fixed,drilling -- trip,ok,success,"Encounterd thight hole at 958 m MD, took 20-30 MT overpull. Worked string with rotation/flow as limited by torque and overpull. Parameters : Flow 200-800 lpm / SPP 2-5 bar / 30 RPM / Torque 6-28 kNm.",3.5 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-14 22:00:00+00:00,2009-04-14 23:45:00+00:00,887.0,m,fixed,drilling -- trip,ok,success,Continued working string from 916 m to 887 m MD. Worked string with rotation/flow as limited by torque and overpull. Parameters : Flow 200 lpm / SPP 2-3 bar / 30 RPM / Torque 6-33 kNm.,1.75 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-14 23:45:00+00:00,2009-04-15 01:15:00+00:00,540.0,m,fixed,drilling -- trip,ok,success,"POOH with 26"" drilling BHA from 887 m to 540 m MD. Worked thight area from 650 m to 640 m MD.",1.5 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 01:15:00+00:00,2009-04-15 01:45:00+00:00,495.0,m,fixed,drilling -- circulating conditioning,ok,success,"Displaced well above 500 m MD to 1,40 sg KCl mud while pullling stand. Pumped a total of 143 m3 mud. Parameters : Flow 4500 lpm / SPP 200-210 bar / 30 RPM (string) / Torque 4-7 kNm. Issued notice to shut-in adjacent wells at 03:30.",0.5 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 01:45:00+00:00,2009-04-15 03:15:00+00:00,250.0,m,fixed,drilling -- trip,ok,success,"POOH with 26"" drilling BHA from 495 m to 250 m MD. Worked tight area from 450 m to 430 m MD.",1.5 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 03:15:00+00:00,2009-04-15 03:30:00+00:00,250.0,m,fixed,drilling -- circulating conditioning,ok,success,"At 250 m MD, topped up well by pumping 15 m3 1,40 sg KCl mud. Flow 1800 lpm / SPP 34 bar. Meanwhile performed toolbox talk for pulling BHA.",0.25 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 03:30:00+00:00,2009-04-15 04:00:00+00:00,146.0,m,fixed,drilling -- trip,ok,success,"POOH with 26"" drilling BHA from 250 m to 146 m MD. Removed PS-21 slips and installed master bushing. Confirmed adjacent wells shut in at 05:45.",0.5 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 04:00:00+00:00,2009-04-15 04:15:00+00:00,136.0,m,fixed,drilling -- drill,ok,success,"POOH with 26"" drilling BHA from 146 m MD to 136 MD. Observed with ROV when comming through CTS funnel / 30"" conductor.",0.25 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 04:15:00+00:00,2009-04-15 05:00:00+00:00,107.0,m,fixed,drilling -- trip,ok,success,"POOH and racked back stand of 8,25"" DC. Broke and laid out jar.",0.75 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 05:00:00+00:00,2009-04-15 07:45:00+00:00,40.0,m,fixed,drilling -- trip,ok,success,"Broke and racked back stand of 8,25"" DC and stand of 9,25"" NMDC. Broke connection between gMWD and MWD, retrieved gyro insert, re-made connection. Attempted to rack to rack back 26"" drilling BHA in derrick - negative - too high weight in PRS. Large amounts of clay trapped on BHA.",2.75 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 07:45:00+00:00,2009-04-15 08:00:00+00:00,40.0,m,fixed,drilling -- trip,ok,success,Held toolbox talk for breaking BHA.,0.25 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 08:00:00+00:00,2009-04-15 09:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Broke and laid out UBHO, MWD, GMWD and stab/motor/26"" bit. Meanwhile removed CTS funnel from conductor using aft crane assisted by ROV.",1.75 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 09:45:00+00:00,2009-04-15 10:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,Cleared and tidied drillfloor. Prepared for rigging casing running equipment.,1.0 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 10:45:00+00:00,2009-04-15 12:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Removed DP elevator and drilling bails. Moved casing casing tong and frame to IR tracks. Hooked up hydraulics to casing tong.,1.25 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 12:00:00+00:00,2009-04-15 12:15:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Held toolbox talk prior to derrick inspection. Isolated equipment.,0.25 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 12:15:00+00:00,2009-04-15 13:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Performed inspection of derrick and TDS using manrider.,0.75 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 13:00:00+00:00,2009-04-15 17:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Made up LaFleur circulating tool. Installed long bails. Installed 310 MT BX elevator and hooked up hydraulics. Meanwhile ROV performed digiquartz measurement of conductor elevation releative to F-15 - 1 mm deviation.,4.0 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 17:00:00+00:00,2009-04-15 17:30:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Held toolbox talk for running 20"" casing. Made adjustments on Lafleur spacing.",0.5 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 17:30:00+00:00,2009-04-15 19:30:00+00:00,26.0,m,fixed,drilling -- casing,ok,success,"Picked up 20"" shoe joint. Hung off in rotary and secured with dog collar. Tested float for flowthough - ok. Picked up and made up 20"" intermediate joint. Adjusted stabbing arm and casing tong. Applied threadlock and made up connection to 46000 ft lbs (max available torque). RIH.",2.0 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 19:30:00+00:00,2009-04-15 20:15:00+00:00,40.0,m,fixed,drilling -- casing,ok,success,"Picked up 20"" landing collar joint. Checked threads. Applied threadlock and made up connection to 46000 ft lbs. Found spacing to make up mark to be approx 5 mm short. Discussed situation and decided to continue operation.",0.75 +15_9_F_10_2009_04_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-15T00:00:00+02:00,2009-04-16T00:00:00+02:00,2009-04-15 20:15:00+00:00,2009-04-15 22:00:00+00:00,78.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" 133# N80 Tenaris ER casing w/centralizers from 40 m to 78 m MD. Checked floats for inflow - ok.",1.75 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-15 22:00:00+00:00,2009-04-16 00:00:00+00:00,139.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" 133# N80 Tenaris ER casing w/centralizers from 78 m to 139 m MD.",2.0 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 00:00:00+00:00,2009-04-16 00:30:00+00:00,150.0,m,fixed,drilling -- casing,ok,success,"Stabbed 20"" casing into conductor. Used ROV push buckle to assist. Issued instruction to start production in adjacent wells at 02:28.",0.5 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 00:30:00+00:00,2009-04-16 01:45:00+00:00,214.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" 133# N80 Tenaris ER casing from 150 m to 214 m MD. Filled casing with KCl mud every 5th joint.",1.25 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 01:45:00+00:00,2009-04-16 02:45:00+00:00,214.0,m,fixed,drilling -- casing,ok,success,Removed master bushing. Installed PS-30 slips which was challenging due to large OD casing through RT.,1.0 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 02:45:00+00:00,2009-04-16 04:00:00+00:00,292.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" 133# N80 Tenaris ER casing from 214 m to 292 m MD. Filled casing with KCl mud every 5th joint.",1.25 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 04:00:00+00:00,2009-04-16 05:00:00+00:00,314.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" 133# N80 Tenaris ER casing from 292 m to 314 m MD. Filled casing with 1,40 sg KCl mud every 5th joint.",1.0 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 05:00:00+00:00,2009-04-16 05:15:00+00:00,314.0,m,fixed,drilling -- casing,ok,success,Held handover meeting.,0.25 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 05:15:00+00:00,2009-04-16 08:45:00+00:00,448.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" 133# N80 Tenaris ER casing from 314 m to 448 m MD. Filled casing with 1,40 sg KCl mud every 5th joint.",3.5 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 08:45:00+00:00,2009-04-16 10:30:00+00:00,460.0,m,fixed,drilling -- casing,ok,success,"Took 20 MT weight at 448 m MD. Attempted to pass restriction 4 times - negative. Broke circulation and worked string down to 460 m MD pumping 1,4 sg mud at 660 lpm / SPP 17 bar. Circulated bottoms up pumping seawater at 1550 lpm / SPP 24 bar. Observed cuttings returns to seabed.",1.75 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 10:30:00+00:00,2009-04-16 11:30:00+00:00,497.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" 133# N80 Tenaris ER casing from 460 m to 497 m MD. Observed loose link-tilt clamp on bails.",1.0 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 11:30:00+00:00,2009-04-16 12:45:00+00:00,497.0,m,fixed,interruption -- other,ok,equipment failure,Prepared permit for manriding. Isolated drillfloor equipment. Re-tightned link tilt clamp. De-isolated equipment.,1.25 +15_9_F_10_2009_04_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-16T00:00:00+02:00,2009-04-17T00:00:00+02:00,2009-04-16 12:45:00+00:00,2009-04-16 22:00:00+00:00,1066.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" 133# N80 Tenaris ER casing from 314 m to 448 m MD. Filled casing with 1,40 sg KCl mud every 5th joint. Tight spot at 640 m to 652 m MD, ~15 MT drag but no circulation needed.",9.25 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-16 22:00:00+00:00,2009-04-17 01:15:00+00:00,1238.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" 133# N80 Tenaris ER casing from 1066 m to 1238 m MD. Filled casing with 1,40 sg KCl mud every 5th joint. Counted joints left on deck - 18 - ok.",3.25 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 01:15:00+00:00,2009-04-17 04:00:00+00:00,1238.0,m,fixed,drilling -- casing,ok,success,Broke out Lafleur packer. Rigged down 310 MT BX elevator. Rigged down long bails. Installed drilling bails and DP elevator. Removed equipment from drillfloor.,2.75 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 04:00:00+00:00,2009-04-17 05:00:00+00:00,1238.0,m,fixed,drilling -- casing,ok,success,"Picked up 18 3/4"" wellhead. Removed protective cap. Washed and checked threads. Made up 18 3/4"" WH to 20"" casing.",1.0 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 05:00:00+00:00,2009-04-17 05:30:00+00:00,1238.0,m,fixed,drilling -- casing,ok,success,Removed PS-30 slips from rotary and installed outer ring.,0.5 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 05:30:00+00:00,2009-04-17 06:30:00+00:00,1238.0,m,fixed,interruption -- fish,ok,stuck equipment,"Attempted to RIH with 20"" casing / 18 3/4"" WH - negative. Worked to free pipe with alternating up/down weights, 50 MT set down / 60 MT overpull - negative - 20"" casing differential stuck. String movement < 50 cm. Set down 50 MT weight. Installed split bowl and set casing in slips. Discussed situation, decided to attempt making up TDS and displace well from 1,40 sg KCl mud to seawater.",1.0 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 06:30:00+00:00,2009-04-17 06:45:00+00:00,1238.0,m,fixed,interruption -- fish,ok,stuck equipment,Screwed in TDS to pup joint on CART while observing movement on CART. Managaed to get torque wrench in position without jeapordizing CART make up. Made up TDS.,0.25 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 06:45:00+00:00,2009-04-17 09:15:00+00:00,1238.0,m,fixed,interruption -- fish,ok,stuck equipment,"Staged up pumps to 660 lpm, verified returns to seabed. Staged up pumps to 2000 lpm / SPP ~30 bar.",2.5 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 09:15:00+00:00,2009-04-17 10:15:00+00:00,1238.0,m,fixed,interruption -- fish,ok,stuck equipment,Attempted to free string while circulating at 2000 lpm. Set down / overpull 60/60 MT. Increased set down weight to 80 MT and observed string comming free. Took up/down weights 270/220 MT. Cummulative volume of seawater pumped ~300 m3.,1.0 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 10:15:00+00:00,2009-04-17 12:00:00+00:00,1238.0,m,fixed,drilling -- casing,ok,success,Reduced flowrate to 500 lpm and reciprocated string while rigging down and removing casing tong. RIH to 1249 m MD and hung off wellhead in manual slips.,1.75 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 12:00:00+00:00,2009-04-17 12:30:00+00:00,1249.0,m,fixed,drilling -- casing,ok,success,Filled gap between wiper plugs through port on CART. Verified free rotation of CART tool.,0.5 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 12:30:00+00:00,2009-04-17 13:15:00+00:00,1249.0,m,fixed,drilling -- casing,ok,success,"Made up TDS to stand of 5 1/2"" HWDP and CART. Worked the string while investigating activity on seabed.",0.75 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 13:15:00+00:00,2009-04-17 13:30:00+00:00,1251.0,m,fixed,drilling -- casing,ok,success,"Removed split bushing from RT. Ran 18 3/4"" WH CART past rotary. Installed master bushings.",0.25 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 13:30:00+00:00,2009-04-17 15:45:00+00:00,1383.0,m,fixed,drilling -- casing,ok,success,"RIH with 20"" casing / 18 3/4"" wellhead on 5 1/2"" HWDP from 1251 m to 1383 m MD. Washed down with 1000 lpm / SPP 14 bar.",2.25 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 15:45:00+00:00,2009-04-17 16:30:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,Worked through tight area from 1383 m to 1389 m MD ~25 MT drag. Washed down with 2000 lpm / SPP 24 bar.,0.75 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 16:30:00+00:00,2009-04-17 17:15:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,"Picked up cement head and continued working tight spot down to 1289 m MD. Landed and locked 18 3/4"" wellhead in 30"" conductor housing at 139,72 m MD by setting down string weight (WH Datum @ 138.94 m RT). Performed 50 MT overpull test on wellhead - ok.",0.75 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 17:15:00+00:00,2009-04-17 17:45:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,"Held prejob meeting for cementing 20"" casing. Hooked up cement hose to cement head.",0.5 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 17:45:00+00:00,2009-04-17 18:15:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,Verified line up. Tested cement line to 200 bar - ok.,0.5 +15_9_F_10_2009_04_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-17T00:00:00+02:00,2009-04-18T00:00:00+02:00,2009-04-17 18:15:00+00:00,2009-04-17 22:00:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,"Dropped 1 3/4"" ball for bottom wiper plug. Sheared bottom wiper plug with 50 bar. Mixed and pumped 90 m3 1,56 sg SSA cement (lead 1) cement at 1100 lpm / CUP 23 bar. Mixed and pumped 120 m3 1,56 sg cement (lead 2) at 1100 lpm / CUP 21 bar.",3.75 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-17 22:00:00+00:00,2009-04-18 00:30:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,"Mixed and pump 113 m3 1,56 sg cement (lead 2) at 1100 lpm / CUP 21 bar. Mixed and pumped 25 m3 1,92 sg tail slurry at 800 lpm / CUP 20 bar.",2.5 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 00:30:00+00:00,2009-04-18 00:45:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,Displaced cement to drillfloor with 890 liters. Dropped dart. Displaced 3000 liter pumping with cement unit. Observed shear of lower wiper plug with 180 bar.,0.25 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 00:45:00+00:00,2009-04-18 02:15:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,"Lined up to pump with mud pumps. Stepped up pumps to 3000 lpm. Pressure rose from 4 bar to 89 bar during displacement. Displaced cement with 9661 strokes (177 strokes less than theoretical). Bumped plug with 170 bar, i.e. 80 bar more than FCP at 3000 lpm. No firm confirmation of cement returns to seabed during displacement, but steady fluid return was observed during the operation.",1.5 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 02:15:00+00:00,2009-04-18 02:45:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,"Lined up to cement unit. Bled back to cement unit, in total 2,3 m3 before backflow stopped. Issued instruction to shut in adjacent wells at 04:40.",0.5 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 02:45:00+00:00,2009-04-18 04:00:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,While depressurising wells. Rigged down cement hose and flushed same. Brought 2 x tension cylinders from moonpool to Centralizer deck. Brought ROV to surface for collecting WH cap.,1.25 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 04:00:00+00:00,2009-04-18 04:30:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,Mounted tension cylinders on Centralizer deck. ROV brought WH cap to seabed. Verified adjacent wells shut in at 06:30.,0.5 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 04:30:00+00:00,2009-04-18 05:00:00+00:00,140.0,m,fixed,drilling -- casing,ok,success,Released CART with 5 clockwise turns.,0.5 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 05:00:00+00:00,2009-04-18 05:15:00+00:00,140.0,m,fixed,drilling -- casing,ok,success,Held toolbox talk for laying out cement head.,0.25 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 05:15:00+00:00,2009-04-18 05:45:00+00:00,137.0,m,fixed,drilling -- casing,ok,success,Broke and laid down cement head. Hooked down hydraulics. laid out cement head on HTS.,0.5 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 05:45:00+00:00,2009-04-18 06:45:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Inserted sponge balls in string. Pumped sponge balls at 500 lpm / SPP 1 bar. POOH with CART on 5 1/2"" HWDP from 137 m MD to surface. Broke and laid out CART.",1.0 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 06:45:00+00:00,2009-04-18 07:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Held toolbox talk for installing tension cylinders.,0.25 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 07:00:00+00:00,2009-04-18 10:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Brought 2 x tension cylinders from Weatherdeck to Centralizer deck. Mounted tension cylinders on Centralizer deck. Meanwhile prepared for running HPDR. Notice given to start production at 09:15. Started production in adjacent wells at 13:30.,3.5 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 10:30:00+00:00,2009-04-18 14:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Rigged up for running HPDR. Brought riser spider to drillfloor and hooked up same. Brought tensioning equipment to drillfloor. Meanwhile cleaned pits for reception of OBM.,4.0 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 14:30:00+00:00,2009-04-18 14:45:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Held toolbox talk for picking up HPDR.,0.25 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 14:45:00+00:00,2009-04-18 15:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Brought TBC / double ""A"" from Cantilever to drillfloor by simultaneous lift by deck crane and TDS. Retracted TDS and set down TBC on drillfoor.",0.75 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 15:30:00+00:00,2009-04-18 19:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Function tested and performed pre-operational checks on TBC according to Vetco procedure. Brought boat collission stool from drillfloor to Centralizer deck. Installed RLGF on wellhead using aft crane and ROV. Verified production shut in of adjacent wells at 18:50.,3.5 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 19:00:00+00:00,2009-04-18 19:30:00+00:00,23.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Ran TBC / double ""A"" through moonpool, Weatherdeck and XMT deck and hung off in spider.",0.5 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 19:30:00+00:00,2009-04-18 20:15:00+00:00,23.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Brought double ""B"" from Cantilever to drillfloor by simultaneous lift by deck crane and TDS. Removed handling flange type C from TBC /double ""A"". Landed double ""B"" onto double ""A"".",0.75 +15_9_F_10_2009_04_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-18T00:00:00+02:00,2009-04-19T00:00:00+02:00,2009-04-18 20:15:00+00:00,2009-04-18 22:00:00+00:00,23.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Made up riser flange using bolt tensioner tool.,1.75 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-18 22:00:00+00:00,2009-04-18 23:15:00+00:00,23.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Tested flange to 3000 psi with handpump. Installed bolt caps and fairings on flange.,1.25 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-18 23:15:00+00:00,2009-04-19 00:30:00+00:00,34.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,RIH with HPDR and located TBC on Centralizer deck. Ran guidewires. Caught guidewires through well slot and threaded same through ROV hooks above HPDR riser. Ran 6T tugger/guidewire to seabed and attached same. Ran 10T tugger/guidewire to sealevel.,1.25 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 00:30:00+00:00,2009-04-19 01:00:00+00:00,52.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Ran HPDR riser to 52 m MD and hung off in spider.,0.5 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 01:00:00+00:00,2009-04-19 01:45:00+00:00,52.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Brought double ""C"" from Cantilever to drillfloor by simultaneous lift by deck crane and TDS. Removed handling flange on double ""B"". Inspected and refurbished flanges.",0.75 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 01:45:00+00:00,2009-04-19 03:30:00+00:00,52.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Landed double ""C"" onto double ""B"". Made up riser flange using bolt tensioner tool. Tested flange to 3000 psi with handpump.",1.75 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 03:30:00+00:00,2009-04-19 04:00:00+00:00,82.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Installed bolt caps and fairings. Ran HPDR to 82 m MD and hung off in spider.,0.5 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 04:00:00+00:00,2009-04-19 04:45:00+00:00,82.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Brought double ""D"" to drillfloor by simultaneous lift by deck crane and TDS. Removed handling flange type ""C"" from double ""C"". Cleaned and refurbished flanges. Landed double ""D"" onto double ""C"".",0.75 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 04:45:00+00:00,2009-04-19 06:15:00+00:00,82.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Made up riser flange using bolt tensioner tools.,1.5 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 06:15:00+00:00,2009-04-19 06:45:00+00:00,82.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Installed bolt caps and fairings.,0.5 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 06:45:00+00:00,2009-04-19 07:00:00+00:00,105.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Ran HPDR from 82 m to 105 m MD.,0.25 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 07:00:00+00:00,2009-04-19 07:45:00+00:00,105.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Brought BOP/tension joint double ""E"" to drillfloor by simultaneous lift by deck crane and TDS. Removed handling flange type ""C"" from double ""D"". Cleaned and refurbished flanges. Landed double ""E"" onto double ""D"".",0.75 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 07:45:00+00:00,2009-04-19 09:30:00+00:00,105.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Made up riser flange using bolt tensioner tools. Installed bolt caps and fairings.,1.75 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 09:30:00+00:00,2009-04-19 10:45:00+00:00,105.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Rigged tuggers for removing riser spider. Split and removed riser spider.,1.25 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 10:45:00+00:00,2009-04-19 11:45:00+00:00,130.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Ran HPDR from 105 m to 130 m MD. Installed outer ring and master bushing in rotary.,1.0 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 11:45:00+00:00,2009-04-19 12:00:00+00:00,130.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Made up stand of 5 1/2"" HWDP to TDS and Claxton tool.",0.25 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 12:00:00+00:00,2009-04-19 12:30:00+00:00,139.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Run in with HPDR and stabbed TBC into RLGF. Observed VX ring out of position. Used ROV arm to push VX ring in correct position. Verified correct orientation of valve panel on TBC. Observed sufficient connector swallow over wellhead in RLGF window.,0.5 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 12:30:00+00:00,2009-04-19 14:00:00+00:00,139.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Re arranged RLGF slings. Split RLGF and removed by ROV. Meanwhile prepared to install hatches and built scaffolding.,1.5 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 14:00:00+00:00,2009-04-19 15:00:00+00:00,140.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Landed TBC on 18 3/4"" wellhead, set dwon 15 mT on wellhead. Ran hotstab and engaged same in TBC receptacle. Locked TBC by applying 3000 psi. Issued intruction to start up adjacent wells at 17:00.",1.0 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 15:00:00+00:00,2009-04-19 17:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Took 15 MT overpull, i.e. 140 MT on block to test tie-back connector - ok. Installed hathces on Weatherdeck. built scaffolding on Weatherdeck to access Claxton tool.",2.5 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 17:30:00+00:00,2009-04-19 19:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Held toolbox talk for pressure test. Lined up cement unit to pump down string. Topped up HPDR with 8 m3 seawater. Instatalled weco cap on Calxton tool.,1.5 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 19:00:00+00:00,2009-04-19 20:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Pressure tested HPDR and 20"" casing to 20/195 bar 5/10 min - ok. volume pumped and bled back 2850 liter. Maintained 140 MT block weight when pressuring up and bleeding off. Observed sudden jump in block weight (10 MT) when pressuring up. Investigated and found that plug of cement had been released through the 30"" conductor cementing ports (observed by ROV).",1.0 +15_9_F_10_2009_04_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-19T00:00:00+02:00,2009-04-20T00:00:00+02:00,2009-04-19 20:00:00+00:00,2009-04-19 22:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Installed centralizers, plastic and brass bushings in Centralizer deck. Meanwhile released BOP NT-2 connector from stump.",2.0 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-19 22:00:00+00:00,2009-04-19 23:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Installed boat collision stool at Centralizer deck. Installed and alligned contact ring. Meanwhile released BOP NT-2 connector from stump.,1.5 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-19 23:30:00+00:00,2009-04-20 01:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Hooked up hydraulics to tension cylinders on Centralizer deck.,1.5 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 01:00:00+00:00,2009-04-20 04:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Installed tensioning assembly half hubs. Oriented half hubs. Made up half hubs to tension ring. Ran tension cylinders and coupled 2 ea to tensioning assembly.,3.0 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 04:00:00+00:00,2009-04-20 05:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Coupled 2 ea tension cylinders to tensioning assembly. Transfered tension from block to tensioning cylinders. Applied 90 bar on tension cylinders, i.e. 150 MT tension.",1.0 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 05:00:00+00:00,2009-04-20 05:15:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Held toolbox talk for releasing Claxton tool.,0.25 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 05:15:00+00:00,2009-04-20 06:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Broke studs on Claxton tool using J-gun. Pulled out Claxton tool and laid out same.,1.25 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 06:30:00+00:00,2009-04-20 08:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Modified scaffolding on Weatherdeck for skidding BOP. Meanwhile retrieved RLGF from seabed using port crane assisted by ROV. Retrieved 10MT guidewire/tugger.,2.0 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 08:30:00+00:00,2009-04-20 12:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Moved BOP to wellcenter, landed BOP on HPDR and started nipling up NT-2 connector. Made up swadge to TDS and tested upper/lower IBOP and kelly hose - ok.",3.5 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 12:00:00+00:00,2009-04-20 14:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Installed bell nipple and diverter.,2.0 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 14:00:00+00:00,2009-04-20 15:00:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,Got problems with HPU due to overheating of hydraulic oil. Reverted to planned maintenance activity on TDS. Changed springs on centralizer bearing and die carrier. Meanwhile allowed hydraulic oil on HPU to cool.,1.0 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 15:00:00+00:00,2009-04-20 18:00:00+00:00,140.0,m,fixed,drilling -- casing,ok,success,Made up pulling tool for nominal seat protector. RIH with NSP pulling tool from surface to 140 m MD. Latched onto NPS and pulled free with 10 MT overpull. Filled BOP with seawater. POOH with NSP from 140 m MD to surface. Set back RT with NSP.,3.0 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 18:00:00+00:00,2009-04-20 19:45:00+00:00,140.0,m,fixed,drilling -- casing,ok,success,"Picked up and made up 18 3/4"" BOP test plug. RIH with test plug and landed same in wellhead at 140 m MD.",1.75 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 19:45:00+00:00,2009-04-20 20:30:00+00:00,140.0,m,fixed,drilling -- bop activities,ok,success,Lined up cement unit and flushed line to trip tank. Lined up to BOP. Closed UPR. Tested BOP connector to 20/345 bar 5/10 min - ok. Volume pumped and bled back 450 liters.,0.75 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 20:30:00+00:00,2009-04-20 21:30:00+00:00,140.0,m,fixed,interruption -- maintain,ok,success,As part of planned maintenance ; changed 1 die block on TDS to slimmer type.,1.0 +15_9_F_10_2009_04_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-20T00:00:00+02:00,2009-04-21T00:00:00+02:00,2009-04-20 21:30:00+00:00,2009-04-20 22:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Picked up and made up RT/NSP and made up to stand of 5 1/2"" DP.",0.5 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-20 22:00:00+00:00,2009-04-20 23:30:00+00:00,140.0,m,fixed,drilling -- casing,ok,success,RIH with NSP to 140 m MD and set according to Vetco instructions.,1.5 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-20 23:30:00+00:00,2009-04-21 00:15:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,POOH with NSP RT from 140 m MD to surface. Broke and laid down RT.,0.75 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 00:15:00+00:00,2009-04-21 00:30:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Held toolbox talk for making up 17 1/2"" drilling BHA.",0.25 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 00:30:00+00:00,2009-04-21 03:30:00+00:00,55.0,m,fixed,drilling -- trip,ok,success,"Made up 17 1/2"" drilling BHA comprising of 17 1/2"" bit/PDX5/stab, Powerpulse, ARC, 17"" NM stab and stand of 9 1/2"" NMDC. Made up x-over to DC.",3.0 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 03:30:00+00:00,2009-04-21 04:00:00+00:00,55.0,m,fixed,drilling -- trip,ok,success,"Picked up stand of 8,25"" DC. Broke and laid out 8,25"" DC singles for onshore inspection.",0.5 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 04:00:00+00:00,2009-04-21 06:15:00+00:00,55.0,m,fixed,drilling -- trip,ok,success,"Broke and laid out 8,25"" DC singles. Ran stand of 8,25"" DC, broke and laid out 2 singels.",2.25 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 06:15:00+00:00,2009-04-21 08:30:00+00:00,115.0,m,fixed,drilling -- trip,ok,success,"Picked up and made up 2 x 8,25"" DC and jar. Picked up and made up 2x8,25"" DC and intensifier.",2.25 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 08:30:00+00:00,2009-04-21 08:45:00+00:00,115.0,m,fixed,drilling -- drill,ok,success,Removed master bushing and installed PS-21 slips.,0.25 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 08:45:00+00:00,2009-04-21 09:30:00+00:00,115.0,m,fixed,interruption -- other,ok,equipment failure,Found sheared bolt on actuator for PS-21. Removed PS-21 for repairs. Installed master bushing. Repaired PS-21 slips.,0.75 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 09:30:00+00:00,2009-04-21 09:45:00+00:00,194.0,m,fixed,drilling -- drill,ok,success,"RIH with 17 1/2"" drilling BHA on 5 1/2"" DP from 115 m to 194 m MD. Used manual slips. Meanwhile repaired PS-21 slips.",0.25 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 09:45:00+00:00,2009-04-21 11:00:00+00:00,194.0,m,fixed,interruption -- maintain,ok,success,Isolated TDS for maintenance. Changed out TDS centralizer bushings. Changed die carriers on TDS torque wrench.,1.25 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 11:00:00+00:00,2009-04-21 11:15:00+00:00,194.0,m,fixed,interruption -- other,ok,equipment failure,Removed masterbushing and installed PS-21 slips.,0.25 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 11:15:00+00:00,2009-04-21 13:00:00+00:00,1000.0,m,fixed,drilling -- drill,ok,success,"RIH with 17 1/2"" drilling BHA on 5 1/2"" DP from 194 m to 1000 m MD.",1.75 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 13:00:00+00:00,2009-04-21 13:45:00+00:00,1000.0,m,fixed,drilling -- drill,ok,success,Filled drillstring with SW. Tested MWD - ok.,0.75 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 13:45:00+00:00,2009-04-21 14:45:00+00:00,1323.0,m,fixed,drilling -- drill,ok,success,"RIH with 17 1/2"" drilling BHA on 5 1/2"" DP from 1000 m to 1323 m MD.",1.0 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 14:45:00+00:00,2009-04-21 15:30:00+00:00,1323.0,m,fixed,drilling -- drill,ok,success,Performed choke drill.,0.75 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 15:30:00+00:00,2009-04-21 15:45:00+00:00,1323.0,m,fixed,drilling -- drill,ok,success,"Held toolbox talk for drilling ahead and dispalcing to 1,40 SG OBM.",0.25 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 15:45:00+00:00,2009-04-21 17:00:00+00:00,1359.0,m,fixed,drilling -- drill,ok,success,Washed down from 1323 m and tagged top of cement/plugs at 1359 m MD. Parameters : Flow 3200 lpm / SPP 64 bar / 30 RPM / Torque 10-13 kNm.,1.25 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 17:00:00+00:00,2009-04-21 17:30:00+00:00,1359.0,m,fixed,drilling -- circulating conditioning,ok,success,Held toolbox talk / handover meeting.,0.5 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 17:30:00+00:00,2009-04-21 18:00:00+00:00,1359.0,m,fixed,drilling -- circulating conditioning,ok,success,Lined up for displacement and drained U-tube in surface equipement. Posted personnel.,0.5 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 18:00:00+00:00,2009-04-21 20:00:00+00:00,1359.0,m,fixed,drilling -- circulating conditioning,ok,success,"While drilling on wiper plugs at 1359 m MD - displaced well from SW to 1,40 sg OBM. Displaced mainfold and C/K lines to OBM. Drilling parameters : Flow 3200 lpm / SPP 60 bar increasing to 125 bar / 60 RPM / Torque 12 kNm decreasing to 8 kNm / WOB ~5 MT / ECD 1,38.",2.0 +15_9_F_10_2009_04_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-21T00:00:00+02:00,2009-04-22T00:00:00+02:00,2009-04-21 20:00:00+00:00,2009-04-21 22:00:00+00:00,1359.0,m,fixed,drilling -- casing,ok,success,Drilled on cement plugs at 1359 m MD. Little or no progress was made. Drilling parameters : Flow 3200 lpm / SPP 123 to 118 bar / 40-60 RPM / WOB 5-10 MT / Torque 9-12 kNm. When increasing WOB to 10 MT - observed high stick/slip on MWD.,2.0 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-21 22:00:00+00:00,2009-04-21 23:45:00+00:00,1360.0,m,fixed,drilling -- casing,ok,success,Drilled on cement plugs at 1359 m MD. Increased WOB to 15 MT. Drilling parameters : Flow 3200 lpm / SPP 115 bar / 40-70 RPM / WOB 6-15 MT / Torque 9-20 kNm. Meanwhile added barite to active to raise mudweight.,1.75 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-21 23:45:00+00:00,2009-04-22 00:15:00+00:00,1360.0,m,fixed,drilling -- casing,ok,success,"Bit stalled out at 35 kNm at 1360,6 m MD. Released torque in string. Worked string free with 20 MT overpull - string free with no excessive drag. Reamed tight area.",0.5 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 00:15:00+00:00,2009-04-22 03:30:00+00:00,1389.0,m,fixed,drilling -- casing,ok,success,"Drilled shoetrack from 1360 m to 1389,5 m MD. Drilling parameters : Flow 3200 lpm / SPP ~115 bar / 60 RPM / WOB ~5 MT / Torque 12-15 kNm / ECD 1,39 sg / ROP 12 m/hrs. Broke through shoe at 1389,7 m MD. Meanwhile rigged up Weatherford casing tong on drillfloor fore.",3.25 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 03:30:00+00:00,2009-04-22 04:00:00+00:00,1395.0,m,fixed,drilling -- casing,ok,success,"Cleaned out rathole down to 1393 m MD in increments of 2 m pulling back into shoe. Flow 3200 lpm / SPP ~115 bar / 60 RPM / WOB < 1 MT / Torque 6-10 kNm / ECD 1,39 sg.",0.5 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 04:00:00+00:00,2009-04-22 04:45:00+00:00,1400.0,m,fixed,drilling -- casing,ok,success,"Cleaned out 26"" rathole from 1393 m to 1400 m MD. Parameters : Flow 3200 lpm / SPP ~115 bar / 60 RPM / WOB < 1 MT / Torque 6-10 kNm / ECD 1,39 sg.",0.75 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 04:45:00+00:00,2009-04-22 05:15:00+00:00,1403.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 1400 m to 1403 m MD prior to FIT. Drilling paramaters : Flow 3200 lpm / SPP ~115 bar / 60 RPM / WOB 3 MT / Torque 11 kNm / ECD 1,39 sg.",0.5 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 05:15:00+00:00,2009-04-22 08:15:00+00:00,1403.0,m,fixed,formation evaluation -- circulating conditioning,ok,success,"Ciruclated 3 x bottoms up to get even mudweight 1,39 in/out prior to FIT. Reciprocated stand. Flow 4000 lpm / SPP 170 bar / 30 RPM.",3.0 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 08:15:00+00:00,2009-04-22 08:45:00+00:00,1403.0,m,fixed,formation evaluation -- circulating conditioning,ok,success,Pumped and spotted LCM pill across open hole at 2200 lpm / SPP 46 bar.,0.5 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 08:45:00+00:00,2009-04-22 10:00:00+00:00,1363.0,m,fixed,formation evaluation -- rft/fit,ok,success,POOH from 1403 m to 1363 m MD. Racked back stand. Made up kelly cock/side entry sub and flushed line. Tested line to 50 bar / 5 min - ok. Closed UPR.,1.25 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 10:00:00+00:00,2009-04-22 10:45:00+00:00,1363.0,m,fixed,formation evaluation -- rft/fit,ok,success,"Lined up to cement unit. Performed FIT to 1,60 EMW. Pumped 420 liter / CUP 29,6 bar. Bled back 460 liter.",0.75 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 10:45:00+00:00,2009-04-22 11:30:00+00:00,1363.0,m,fixed,drilling -- drill,ok,success,Broke out and laid down kelly cock/side entry sub. Lined up to standpipe. Took SCRs. Filled sandtraps.,0.75 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 11:30:00+00:00,2009-04-22 12:15:00+00:00,1403.0,m,fixed,drilling -- drill,ok,success,RIH to TD at 1403 m MD. Downlinked powerdrive prior to drilling ahead.,0.75 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 12:15:00+00:00,2009-04-22 12:45:00+00:00,1405.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" section from 1403 m to 1405 m MD. Drilling parameters : Flow 4000 lpm / SPP ~180 bar / 60 RPM / WOB 5 MT / Torque 8-10 kNm / ECD 1,39 sg.",0.5 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 12:45:00+00:00,2009-04-22 13:15:00+00:00,1405.0,m,fixed,drilling -- drill,ok,success,Cleared augers in shaker room due to stop/blockage. Auger stop caused by rubber.,0.5 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 13:15:00+00:00,2009-04-22 15:15:00+00:00,1443.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 1405 m to 1443 m MD. Drilling parameters : Flow 4000-4300 lpm / SPP 180-197 bar / 60-150 RPM / WOB 4-10 MT / Torque 6-16 kNm / ECD 1,39-1,40 sg. Set powerdrive to 342 deg / 100%. Observed no reposonse from powerdrive - hold and slight drop, no steering.",2.0 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 15:15:00+00:00,2009-04-22 17:15:00+00:00,1443.0,m,fixed,drilling -- drill,ok,success,"Discussed situation. Produced alternative well projections for drilling ahead one more stand. Set powerdrive to 270 deg / 100%. + +Meanwhile pulled off bottom and reciprocated stand. Paramaters : Flow 2500-3000 lpm / SPP 73-105 bar / 30 RPM / Torque 7 kNm / ECD 1,40-1,45 as determined by weighing up mud.",2.0 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 17:15:00+00:00,2009-04-22 18:30:00+00:00,1463.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 1443 m to 1463 m MD. Drilling parameters : Flow 4100 lpm / SPP ~195 bar / 120 RPM / WOB 2-7 MT / Torque 6-8 kNm / ECD 1,45-1,46 sg. Observed no left reposonse from powerdrive - hold and slight drop, no steering. Recessed drilling. Decided to POOH to change to back-up powerdrive.",1.25 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 18:30:00+00:00,2009-04-22 21:15:00+00:00,1453.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated hole clean and obtained even mudweight in/out. Parameters : Flow 4500 lpm / SPP~245 bar / Torque 6 kNm / ECD 1,47.",2.75 +15_9_F_10_2009_04_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-22T00:00:00+02:00,2009-04-23T00:00:00+02:00,2009-04-22 21:15:00+00:00,2009-04-22 22:00:00+00:00,1453.0,m,fixed,drilling -- trip,ok,success,Flowchecked - well static. Pumped slug for POOH.,0.75 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-22 22:00:00+00:00,2009-04-22 23:00:00+00:00,1435.0,m,fixed,drilling -- trip,ok,success,"POOH with 17 1/2"" BHA from 1453 m to 1435 m MD. Observed overpull of 10-15 MT at 1452 m MD. Worked string with 30 RPM as dictated overpull (10-15 MT) and torque (max 20 kNm). String free to move down. Normal drag obatained at 1435 m MD.",1.0 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-22 23:00:00+00:00,2009-04-23 01:45:00+00:00,174.0,m,fixed,drilling -- trip,ok,success,"POOH with 17 1/2"" BHA on 5 1/2"" DP from 1435 m to 174 m MD.",2.75 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 01:45:00+00:00,2009-04-23 02:15:00+00:00,174.0,m,fixed,drilling -- trip,ok,success,Flowchecked - well static. Filled triptanks.,0.5 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 02:15:00+00:00,2009-04-23 02:45:00+00:00,116.0,m,fixed,drilling -- trip,ok,success,"POOH with 17 1/2"" BHA on 5 1/2"" DP/HWDP from 174 m to 116 m MD. Removed PS-21 slips. Installed master bushing.",0.5 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 02:45:00+00:00,2009-04-23 04:00:00+00:00,116.0,m,fixed,drilling -- trip,ok,success,"Pulled and racked back stand of 8,25"" DC/intensifier and stand of 8,25"" DC/jar.",1.25 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 04:00:00+00:00,2009-04-23 04:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"POOH with 17 1/2"" BHA, racked on set back. Inspected bit and damaged Power Drive.",0.75 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 04:45:00+00:00,2009-04-23 05:00:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,Drill crew hand over.,0.25 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 05:00:00+00:00,2009-04-23 05:15:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Toolbox talk prior to handling BHA, rig tongs required.",0.25 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 05:15:00+00:00,2009-04-23 05:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,Cleared and cleaned rigfloor after POOH.,0.5 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 05:45:00+00:00,2009-04-23 06:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Broke off 17 1/2"" bit from damaged Power Drive. Bit to be re-run. L/D Power Drive on deck.",1.0 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 06:45:00+00:00,2009-04-23 07:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"P/U new Power Drive, made up bit.",1.0 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 07:45:00+00:00,2009-04-23 09:00:00+00:00,84.0,m,fixed,drilling -- trip,ok,success,RIH from surface to 84m.,1.25 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 09:00:00+00:00,2009-04-23 09:15:00+00:00,84.0,m,fixed,drilling -- trip,ok,equipment failure,Stopped due to uncertainty of float status. Toolbox talk prior to POOH to check float.,0.25 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 09:15:00+00:00,2009-04-23 11:00:00+00:00,4.0,m,fixed,drilling -- trip,ok,equipment failure,"POOH from 84m to 4m. Broke BHA, inspected float, twisted. Removed twisted float.",1.75 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 11:00:00+00:00,2009-04-23 13:30:00+00:00,27.0,m,fixed,drilling -- trip,ok,equipment failure,"RIH from 4m fo 27m, installed float sub and standard float on top of 17"" NM string stabilizer. Rig tongs required.",2.5 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 13:30:00+00:00,2009-04-23 14:45:00+00:00,115.0,m,fixed,drilling -- trip,ok,equipment failure,"RIH with 17 1/2"" BHA from 27m to 115m.",1.25 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 14:45:00+00:00,2009-04-23 15:15:00+00:00,115.0,m,fixed,drilling -- trip,ok,success,"Installed PS-21 slips dressed for 5 1/2"" DP.",0.5 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 15:15:00+00:00,2009-04-23 17:00:00+00:00,559.0,m,fixed,drilling -- trip,ok,success,RIH from 115m to 559m.,1.75 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 17:00:00+00:00,2009-04-23 17:15:00+00:00,559.0,m,fixed,drilling -- trip,ok,success,"Tool box talk with on comming shift prior to RIH with 17 1/2"" BHA on 5 1/2"" DP from 559m.",0.25 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 17:15:00+00:00,2009-04-23 18:45:00+00:00,1364.0,m,fixed,drilling -- trip,ok,success,"RIH from 559m to 1364m, emptying trip tank every 10 stand, filled pipe at 1000m.",1.5 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 18:45:00+00:00,2009-04-23 19:15:00+00:00,1406.0,m,fixed,drilling -- trip,ok,success,"Made up top drive and slided through 20"" casing shoe to 1406m. No restrictions observed.",0.5 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 19:15:00+00:00,2009-04-23 20:15:00+00:00,1463.0,m,fixed,drilling -- trip,ok,success,"Took up/down weight, 135/121 ton, free rotation weight, 50 rpm, 127 ton. Started pumps and rotation, 3200 l/min, 137 bar, 50 rpm, 8-10 kNm. Washed from 1406m to tagging depth 1463m.",1.0 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 20:15:00+00:00,2009-04-23 20:30:00+00:00,1463.0,m,fixed,drilling -- drill,ok,success,"Pulled 2m, established drilling parameters, 4300 l/min, 225 bar, 150 rpm, 8-10 kNm. Tagged with 2-4 ton, 4300 l/min, 228 bar, 150 rpm, 10-12 kNm.",0.25 +15_9_F_10_2009_04_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-23T00:00:00+02:00,2009-04-24T00:00:00+02:00,2009-04-23 20:30:00+00:00,2009-04-23 22:00:00+00:00,1495.0,m,fixed,drilling -- drill,ok,success,"Drilled from 1463m to 1495m, 4490 l/min, 240 bar, 160 rpm, 9-12 kNm, WOB 2-5 ton, ROP 18-20 m/hr.",1.5 +15_9_F_10_2009_04_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-24T00:00:00+02:00,2009-04-25T00:00:00+02:00,2009-04-23 22:00:00+00:00,2009-04-23 23:00:00+00:00,1515.0,m,fixed,drilling -- drill,ok,success,"Drilled from 1495m to 1515m, 4490 l/min, 240 bar, 160 rpm, 9-12 kNm, WOB 2-5 ton, ROP 15-20 m/hr.",1.0 +15_9_F_10_2009_04_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-24T00:00:00+02:00,2009-04-25T00:00:00+02:00,2009-04-23 23:00:00+00:00,2009-04-23 23:15:00+00:00,1516.0,m,fixed,drilling -- drill,ok,success,"Drilled with reduced ROP, 10 m/hr, due to problems with injection of cuttings.",0.25 +15_9_F_10_2009_04_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-24T00:00:00+02:00,2009-04-25T00:00:00+02:00,2009-04-23 23:15:00+00:00,2009-04-24 01:00:00+00:00,1516.0,m,fixed,drilling -- drill,ok,success,"Pulled off bottom and circulated, due to problems with cuttings injection. 3500 l/min, 153 bar, 60 rpm, 7-9 kNm. Reciprocated pipe.",1.75 +15_9_F_10_2009_04_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-24T00:00:00+02:00,2009-04-25T00:00:00+02:00,2009-04-24 01:00:00+00:00,2009-04-24 04:00:00+00:00,1567.0,m,fixed,drilling -- drill,ok,success,"Back on bottom for drilling 17 1/2"" hole from 1516m to 1567m. 4490 l/min, 240 bar, 160 rpm, 9-12 kNm, WOB 2-3 ton, ROP 19-20 m/hr. Meanwhile delivered cuttings to skip and trouble shot cuttings injecting system. Observed rubber in cutting pumps.",3.0 +15_9_F_10_2009_04_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-24T00:00:00+02:00,2009-04-25T00:00:00+02:00,2009-04-24 04:00:00+00:00,2009-04-24 09:45:00+00:00,1640.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 1567m to 1640m. 4490 l/min, 240 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 10-17 m/hr. +Simultaneously P/U and build 2 stands of 13 3/8"" casing set back. Malfunction occurred on alignment in FWD PRS. Emergency switch accidently activated during trouble shooting alignment problems on FWD PRS. Stop in operation while re-set (10 min).",5.75 +15_9_F_10_2009_04_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-24T00:00:00+02:00,2009-04-25T00:00:00+02:00,2009-04-24 09:45:00+00:00,2009-04-24 17:00:00+00:00,1734.0,m,fixed,drilling -- drill,ok,success,"Drilled and steared 17 1/2"" hole from 1640m to 1734m. 4490 l/min, 240 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr.",7.25 +15_9_F_10_2009_04_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-24T00:00:00+02:00,2009-04-25T00:00:00+02:00,2009-04-24 17:00:00+00:00,2009-04-24 22:00:00+00:00,1809.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 1734m to 1809m. 4490 l/min, 245 bar, 160 rpm, 12-15 kNm, WOB 3-5 ton, ROP 15-17 m/hr.",5.0 +15_9_F_10_2009_04_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-25T00:00:00+02:00,2009-04-26T00:00:00+02:00,2009-04-24 22:00:00+00:00,2009-04-25 01:45:00+00:00,1866.0,m,fixed,drilling -- drill,ok,success,"Drilled and steared 17 1/2"" hole from 1809m to 1866m. 4490 l/min, 250 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr.",3.75 +15_9_F_10_2009_04_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-25T00:00:00+02:00,2009-04-26T00:00:00+02:00,2009-04-25 01:45:00+00:00,2009-04-25 02:15:00+00:00,1866.0,m,fixed,drilling -- drill,ok,success,"Picked off bottom, circulated and reciprocated pipe while trouble shooting problems in cutting injection system. 3100 l/min, 140 bar, 60 rpm, 7-9 kNm.",0.5 +15_9_F_10_2009_04_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-25T00:00:00+02:00,2009-04-26T00:00:00+02:00,2009-04-25 02:15:00+00:00,2009-04-25 03:30:00+00:00,1884.0,m,fixed,drilling -- drill,ok,success,"Drilled and steared 17 1/2"" hole from 1866m to 1884m. 4490 l/min, 250 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr. Cuttings to skip, while cleaning slurry pump.",1.25 +15_9_F_10_2009_04_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-25T00:00:00+02:00,2009-04-26T00:00:00+02:00,2009-04-25 03:30:00+00:00,2009-04-25 04:00:00+00:00,1889.0,m,fixed,drilling -- drill,ok,success,"Drilled and steared 17 1/2"" hole from 1884m to 1889m. 4490 l/min, 250 bar, 160 rpm, 11-13 kNm. WOB 3-4 ton, ROP 15-17 m/hr. Cuttings pump back, injection re-established. +P/U and build 5 stands of 13 3/8"" casing and racked on set back during last 12 hrs.",0.5 +15_9_F_10_2009_04_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-25T00:00:00+02:00,2009-04-26T00:00:00+02:00,2009-04-25 04:00:00+00:00,2009-04-25 10:00:00+00:00,1970.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 1889m to 1970m. 4490 l/min, 250 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr. +Meanwhile MU 13 3/8"" csg in stands. 09:00 broke two bolts on flushjoint elevator tilt cylinder. Secured and repaired flush joint elevator.",6.0 +15_9_F_10_2009_04_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-25T00:00:00+02:00,2009-04-26T00:00:00+02:00,2009-04-25 10:00:00+00:00,2009-04-25 17:15:00+00:00,2062.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 1970m to 2062m. 4490 l/min, 253 bar, 160 rpm, 11-13 kNm. WOB 1-4 ton, ROP 15-17 m/hr. Plugging i CRI and conveyers. +Meanwhile repaired flushjoint elevator on fwd PRS.",7.25 +15_9_F_10_2009_04_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-25T00:00:00+02:00,2009-04-26T00:00:00+02:00,2009-04-25 17:15:00+00:00,2009-04-25 19:45:00+00:00,2062.0,m,fixed,drilling -- drill,ok,equipment failure,"Pulled off bottom due to plugging on CRI and cuttings conveyers. Circulated and reciprocated pipe, 3000 l/min, 125 bar, 60 rpm, 9 kNm while sorting out CRI and conveyers.",2.5 +15_9_F_10_2009_04_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-25T00:00:00+02:00,2009-04-26T00:00:00+02:00,2009-04-25 19:45:00+00:00,2009-04-25 22:00:00+00:00,2104.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 2062m to 2104m. 4490 l/min, 256 bar, 160 rpm, 11-13 kNm. WOB 2-4 ton, ROP 15-17 m/hr.",2.25 +15_9_F_10_2009_04_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-26T00:00:00+02:00,2009-04-27T00:00:00+02:00,2009-04-25 22:00:00+00:00,2009-04-26 01:45:00+00:00,2155.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 2104m to 2155m. 4490 l/min, 258 bar, 160 rpm, 11-13 kNm. WOB 2-4 ton, ROP 15-17 m/hr.",3.75 +15_9_F_10_2009_04_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-26T00:00:00+02:00,2009-04-27T00:00:00+02:00,2009-04-26 01:45:00+00:00,2009-04-26 02:00:00+00:00,2155.0,m,fixed,drilling -- drill,ok,success,"Pulled off bottom due to clearing CRI tank. Circulated and reciprocated pipe, 3000 l/min, 125 bar, 60 rpm, 9 kNm.",0.25 +15_9_F_10_2009_04_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-26T00:00:00+02:00,2009-04-27T00:00:00+02:00,2009-04-26 02:00:00+00:00,2009-04-26 04:00:00+00:00,2179.0,m,fixed,drilling -- drill,ok,success,"Drilled 17 1/2"" hole from 2155m to 2179m. 4490 l/min, 258 bar, 160 rpm, 11-13 kNm. WOB 3-5 ton, ROP 15-17 m/hr. +MU 3 stands of 13 3/8"" casing last 12 hrs.",2.0 +15_9_F_10_2009_04_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-26T00:00:00+02:00,2009-04-27T00:00:00+02:00,2009-04-26 04:00:00+00:00,2009-04-26 10:00:00+00:00,2267.0,m,fixed,drilling -- drill,ok,success,"Drilled and steered 17 1/2"" hole from 2179m to 2267m. 4490 l/min, 256 bar, 160 rpm, 11-13 kNm. WOB 2-4 ton, ROP 15-17 m/hr.",6.0 +15_9_F_10_2009_04_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-26T00:00:00+02:00,2009-04-27T00:00:00+02:00,2009-04-26 10:00:00+00:00,2009-04-26 17:00:00+00:00,2361.0,m,fixed,drilling -- drill,ok,success,"Drilled and steered 17 1/2"" hole from 2267m to 2361m. 4490 l/min, 258 bar, 160 rpm, 13-15 kNm. WOB 2-4 ton, ROP 15-17 m/hr.",7.0 +15_9_F_10_2009_04_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-26T00:00:00+02:00,2009-04-27T00:00:00+02:00,2009-04-26 17:00:00+00:00,2009-04-26 19:00:00+00:00,2385.0,m,fixed,drilling -- drill,ok,success,"Drilled and steered 17 1/2"" hole from 2361m to 2385m. 4530 l/min, 277 bar, 180 rpm, 13-15 kNm. WOB 2-4 ton, ROP 15-17 m/hr. Problem with mud pump.",2.0 +15_9_F_10_2009_04_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-26T00:00:00+02:00,2009-04-27T00:00:00+02:00,2009-04-26 19:00:00+00:00,2009-04-26 19:15:00+00:00,2385.0,m,fixed,interruption -- maintain,ok,equipment failure,Picked off bottom due to wash out in mud pump 1 piston. Lost suction on mud pumps. Lined up for drilling with 2 mud pumps. Lost suction on CRI pump.,0.25 +15_9_F_10_2009_04_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-26T00:00:00+02:00,2009-04-27T00:00:00+02:00,2009-04-26 19:15:00+00:00,2009-04-26 22:00:00+00:00,2414.0,m,fixed,drilling -- drill,ok,success,"Problem cleared. Drilled and steered 17 1/2"" hole from 2385m to 2414m. 4530 l/min, 277 bar, 180 rpm, 13-15 kNm. WOB 4-6 ton, ROP 15-17 m/hr.",2.75 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-26 22:00:00+00:00,2009-04-27 00:15:00+00:00,2432.0,m,fixed,drilling -- drill,ok,success,"Drilled and steered 17 1/2"" hole from 2414m to 2432m. 4500 l/min, 275 bar, 180 rpm, 13-23 kNm. WOB 6-8 ton, ROP 15-17 m/hr. MWD tool battery empty. All signals work when pumps on, no signal without pumping.",2.25 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-27 00:15:00+00:00,2009-04-27 00:30:00+00:00,2432.0,m,fixed,drilling -- drill,ok,success,Picked off bottom and reamed 1 joint due to stick slip and shocks at level 2 in BHA.,0.25 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-27 00:30:00+00:00,2009-04-27 04:00:00+00:00,2467.0,m,fixed,drilling -- drill,ok,success,"Drilled and steered 17 1/2"" hole from 2432m to 2467m. 4500 l/min, 275 bar, 160 rpm, 20-26 kNm. WOB 6-8 ton, ROP 10-15 m/hr. + +Simultaneously mU and racked 15 stands of 13 3/8"" casing in derrick over last 24 hrs, 27 stands in total.",3.5 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-27 04:00:00+00:00,2009-04-27 10:00:00+00:00,2550.0,m,fixed,drilling -- drill,ok,success,"Drilled and steered 17 1/2"" hole from 2467m to 2550m. 4500 l/min, 275 bar, 150 rpm, 17-19 kNm. WOB 4-7 ton, ROP 15-17 m/hr.",6.0 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-27 10:00:00+00:00,2009-04-27 11:30:00+00:00,2574.0,m,fixed,drilling -- drill,ok,success,"Drilled and steered 17 1/2"" hole from 2550m to 2574m. 4500 l/min, 275 bar, 150 rpm, 17-19 kNm. WOB 4-7 ton, ROP 15-17 m/hr.",1.5 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-27 11:30:00+00:00,2009-04-27 12:00:00+00:00,2574.0,m,fixed,drilling -- drill,ok,success,"Picked off bottom, serviced TDS, 2500 l/min, no rotation.",0.5 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-27 12:00:00+00:00,2009-04-27 15:30:00+00:00,2616.0,m,fixed,drilling -- drill,ok,success,"Drilled and steered 17 1/2"" hole from 2574m to 2616m, TD of section. 4500 l/min, 275 bar, 150 rpm, 17-19 kNm. WOB 4-7 ton, ROP 15-17 m/hr.",3.5 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-27 15:30:00+00:00,2009-04-27 16:45:00+00:00,2616.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated 2000 ltrs at bottom. 4500 l/min, 275 bar, 160 rpm, 17-19 kNm. 2,5m3/hr mud loss.",1.25 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-27 16:45:00+00:00,2009-04-27 19:45:00+00:00,2616.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated hole clean. 4490 l/min, 280 bar, 150 rpm, 12-14 kNm. Reciprocated pipe between 2616m and 2589m. Had 1,5m3/hr mud loss during circulation.",3.0 +15_9_F_10_2009_04_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-27T00:00:00+02:00,2009-04-28T00:00:00+02:00,2009-04-27 19:45:00+00:00,2009-04-27 22:00:00+00:00,2616.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated hole clean. 4490 l/min, 280 bar, 150 rpm, 12-14 kNm. Reciprocated pipe between 2616m and 2589m. Had 1m3/hr mud loss during circulation, increasing to 1,5m3/hr. Started to mix LCM pill.",2.25 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-27 22:00:00+00:00,2009-04-28 03:00:00+00:00,2616.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated hole while waiting on LCM pill mixing. 3500 l/min, 180 bar, 50 rpm, 12-14 kNm. Reciprocated pipe between 2616m and 2589m.",5.0 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-28 03:00:00+00:00,2009-04-28 03:30:00+00:00,2616.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated hole while waiting on hi-vis pill mixing. 3500 l/min, 180 bar, 50 rpm, 12-14 kNm. Reciprocated pipe between 2616m and 2589m.",0.5 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-28 03:30:00+00:00,2009-04-28 04:00:00+00:00,2535.0,m,fixed,drilling -- circulating conditioning,ok,success,-,0.5 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-28 04:00:00+00:00,2009-04-28 06:15:00+00:00,2351.0,m,fixed,drilling -- circulating conditioning,ok,success,"Pumped LCM pill as we pullled 17 1/2"" BHA from 2495m to 2351m. 900 l/min, 20 bar, no rotation.",2.25 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-28 06:15:00+00:00,2009-04-28 14:15:00+00:00,2328.0,m,fixed,drilling -- ream,ok,success,"Pulled from 2351m to 2328m. Observed 30 ton overpull. Observed pack off repetedly. Worked string from 2360m to 2328m, 0-4500 l/min, 0-270 bar, 0-120 rpm, 0-25 kNm, 0-30 ton over pull.",8.0 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-28 14:15:00+00:00,2009-04-28 16:30:00+00:00,2360.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated bottom up, 4500 l/min, 270 bar, 120 rpm, 10-13 kNm. Reciptocated pipe between 2360m and 2346m.",2.25 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-28 16:30:00+00:00,2009-04-28 17:30:00+00:00,2360.0,m,fixed,drilling -- circulating conditioning,ok,success,Pulled from 2360m to 2346m. No pumping no rotation. Pulled 2m lowered 1m in steps. Took weight at 2350m.,1.0 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-28 17:30:00+00:00,2009-04-28 20:00:00+00:00,2293.0,m,fixed,drilling -- circulating conditioning,ok,success,"Lowered string to 2356m, started to backream from 2356m to 2293m. Increased pumps tn steps to 2000 l/min, 65-70 bar, 80 rpm, 11-13 kNm. Layed out 1 joint of 5 1/2"" DP.",2.5 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-28 20:00:00+00:00,2009-04-28 21:30:00+00:00,2250.0,m,fixed,drilling -- ream,ok,success,"Back reamed from 2293m to 2250m with increased flow to 3600 l/min, 188-190 bar, 80 rpm, 12-15 kNm.",1.5 +15_9_F_10_2009_04_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-28T00:00:00+02:00,2009-04-29T00:00:00+02:00,2009-04-28 21:30:00+00:00,2009-04-28 22:00:00+00:00,2250.0,m,fixed,drilling -- circulating conditioning,ok,success,"Increased parameters to 4500 l/min, 275 bar, 180 rpm, 13-15 kNm.",0.5 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-28 22:00:00+00:00,2009-04-29 00:00:00+00:00,2250.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated 2 x bottom up, 4500 l/min, 275 bar, 180 rpm, 13-15 kNm. Observed increase in cuttings at shakers when 1 x bottom up. Reciprocated pipe between 2250m and 2213m.",2.0 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 00:00:00+00:00,2009-04-29 00:15:00+00:00,2213.0,m,fixed,drilling -- circulating conditioning,ok,success,"Flow checked well, 300 l/hr static loss.",0.25 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 00:15:00+00:00,2009-04-29 01:15:00+00:00,2090.0,m,fixed,drilling -- trip,ok,success,POOH from 2213m. Pulled 4 stands increasing over pull to 25-30 ton. Observed Trip tank 200 l above expected level. Checked level in drill string: 20m below RKB.,1.0 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 01:15:00+00:00,2009-04-29 02:45:00+00:00,2252.0,m,fixed,drilling -- circulating conditioning,ok,success,"RIH to 2248m, took 10-12 ton, started pumps in steps to 3600 l/hr, RIH to 2252m.",1.5 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 02:45:00+00:00,2009-04-29 03:00:00+00:00,2252.0,m,fixed,drilling -- circulating conditioning,ok,success,Flow checked prior to back reaming. 360 l/min static loss.,0.25 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 03:00:00+00:00,2009-04-29 03:30:00+00:00,2252.0,m,fixed,drilling -- ream,ok,success,"Established parameters for back reaming, 4500 l/min, 275 bar, 180 rpm, 12-14 kNm.",0.5 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 03:30:00+00:00,2009-04-29 04:00:00+00:00,2212.0,m,fixed,drilling -- ream,ok,success,"Back reamed from 2252m to 2212m. 4500 l/min, 275 bar, 180 rpm, 12-14 kNm.",0.5 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 04:00:00+00:00,2009-04-29 05:00:00+00:00,2090.0,m,fixed,drilling -- ream,ok,success,"Back reamed with 17 1/2"" BHA from 2212m to 2090m. 4500 l/min, 265 bar, 180 rpm, 12-14 kNm.",1.0 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 05:00:00+00:00,2009-04-29 05:15:00+00:00,2090.0,m,fixed,drilling -- circulating conditioning,ok,success,Set Power Drive to neutral.,0.25 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 05:15:00+00:00,2009-04-29 06:45:00+00:00,2013.0,m,fixed,drilling -- ream,ok,success,"Back reamed from 2090m to 2013m. 4500 l/min, 260 bar, 180 rpm, 12-14 kNm.",1.5 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 06:45:00+00:00,2009-04-29 08:15:00+00:00,2013.0,m,fixed,drilling -- circulating conditioning,ok,success,"Packed off stright afher connection. Took 10-15 ton over pull at 2013m. RIH to 2021m. Established circulation, staged pumps to 4500 l/min, 265 bar, 150 rpm, 10-15 kNm.",1.5 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 08:15:00+00:00,2009-04-29 11:45:00+00:00,1891.0,m,fixed,drilling -- ream,ok,success,"Circulated hole clean, reciprocated string from 2021m to 2035m. 4500 l/min, 265 bar, 150 rpm, 12-14 kNm. Lots of cuttings on shakers after 1 x bottom up. Circulated 4 x bottom up in total.",3.5 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 11:45:00+00:00,2009-04-29 12:45:00+00:00,1891.0,m,fixed,drilling -- circulating conditioning,ok,success,"Pumped out from 2021m to 1891m. 2500 l/min, 91 bar.",1.0 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 12:45:00+00:00,2009-04-29 13:00:00+00:00,1891.0,m,fixed,drilling -- circulating conditioning,ok,success,Attempted to POOH from 1891m without pumping. Took 20 tom over pull at 1889m.,0.25 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 13:00:00+00:00,2009-04-29 18:00:00+00:00,1449.0,m,fixed,drilling -- circulating conditioning,ok,success,"Pumped out from 1891m to 1449m. 4500 l/min, 250 bar.",5.0 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 18:00:00+00:00,2009-04-29 18:15:00+00:00,1367.0,m,fixed,drilling -- circulating conditioning,ok,success,"Reduced flow to 2000 l/min, 54 bar while pulling Power Drive into shoe and 1 stand into 20"" casing to 1367m..",0.25 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 18:15:00+00:00,2009-04-29 20:15:00+00:00,1367.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated 2 x bottom up at shoe, 4000 l/min, 175 bar.",2.0 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 20:15:00+00:00,2009-04-29 20:30:00+00:00,1367.0,m,fixed,drilling -- circulating conditioning,ok,success,"Flow checked well, 400 l/hr static loss. Simultaneously, checked and greased PRS.",0.25 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 20:30:00+00:00,2009-04-29 20:45:00+00:00,1367.0,m,fixed,drilling -- circulating conditioning,ok,success,"Pumped and displaced 4,7m3 1,75 sg slug.",0.25 +15_9_F_10_2009_04_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-29T00:00:00+02:00,2009-04-30T00:00:00+02:00,2009-04-29 20:45:00+00:00,2009-04-29 22:00:00+00:00,774.0,m,fixed,drilling -- circulating conditioning,ok,success,POOH from 1367m to 774m.,1.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-29 22:00:00+00:00,2009-04-29 23:00:00+00:00,196.0,m,fixed,drilling -- circulating conditioning,ok,success,"POOH with 17 1/2"" BHA from 774m to 196m.",1.0 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-29 23:00:00+00:00,2009-04-29 23:15:00+00:00,196.0,m,fixed,drilling -- circulating conditioning,ok,success,Flow checked well prior to pull BHA through BOP. Meanwhile removed PS 21 slips and installed master bushing.,0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-29 23:15:00+00:00,2009-04-29 23:30:00+00:00,196.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Operated BOP rams and annular.,0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-29 23:30:00+00:00,2009-04-29 23:45:00+00:00,196.0,m,fixed,drilling -- trip,ok,success,Tool Box Talk prior to pull and rack BHA.,0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-29 23:45:00+00:00,2009-04-30 00:30:00+00:00,85.0,m,fixed,drilling -- trip,ok,success,"Pulled and racked 17 1/2 "" BHA from 196m to 85m and racked on set back.",0.75 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 00:30:00+00:00,2009-04-30 01:30:00+00:00,85.0,m,fixed,interruption -- rig up/down,ok,equipment failure,Stop due to malfunction on fingers on finger board in derrick. Trouble shot.,1.0 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 01:30:00+00:00,2009-04-30 02:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"POOH with 17 1/2"" BHA from 85m to surface. B/O x-overs and layed down. Downloaded ARC tool as pr Schlumberger procedure. Racked 9 1/2"" stand on set back.",1.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 02:45:00+00:00,2009-04-30 03:00:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,Cleared and cleaned rigfloor.,0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 03:00:00+00:00,2009-04-30 03:15:00+00:00,0.0,m,fixed,drilling -- circulating conditioning,ok,success,Held Tool Box Talk prior to pick up wear bushing pulling tool and stand with jetsub.,0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 03:15:00+00:00,2009-04-30 04:00:00+00:00,38.0,m,fixed,drilling -- circulating conditioning,ok,success,"Picked 1 stand of 5 1/2"" HWDP and connected jet sub. RIH and jetted BOP.",0.75 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 04:00:00+00:00,2009-04-30 05:00:00+00:00,40.0,m,fixed,drilling -- casing,ok,success,"Picked up and run wear bushing pulling tool on top of 1 stand 5 1/2"" HWDP with jetting sub.",1.0 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 05:00:00+00:00,2009-04-30 05:15:00+00:00,40.0,m,fixed,drilling -- casing,ok,success,Held Tool Box Talk prior to RIH and retrieve wear bushing.,0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 05:15:00+00:00,2009-04-30 05:30:00+00:00,138.0,m,fixed,drilling -- casing,ok,success,"RIH from 40m to 138m. Dropped 2 3/4"" drift.",0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 05:30:00+00:00,2009-04-30 05:45:00+00:00,138.0,m,fixed,drilling -- casing,ok,success,"Jetted wear bushing prior to retrieving same. 2400 l/min, 40 bar, 2 rpm.",0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 05:45:00+00:00,2009-04-30 06:00:00+00:00,138.0,m,fixed,drilling -- casing,ok,success,"Latched on wear bushing. Took 8 ton over pull and pulled free. Measured from tooljoint to land off point, 8,70m.",0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 06:00:00+00:00,2009-04-30 07:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,POOH with wear bushing from 138m to surface.,1.0 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 07:00:00+00:00,2009-04-30 07:30:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,L/D wear bushing and 4 joints of HWDP. Retrieved drift.,0.5 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 07:30:00+00:00,2009-04-30 08:45:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Cleared and cleaned rigfloor.,1.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 08:45:00+00:00,2009-04-30 09:00:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,Lowered work platform and piston TDS.,0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 09:00:00+00:00,2009-04-30 09:15:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,Held Tool Box Talk prior to change washpipe.,0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 09:15:00+00:00,2009-04-30 11:15:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,"Changed washpipe on DDM. Leakage tested same to 240 bar, OK.",2.0 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 11:15:00+00:00,2009-04-30 11:30:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Held Tool Box Talk prior to rig up for running 13 3/8"" casing.",0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 11:30:00+00:00,2009-04-30 15:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Rigged up 13 3/8"" casing handling equipment.",3.5 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 15:00:00+00:00,2009-04-30 15:15:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Held Tool Box Talk prior to run 13 3/8"" casing.",0.25 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 15:15:00+00:00,2009-04-30 17:00:00+00:00,13.0,m,fixed,drilling -- casing,ok,success,"P/U 13 3/8"" casing shoe joint with reamer shoe and checked for flow through with water. Installed bypass baffle.",1.75 +15_9_F_10_2009_05_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-04-30T00:00:00+02:00,2009-05-01T00:00:00+02:00,2009-04-30 17:00:00+00:00,2009-04-30 22:00:00+00:00,290.0,m,fixed,drilling -- casing,ok,success,"Ran 13 3/8"" casing as per tally from 13m to 290m.",5.0 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-04-30 22:00:00+00:00,2009-05-01 04:00:00+00:00,794.0,m,fixed,drilling -- casing,ok,success,"Ran 13 3/8"" casing as per tally from 290m to 794m. Max running speed 10 joints per hour.",6.0 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 04:00:00+00:00,2009-05-01 10:30:00+00:00,1310.0,m,fixed,drilling -- casing,ok,success,"RIH with 13 3/8"" casing from 794 - 1315 m; held pre-job safety meeting with day crew, filled casing with 1.51 sg OBM every 5 joints.",6.5 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 10:30:00+00:00,2009-05-01 12:15:00+00:00,1310.0,m,fixed,drilling -- casing,ok,success,R/U and function tested Tesco CDS tool; held pre-job safety meeting with involved personnel prior to operations.,1.75 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 12:15:00+00:00,2009-05-01 12:30:00+00:00,1310.0,m,fixed,drilling -- casing,ok,success,Cleaned and tidied up rig floor.,0.25 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 12:30:00+00:00,2009-05-01 13:30:00+00:00,1382.0,m,fixed,drilling -- casing,ok,success,"RIH with stands of 13 3/8"" casing from 1310 - 1382 m; held pre-job safety meeting with involved personnel prior to operations, filled casing with 1.51 sg OBM as RIH.",1.0 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 13:30:00+00:00,2009-05-01 14:00:00+00:00,1382.0,m,fixed,drilling -- casing,ok,success,"Broke circulation and circulated casing with 1.51 sg OBM prior to running into open hole (1100 lpm, 13 bar).",0.5 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 14:00:00+00:00,2009-05-01 14:15:00+00:00,1382.0,m,fixed,drilling -- casing,ok,success,"P/U new stand of 13 3/8"" casing from derrick, unable to operate forward PRS.",0.25 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 14:15:00+00:00,2009-05-01 17:00:00+00:00,1382.0,m,fixed,interruption -- maintain,ok,equipment failure,Troubleshot PRS lower arm; replaced drilling control software.,2.75 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 17:00:00+00:00,2009-05-01 17:30:00+00:00,1382.0,m,fixed,drilling -- casing,ok,success,Performed toolbox talks with new crew; went through Tesco CDS tool operations.,0.5 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 17:30:00+00:00,2009-05-01 18:00:00+00:00,1382.0,m,fixed,interruption -- maintain,ok,equipment failure,Continued to troubleshot forward PRS; unable to lift upper arm.,0.5 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 18:00:00+00:00,2009-05-01 19:30:00+00:00,1418.0,m,fixed,drilling -- casing,ok,success,"RIH with stands of 13 3/8"" casing from 1382 - 1484 m; broke out and dressed threads on Tesco CDS tool due to alignement problems.",1.5 +15_9_F_10_2009_05_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-01T00:00:00+02:00,2009-05-02T00:00:00+02:00,2009-05-01 19:30:00+00:00,2009-05-01 22:00:00+00:00,1848.0,m,fixed,drilling -- casing,ok,success,"RIH with stands of 13 3/8"" casing from 1418 - 1848 m; filled casing with 1.51 sg OBM as RIH.",2.5 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-01 22:00:00+00:00,2009-05-02 00:45:00+00:00,2195.0,m,fixed,drilling -- casing,ok,success,"RIH with stands of 13 3/8"" casing from 1848 - 2195 m while simultaneously filling casing with 1.51 sg OBM, lost max 15 tons weight . Attempted to pass through obstruction at 2195 m, no-go.",2.75 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 00:45:00+00:00,2009-05-02 01:30:00+00:00,2210.0,m,fixed,drilling -- casing,ok,success,Broke circulation and gradually increased pump rate to 1000 lpm / 18 bar. Carefully washed down casing stand to 2210 m. Attempted to RIH with next casing stand without circulation; imediately lost weight.,0.75 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 01:30:00+00:00,2009-05-02 04:00:00+00:00,2235.0,m,fixed,drilling -- casing,ok,success,"Washed down with 13 3/8"" casing from 2210 - 2235 m (1500 lpm, 22 bar); lost max 15 tons weight, unable to pass through obstruction. Gradually increased pump rate from 1500 - 2000 lpm / 22 - 35 bar.",2.5 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 04:00:00+00:00,2009-05-02 06:00:00+00:00,2235.0,m,fixed,drilling -- casing,ok,success,"Circulated 13 3/8"" casing at 2000 lpm / 37 bar; had to restart circulation twice due to pack-off, max SPP 75 bar.",2.0 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 06:00:00+00:00,2009-05-02 10:15:00+00:00,2290.0,m,fixed,drilling -- casing,ok,success,"Washed / reamed 13 3/8"" casing down from 2235 - 2290 m; 2000 lpm, 16 - 35 bar, 1 rpm, 20 - 25 kNm. Observed increasing drag, packed off casing string at 2290 m.",4.25 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 10:15:00+00:00,2009-05-02 11:45:00+00:00,2290.0,m,fixed,drilling -- casing,ok,success,"Shut down pumps, worked casing string and re-established circulation. Gradually increased pump rate to 2500 lpm / 23 bar.",1.5 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 11:45:00+00:00,2009-05-02 16:00:00+00:00,2354.0,m,fixed,drilling -- casing,ok,success,"Washed / reamed 13 3/8"" casing down from 2290 - 2354 m (2500 lpm, 22 - 35 bar, 1 rpm, 20 - 25 kNm); set down max 15 tons on casing.",4.25 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 16:00:00+00:00,2009-05-02 16:45:00+00:00,2356.0,m,fixed,drilling -- casing,ok,success,"Established circulation after connection, worked casing down from 2354 - 2356 m; 2500 lpm, 22 - 35 bar, 1 rpm, 20 - 25 kNm. Packed off casing string at 2356 m.",0.75 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 16:45:00+00:00,2009-05-02 17:30:00+00:00,2354.0,m,fixed,drilling -- casing,ok,success,"Shut down pumps, worked casing string and gradually increased pump rate (2200 lpm, max SPP 40 bar, 1 rpm, max 25 kNm); packed off several times and finally lost returns.",0.75 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 17:30:00+00:00,2009-05-02 18:00:00+00:00,2354.0,m,fixed,drilling -- casing,ok,success,"Worked casing string and attempted to re-establish circulation, no-go.",0.5 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 18:00:00+00:00,2009-05-02 18:45:00+00:00,2354.0,m,fixed,drilling -- casing,ok,success,"Broke out wet and racked back 13 3/8"" casing stand in derrick; held pre-job safety meeting with involved personnel prior to operation. Broke casing coupling on box end; had to adjust Weatherford tong back-up jaws accordingly to prevent unscrewing coupling.",0.75 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 18:45:00+00:00,2009-05-02 21:15:00+00:00,2354.0,m,fixed,drilling -- casing,ok,success,POOH 5 m and verified casing string free. Gradually increased pump rate to 2500 lpm / 23 bar. Circulated BU while reciprocated casing string from 2354 - 2348 m; observed clean returns over shakers. M/U next casing stand.,2.5 +15_9_F_10_2009_05_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-02T00:00:00+02:00,2009-05-03T00:00:00+02:00,2009-05-02 21:15:00+00:00,2009-05-02 22:00:00+00:00,2357.0,m,fixed,drilling -- casing,ok,success,"Broke circulation and gradually increased pump rate. Washed 13 3/8"" casing down from 2354 - 2357 m; 2500 lpm, 23 bar.",0.75 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-02 22:00:00+00:00,2009-05-03 04:00:00+00:00,2462.0,m,fixed,drilling -- casing,ok,success,"Washed 13 3/8"" casing down from 2357 - 2462 m; 2500 lpm, 23 - 25 bar.",6.0 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 04:00:00+00:00,2009-05-03 05:00:00+00:00,2462.0,m,fixed,drilling -- casing,ok,success,"Circulated 13 3/8"" casing at 2500 lpm / 23 bar. Meanwhile held pre-job safety meeting with involved personnel prior to R/D Tesco tool and M/U casing hanger.",1.0 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 05:00:00+00:00,2009-05-03 06:00:00+00:00,2462.0,m,fixed,drilling -- casing,ok,success,"R/D Tesco CDS tool and changed to 5 1/2"" DP handling equipment.",1.0 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 06:00:00+00:00,2009-05-03 06:15:00+00:00,2462.0,m,fixed,drilling -- casing,ok,success,"M/U 13 3/8"" casing hanger assy.",0.25 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 06:15:00+00:00,2009-05-03 07:00:00+00:00,2462.0,m,fixed,drilling -- casing,ok,success,Removed FMS and installed master bushing. Meanwhile established circulation at 2000 lpm / 21 bar.,0.75 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 07:00:00+00:00,2009-05-03 07:30:00+00:00,2471.0,m,fixed,drilling -- casing,ok,success,"Washed down with 13 3/8"" casing from 2462 - 2471 m at 2000 lpm / 21 bar.",0.5 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 07:30:00+00:00,2009-05-03 07:45:00+00:00,2471.0,m,fixed,drilling -- casing,ok,success,R/D casing tong.,0.25 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 07:45:00+00:00,2009-05-03 15:15:00+00:00,2603.0,m,fixed,drilling -- casing,ok,success,"M/U first stand of 5 1/2"" HWDP. Broke circulation and gradually increased pump rate to 2430 lpm / 34 - 46 bar. Washed down with 13 3/8"" casing from 2471 - 2603 m on 5 1/2"" HWDP landing string.",7.5 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 15:15:00+00:00,2009-05-03 15:30:00+00:00,2603.0,m,fixed,drilling -- casing,ok,success,M/U cementing head.,0.25 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 15:30:00+00:00,2009-05-03 17:30:00+00:00,2607.5,m,fixed,drilling -- casing,ok,success,"Broke circulation and gradually increased pump rate to 2200 lpm / 44 bar. Washed down with 13 3/8"" casing from 2603 - 2607.5 m, landed hanger and set down casing weight + 8 tons.",2.0 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 17:30:00+00:00,2009-05-03 19:30:00+00:00,2607.5,m,fixed,drilling -- casing,ok,success,"Circulated and conditioned mud prior to casing cementing job; broke circulation and gradually increased pump rate to 2960 lpm / 64 bar, circulated a total of 1.2 x casing volumes. Mud weights in/out = 1.51 sg, no losses seen. Meanwhile held pre-job safety meeting with involved personnel prior to cementing operations; reviewed check lists and relevant safety / operational issues.",2.0 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 19:30:00+00:00,2009-05-03 20:00:00+00:00,2607.5,m,fixed,drilling -- casing,ok,success,"Pumped 8 m3 of base oil, followed by 20 m3 of 1.60 sg Tuned spacer E+ with rig pumps at 1200 - 1550 lpm. Displaced spacer to rig floor with 3 m3 of 1.51 sg OBM. Lined up to pump from cement unit, verified surface routing - OK.",0.5 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 20:00:00+00:00,2009-05-03 21:00:00+00:00,2607.5,m,fixed,drilling -- casing,ok,success,"Released bottom dart. Mixed and pumped 28 m3 of 1.90 sg cement slurry with cement unit at 800 - 900 lpm. Displaced surface cementing lines with 0.5 m3 drill water, released top dart. Flushed surface cementing lines with additional 1.5 m3 drill water. Lined up to pump 1.51 sg OBM with rig pumps.",1.0 +15_9_F_10_2009_05_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-03T00:00:00+02:00,2009-05-04T00:00:00+02:00,2009-05-03 21:00:00+00:00,2009-05-03 22:00:00+00:00,2607.5,m,fixed,drilling -- casing,ok,success,Started to displace cement slurry in place with rig pumps at 2960 lpm / 47 bar. Unable to verify bottom wiper plug land / shear.,1.0 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-03 22:00:00+00:00,2009-05-03 22:30:00+00:00,2607.5,m,fixed,drilling -- casing,ok,success,"Continued to displace cement slurry in place with rig pumps; recorded 20 bar pressure increase when cement spacer / slurry entered into open hole. Reduced pump rate to 1200 lpm / 27 bar prior to bumping top plug. No losses seen during the entire cementing and displacement operations. Bumped top wiper plug at 8704 strokes, corresponding to 96.2 % pump efficiency. Shut down pumps and observed pressure drop from 38 - 18 bar. Pumped additional 20 strokes and observed pressure increase from 18 - 31 bar with returns back to surface. Shut down pumps.",0.5 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-03 22:30:00+00:00,2009-05-03 22:45:00+00:00,2607.5,m,fixed,drilling -- casing,ok,success,"Bled off casing pressure; 0.4 m3 OBM in return, verified float - OK.",0.25 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-03 22:45:00+00:00,2009-05-04 00:30:00+00:00,2607.5,m,fixed,drilling -- casing,ok,success,Installed seal assembly according to Vetco procedure; held pre-job safety meeting with involved personnel prior to operations.,1.75 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 00:30:00+00:00,2009-05-04 03:30:00+00:00,2607.5,m,fixed,drilling -- casing,ok,success,Leak tested seal assembly to 35/300 bar for 5/15 min - OK.,3.0 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 03:30:00+00:00,2009-05-04 04:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Released PADRT and L/D cementing head.,0.5 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 04:00:00+00:00,2009-05-04 04:15:00+00:00,138.0,m,fixed,drilling -- casing,ok,success,Cleaned and tidied up rig floor.,0.25 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 04:15:00+00:00,2009-05-04 04:30:00+00:00,138.0,m,fixed,drilling -- casing,ok,success,"Installed 2 x sponge balls, wiped / flushed 5 1/2"" HWDP landing string at 660 lpm / 4 bar.",0.25 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 04:30:00+00:00,2009-05-04 06:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Retrieved casing landing string, L/D PADRT and 2 x 5 1/2"" HWDP joints. Held pre-job safety meeting with involved personnel prior to operations.",1.5 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 06:00:00+00:00,2009-05-04 06:30:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"R/D top drive air hose for Tesco CDS tool, removed excess casing handling equipment from rig floor.",0.5 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 06:30:00+00:00,2009-05-04 08:15:00+00:00,140.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"RIH with jet sub and WB assy, cleaned WH area at 1500 lpm / 10 bar.",1.75 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 08:15:00+00:00,2009-05-04 10:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Installed 13 3/8"" wear bushing; over-pull tested same 4 tons - OK. POOH and L/D WBRT.",1.75 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 10:00:00+00:00,2009-05-04 11:30:00+00:00,48.0,m,fixed,drilling -- bop activities,ok,success,M/U and RIH with BOP test tool; held pre-job safety meeting with involved personnel prior to operations.,1.5 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 11:30:00+00:00,2009-05-04 16:00:00+00:00,48.0,m,fixed,drilling -- bop activities,ok,success,Leak tested BOP and TDS IBOP`s to 20/345 bar for 5/10 min - OK.,4.5 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 16:00:00+00:00,2009-05-04 17:45:00+00:00,0.0,m,fixed,drilling -- bop activities,ok,success,"POOH with BOP test assy, L/D test tool, XO`s and jet sub.",1.75 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 17:45:00+00:00,2009-05-04 18:15:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Cleaned and tidied up rig floor. Meanwhile inspected / greased top drive.,0.5 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 18:15:00+00:00,2009-05-04 21:00:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,Cut and slipped drilling line; held pre-job safety meeting with involved personnel prior to operations. Calibrated crown and floor savers.,2.75 +15_9_F_10_2009_05_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-04T00:00:00+02:00,2009-05-05T00:00:00+02:00,2009-05-04 21:00:00+00:00,2009-05-04 22:00:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"L/D 17 1/2"" drilling BHA from derrick; inspected PRS dies / rollers and held pre-job safety meeting with involved personnel prior to operations.",1.0 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-04 22:00:00+00:00,2009-05-05 01:00:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Continued to L/D 17 1/2"" drilling BHA from derrick.",3.0 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 01:00:00+00:00,2009-05-05 01:15:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Cleaned and tidied up rig floor. Meanwhile prepared to P/U 12 1/4"" BHA.",0.25 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 01:15:00+00:00,2009-05-05 02:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Started to M/U 12 1/4"" BHA; held pre-job safety meeting with involved personnel prior to operations. Meanwhile prepared for casing test.",1.5 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 02:45:00+00:00,2009-05-05 03:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Leak tested surface lines to 35/300 bar for 5/10 min - OK. Meanwhile lifted BHA out of hole.,0.25 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 03:00:00+00:00,2009-05-05 03:45:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Attempted to leak test 13 3/8"" casing against shear rams with 1.51 sg OBM; pressure dropped at 90 bar and stabilised at 67 bar, 1250 ltr pumped when shutting down pump.",0.75 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 03:45:00+00:00,2009-05-05 04:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,equipment failure,"Bled off casing pressure, evaluated further operations.",0.25 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 04:00:00+00:00,2009-05-05 05:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,equipment failure,"Deactivated Schlumberger ARC tool, racked 12 1/4"" BHA stand in derrick.",1.0 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 05:00:00+00:00,2009-05-05 06:15:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"P/U 3 x 8 1/4"" DC`s from deck, M/U and racked stand in derrick; held pre-job safety meeting with involved personnel prior to operations.",1.25 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 06:15:00+00:00,2009-05-05 07:00:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Held pre-job safety meeting with involved personnel prior to P/U 5 1/2"" DP from deck. Moved rollers and changed to 5 1/2"" DP handling equipment.",0.75 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 07:00:00+00:00,2009-05-05 11:45:00+00:00,795.0,m,fixed,drilling -- trip,ok,success,"M/U and RIH with 5 1/2"" DP to 795 m; P/U single joints from deck.",4.75 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 11:45:00+00:00,2009-05-05 14:15:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"POOH with 5 1/2"" DP, racked same in derrick.",2.5 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 14:15:00+00:00,2009-05-05 15:30:00+00:00,0.0,m,fixed,drilling -- casing,ok,equipment failure,"Leak tested 13 3/8"" casing with 1.51 sg OBM to 55 bar, pumped 746 ltr, bled back 720 ltr - OK; held pre-job safety meeting with involved personnel prior to operations.",1.25 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 15:30:00+00:00,2009-05-05 16:00:00+00:00,0.0,m,fixed,drilling -- drill,ok,success,"Held pre-job safety meeting with involved personnel prior to M/U 12 1/4"" BHA, cleaned and tidied up rig floor.",0.5 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 16:00:00+00:00,2009-05-05 18:15:00+00:00,178.0,m,fixed,drilling -- trip,ok,success,"M/U and RIH with 12 1/4"" BHA; initialized Schlumberger ARC tool.",2.25 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 18:15:00+00:00,2009-05-05 19:45:00+00:00,600.0,m,fixed,drilling -- drill,ok,success,"RIH with BHA on 5 1/2"" DP from 178 - 600 m; filled pipe every 300 m.",1.5 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 19:45:00+00:00,2009-05-05 20:00:00+00:00,600.0,m,fixed,drilling -- other,ok,success,Function tested Schlumberger tools at 2300 lpm / 95 bar - OK.,0.25 +15_9_F_10_2009_05_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-05T00:00:00+02:00,2009-05-06T00:00:00+02:00,2009-05-05 20:00:00+00:00,2009-05-05 22:00:00+00:00,1550.0,m,fixed,drilling -- drill,ok,success,"RIH with BHA on 5 1/2"" DP from 600 - 1550 m; filled pipe every 300 m, performed kick drill with crew.",2.0 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-05 22:00:00+00:00,2009-05-06 00:00:00+00:00,2562.0,m,fixed,drilling -- drill,ok,success,"RIH with BHA on 5 1/2"" DP from 1550 - 2562 m; filled pipe every 300 m.",2.0 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 00:00:00+00:00,2009-05-06 00:30:00+00:00,2562.0,m,fixed,drilling -- drill,ok,success,"Broke circulation and gradually increased pump rate to 2300 lpm / 149 bar. Took up / down / free rotating torq = 167 / 133 / 148 tons, free rotating torq 13 - 16 kNm at 20 rpm. Meanwhile held pre-job safety meeting with involved personnel prior to mud displacement operations.",0.5 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 00:30:00+00:00,2009-05-06 00:45:00+00:00,2577.0,m,fixed,drilling -- drill,ok,success,"Washed down with BHA from 2562 m, tagged float at 2577 m.",0.25 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 00:45:00+00:00,2009-05-06 02:30:00+00:00,2578.0,m,fixed,drilling -- drill,ok,success,"Drilled cement wiper plugs and casing float from 2577 - 2578 m; 2780 lpm, 204 - 158 bar, 40 - 70 rpm, 14 - 17 kNm, 1 - 3 tons WOB. No indications of hard cement. Meanwhile displaced well to 1.30 sg OBM.",1.75 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 02:30:00+00:00,2009-05-06 04:00:00+00:00,2599.0,m,fixed,drilling -- drill,ok,success,"Drilled 13 3/8"" casing shoe track from 2578 - 2599 m; 2780 lpm, 154 - 158 bar, 70 rpm, 14 - 16 kNm, 0 - 3 tons WOB. No indications of hard cement.",1.5 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 04:00:00+00:00,2009-05-06 04:30:00+00:00,2599.0,m,fixed,drilling -- drill,ok,success,Displaced kill / choke lines to 1.30 sg OBM.,0.5 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 04:30:00+00:00,2009-05-06 08:30:00+00:00,2607.0,m,fixed,drilling -- drill,ok,success,"Drilled 13 3/8"" casing shoe / shoe track from 2599 - 2607 m (2780 lpm, 153 - 156 bar, 50 - 70 rpm, 13 - 19 kNm, 1 - 7 tons WOB); hard drilling from 2604 m.",4.0 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 08:30:00+00:00,2009-05-06 10:00:00+00:00,2616.0,m,fixed,drilling -- drill,ok,success,"Reamed / cleaned out rat hole from 2607 - 2616 m; 2780 lpm, 147 - 150 bar, 100 rpm, 13 - 16 kNm, 0 - 0.5 tons WOB.",1.5 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 10:00:00+00:00,2009-05-06 10:15:00+00:00,2619.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 2616 - 2619 m; 2780 lpm, 148 bar, 100 rpm, 16 - 18 kNm, 5 tons WOB.",0.25 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 10:15:00+00:00,2009-05-06 11:15:00+00:00,2599.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated and conditioned mud BU while reciprocating pipe (2780 lpm, 149 bar, 0 - 100 rpm, 0 - 16 kNm); MW in/out = 1.30 sg, clean returns over shakers. Pulled BHA above 13 3/8"" casing shoe.",1.0 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 11:15:00+00:00,2009-05-06 12:45:00+00:00,2599.0,m,fixed,formation evaluation -- rft/fit,ok,success,"Performed FIT to 1.4 sg EMW, pumping down pipe and annulus simultaneously; max 26 bar, pumped 361 ltr and bled back 330 ltr during test.",1.5 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 12:45:00+00:00,2009-05-06 13:30:00+00:00,2618.0,m,fixed,drilling -- drill,ok,success,"Washed / reamed down to 2618 m, took SCR`s. Monitored up / down / free rotating torq = 170 / 139 / 153 tons, free rotating torq 13 kNm / 20 rpm. Established drilling parameters; monitored ESD from ARC tool = 1.422 sg EMW.",0.75 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 13:30:00+00:00,2009-05-06 18:45:00+00:00,2719.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 2619 - 2719 m; 3500 lpm, 216 - 220 bar, WOB 5 - 8 tons, 170 rpm, 17 - 21 kNm, ECD 1.31 - 1.33 sg EMW, ESD 1.30 - 1.32 sg EMW, ROP 30 m/hr.",5.25 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 18:45:00+00:00,2009-05-06 19:00:00+00:00,2719.0,m,fixed,interruption -- wait,ok,success,Shut down rig power for generator maintenance.,0.25 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 19:00:00+00:00,2009-05-06 20:45:00+00:00,2758.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 2719 - 2758 m; 3500 lpm, 217 - 222 bar, WOB 5 - 8 tons, 170 rpm, 18 - 20 kNm, ECD 1.32 - 1.34 sg EMW, ESD 1.31 - 1.32 sg EMW, ROP 26 - 28 m/hr. Mud pumps shut down. +Meanwhile PU and racked 9 5/8"" stands in derrick.",1.75 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 20:45:00+00:00,2009-05-06 21:15:00+00:00,2758.0,m,fixed,interruption -- maintain,ok,equipment failure,"Troubleshot mud pumps; cleared filter for cooling of switchboard, resat electrical breaker switch. +Meanwhile PU and racked 9 5/8"" stands in derrick.",0.5 +15_9_F_10_2009_05_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-06T00:00:00+02:00,2009-05-07T00:00:00+02:00,2009-05-06 21:15:00+00:00,2009-05-06 22:00:00+00:00,2770.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 2758 - 2770 m; 3500 lpm, 217 - 222 bar, WOB 5 - 8 tons, 170 rpm, 18 - 20 kNm, ECD 1.33 - 1.34 sg EMW, ESD 1.31 - 1.32 sg EMW, ROP 26 - 30 m/hr. +Meanwhile PU and racked 9 5/8"" stands in derrick.",0.75 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-06 22:00:00+00:00,2009-05-07 00:00:00+00:00,2825.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 2770 - 2825 m; 3500 lpm, 221 - 223 bar, WOB 5 - 8 tons, 170 rpm, 18 - 23 kNm, ECD 1.33 - 1.34 sg EMW, ESD 1.31 - 1.32 sg EMW, ROP 30 - 32 m/hr. Unable to obtain directional control with Xceed tool. +Meanwhile PU and racked 9 5/8"" stands in derrick.",2.0 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 00:00:00+00:00,2009-05-07 00:30:00+00:00,2820.0,m,fixed,drilling -- trip,ok,equipment failure,"Picked off bottom and troubleshot Xceed tool; unable to obtain tool response on downlink commands, decided to POOH. +Meanwhile PU and racked 9 5/8"" stands in derrick.",0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 00:30:00+00:00,2009-05-07 02:45:00+00:00,2825.0,m,fixed,drilling -- trip,ok,equipment failure,"Circulated hole clean with 2 x BU; 3500 lpm, 223 bar, 80 - 130 rpm, 14 - 15 kNm. +Meanwhile completeted PU and racking 9 5/8"" stands in derrick. 9 stands made up totally. Status: 24 stands of 9 5/8"" casing in derrick.",2.25 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 02:45:00+00:00,2009-05-07 03:15:00+00:00,2800.0,m,fixed,drilling -- trip,ok,equipment failure,Set back last stand in derrick. Flow checked well on trip tank - OK.,0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 03:15:00+00:00,2009-05-07 04:00:00+00:00,2680.0,m,fixed,drilling -- trip,ok,equipment failure,"POOH wet with 12 1/4"" BHA from 2825 - 2680 m.",0.75 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 04:00:00+00:00,2009-05-07 04:30:00+00:00,2595.0,m,fixed,drilling -- trip,ok,equipment failure,"POOH wet to the shoe with 12 1/4"" BHA from 2680 m to 2595 m.",0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 04:30:00+00:00,2009-05-07 05:15:00+00:00,2595.0,m,fixed,drilling -- trip,ok,equipment failure,"Flowchecked well inside shoe at 2595 m. Lossrate 180 l/ hr. Meanwhile held TBT prior to POOH, checked PRS dies.",0.75 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 05:15:00+00:00,2009-05-07 05:45:00+00:00,2595.0,m,fixed,drilling -- trip,ok,equipment failure,"Pumped 5 m3 1,55 sg slug and filled trip tank. Removed mud bucket. Observed problem with drawwork motor.",0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 05:45:00+00:00,2009-05-07 06:15:00+00:00,2595.0,m,fixed,interruption -- repair,ok,equipment failure,Investigated problem with drawwork. Kept hard tripping in both directions.,0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 06:15:00+00:00,2009-05-07 09:30:00+00:00,178.0,m,fixed,drilling -- trip,ok,equipment failure,"POOH with 12 1/4"" BHA from 2598 m to 178 m. Slower pulling speed to 2196 m due to problem with drawwork. Rectified problem and de-assign motor #4.",3.25 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 09:30:00+00:00,2009-05-07 10:00:00+00:00,178.0,m,fixed,drilling -- trip,ok,equipment failure,"Flowchecked well prior to POOH with BHA, static. Meanwhile held TBT and removed PS-21 slips.",0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 10:00:00+00:00,2009-05-07 12:15:00+00:00,0.0,m,fixed,drilling -- trip,ok,equipment failure,"POOH with 12 1/4"" BHA from 178 m to surface. B/O 12 1/4"" bit and L/D Xceed tool.",2.25 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 12:15:00+00:00,2009-05-07 12:30:00+00:00,0.0,m,fixed,drilling -- trip,ok,equipment failure,Cleaned and cleared rig floor.,0.25 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 12:30:00+00:00,2009-05-07 13:15:00+00:00,19.0,m,fixed,drilling -- trip,ok,equipment failure,"TBT prior to P/U new Xceed tool. P/U new Xceed tool and M/U 12 1/4"" bit. RIH from surface to 19 m.",0.75 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 13:15:00+00:00,2009-05-07 14:30:00+00:00,0.0,m,fixed,drilling -- trip,ok,equipment failure,Downloaded data from telescope and Arc tools as per Schlumberger instructions.,1.25 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 14:30:00+00:00,2009-05-07 15:30:00+00:00,179.0,m,fixed,drilling -- trip,ok,equipment failure,"RIH with 12 1/4"" BHA from 19 m to 179 m.",1.0 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 15:30:00+00:00,2009-05-07 15:45:00+00:00,179.0,m,fixed,drilling -- trip,ok,equipment failure,Removed master bushing and installed PS-21 slips.,0.25 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 15:45:00+00:00,2009-05-07 16:15:00+00:00,620.0,m,fixed,drilling -- trip,ok,equipment failure,"RIH with 12 1/4"" BHA on 5 1/2"" DP from 179 m to 620 m.",0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 16:15:00+00:00,2009-05-07 16:45:00+00:00,620.0,m,fixed,drilling -- trip,ok,equipment failure,Filled pipe and shallow tested MWD tools with 2300 lpm/ 78 bar.,0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 16:45:00+00:00,2009-05-07 20:00:00+00:00,2595.0,m,fixed,drilling -- trip,ok,equipment failure,"RIH with 12 1/4"" BHA on 5 1/2"" DP from 620 m to 2595 m. Filled pipe every 600 m.",3.25 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 20:00:00+00:00,2009-05-07 20:30:00+00:00,2595.0,m,fixed,drilling -- trip,ok,equipment failure,Serviced TDS. Observed problem with Drawwork motors.,0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 20:30:00+00:00,2009-05-07 21:00:00+00:00,2595.0,m,fixed,interruption -- repair,ok,equipment failure,Investigated problem with drawwork motors. Rectified problem and de-assign motor # 2.,0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 21:00:00+00:00,2009-05-07 21:30:00+00:00,2761.0,m,fixed,drilling -- trip,ok,equipment failure,"RIH with 12 1/4"" BHA on 5 1/2"" DP from 2595 m to 2761 m.",0.5 +15_9_F_10_2009_05_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-07T00:00:00+02:00,2009-05-08T00:00:00+02:00,2009-05-07 21:30:00+00:00,2009-05-07 22:00:00+00:00,2780.0,m,fixed,drilling -- trip,ok,equipment failure,Reamed and washed down from 2761 m to 2780 m. Parameters; 3000 lpm/ 182 bar - 60 rpm/ 13 kNm.,0.5 +15_9_F_10_2009_05_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-08T00:00:00+02:00,2009-05-09T00:00:00+02:00,2009-05-07 22:00:00+00:00,2009-05-07 23:15:00+00:00,2825.0,m,fixed,drilling -- trip,ok,equipment failure,"Reamed and washed down from 2780 m to 2825 m, whilst setting toolface. Parameters; 3000 lpm/ 182 bar - 60 rpm/ 13 kNm.",1.25 +15_9_F_10_2009_05_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-08T00:00:00+02:00,2009-05-09T00:00:00+02:00,2009-05-07 23:15:00+00:00,2009-05-08 04:00:00+00:00,2902.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 2825 to 2902 m; 3500 lpm, 228 - 230 bar, WOB 6 - 14 tons, 170 rpm, 18 - 24 kNm, ECD 1.33 - 1.34 sg. ROP 25 m/hr. +Note: Hard formation from 2889 m to 2892 m. Started adding LCM mud into active when started drilling.",4.75 +15_9_F_10_2009_05_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-08T00:00:00+02:00,2009-05-09T00:00:00+02:00,2009-05-08 04:00:00+00:00,2009-05-08 22:00:00+00:00,3212.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 2902 to 3212 m; 3500 lpm, 225 - 230 bar, WOB 5 - 8 tons, 170 rpm, 18 - 25 kNm, ECD 1.34 - 1.36 sg. ROP 20-40 m/hr +Note: Hard stringers from 3013 m to 3022 m, 3153 m to 3156 m. Used different RPM and WOB parameters while drilling stringers. ROP in stringers: 2-5 m/hrs",18.0 +15_9_F_10_2009_05_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-09T00:00:00+02:00,2009-05-10T00:00:00+02:00,2009-05-08 22:00:00+00:00,2009-05-09 04:00:00+00:00,3280.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 3212 m to 3280 m; 3500 lpm, 227 - 230 bar, WOB 6 - 14 tons, 170 rpm, 18 - 30 kNm, ECD 1.34 - 1.35 sg. ROP 30-40 m/hr +Note: Hard stringers from 3227 m to 3229 m, 3262 m to 3280 m. Used different RPM and WOB parameters while drilling stringers. ROP in stringers: 2-5 m/ hrs.",6.0 +15_9_F_10_2009_05_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-09T00:00:00+02:00,2009-05-10T00:00:00+02:00,2009-05-09 04:00:00+00:00,2009-05-09 22:00:00+00:00,3309.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 3280 m to 3309 m; 3500 lpm, 221 - 222 bar, WOB 8 - 14 tons, 120 - 190 rpm, 18 - 30 kNm, ECD 1.33 - 1.34 sg. ROP 1- 4 m/hr +Note: Top Shetland and hard formation from 3266 m. Attempted to optimise ROP by using different RPM and WOB parameters.",18.0 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-09 22:00:00+00:00,2009-05-10 04:00:00+00:00,3315.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 3309 m to 3315 m; 3500 lpm, 219 - 222 bar, WOB 12 - 15 tons, 120 - 190 rpm, 18 - 26 kNm, ECD 1.33 - 1.34 sg. ROP 0,5 - 2 m/hr +Note: Top Shetland and hard formation from 3266 m. Attempted to optimise ROP by using different RPM and WOB parameters.",6.0 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 04:00:00+00:00,2009-05-10 10:30:00+00:00,3319.0,m,fixed,drilling -- drill,ok,success,"Drilled 12 1/4"" hole from 3315 m to 3319 m; 3500 lpm, 217 - 219 bar, WOB 12 - 15 tons, 120 - 190 rpm, 19 - 28 kNm, ECD 1.33 - 1.34 sg. ROP 0,5 - 1 m/hr. Had minor progress in ROP last 2 hours, and decided to POOH. +Note: Top Shetland and hard formation from 3266 m. Attempted to optimise ROP by using different RPM and WOB parameters.",6.5 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 10:30:00+00:00,2009-05-10 11:00:00+00:00,3319.0,m,fixed,drilling -- drill,ok,success,Flow checked well prior to POOH. Observed loss of 70 l/ 30 min.,0.5 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 11:00:00+00:00,2009-05-10 12:00:00+00:00,3083.0,m,fixed,drilling -- trip,ok,success,"POOH wet with 12 1/4"" BHA from 3319 m to 3083 m. Recorded up/ down weight prior to POOH; 185 ton/ 133 ton.",1.0 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 12:00:00+00:00,2009-05-10 12:15:00+00:00,3083.0,m,fixed,drilling -- trip,ok,success,"Pumped 5 m3 1,60 sg slug. Meanwhile checked PRS dies.",0.25 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 12:15:00+00:00,2009-05-10 12:45:00+00:00,2889.0,m,fixed,drilling -- trip,ok,success,"POOH with 12 1/4"" BHA on 5 1/2"" DP from 3083 m to 2889 m. Took weight at 2889 m, max OP 30 ton. +Note: 2889 m, limestone stringer at transition zone Heimdal/ Lista formations.",0.5 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 12:45:00+00:00,2009-05-10 14:15:00+00:00,2850.0,m,fixed,drilling -- trip,ok,success,Reamed tight area at 2889 m with no pump. String torqued up to 40 kNm/ 30 rpm. Established circulation with 500 lpm/ 39 bar. Increased flowrate stepwise to 3500 lpm/ 225 bar - 15 rpm/ 13 kNm. Pumped out from 2889 m to 2875 m.,1.5 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 14:15:00+00:00,2009-05-10 15:15:00+00:00,2595.0,m,fixed,drilling -- trip,ok,success,"POOH wet with 12 1/4"" BHA from 2875 m to 2595 m inside 13 3/8"" shoe. No obstruction in rest of OH and shoe area.",1.0 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 15:15:00+00:00,2009-05-10 15:45:00+00:00,2595.0,m,fixed,drilling -- trip,ok,success,"Flowchecked well inside shoe, static. Meanwhile performed service on TDS and aft PRS.",0.5 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 15:45:00+00:00,2009-05-10 16:00:00+00:00,2595.0,m,fixed,drilling -- trip,ok,success,"Pumped 5 m3 1,60 sg slug.",0.25 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 16:00:00+00:00,2009-05-10 16:30:00+00:00,2595.0,m,fixed,interruption -- maintain,ok,success,"Continued servicing TDS, PRS and drawwork.",0.5 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 16:30:00+00:00,2009-05-10 19:30:00+00:00,192.0,m,fixed,drilling -- trip,ok,success,"POOH with 12 1/4"" BHA on 5 1/2"" DP from 2595 m to 192 m.",3.0 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 19:30:00+00:00,2009-05-10 20:00:00+00:00,192.0,m,fixed,drilling -- trip,ok,success,Removed PS-21 slips and installed master bushing. Performed kick drill with involved personnel.,0.5 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 20:00:00+00:00,2009-05-10 20:15:00+00:00,192.0,m,fixed,drilling -- trip,ok,success,Flowchecked well prior to POOH with BHA. Meanwhile repaired loose connection on drawwork motor # 2.,0.25 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 20:15:00+00:00,2009-05-10 21:15:00+00:00,192.0,m,fixed,interruption -- other,ok,equipment failure,Continued to repair loose connection on drawwork motor # 2. Meanwhile observed well on trip tank.,1.0 +15_9_F_10_2009_05_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-10T00:00:00+02:00,2009-05-11T00:00:00+02:00,2009-05-10 21:15:00+00:00,2009-05-10 22:00:00+00:00,100.0,m,fixed,drilling -- trip,ok,success,"POOH with 12 1/4"" BHA from 192 m to 100 m.",0.75 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-10 22:00:00+00:00,2009-05-10 22:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"POOH with 12 1/4"" BHA from 100 m to surface. Racked same in derrick.",0.75 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-10 22:45:00+00:00,2009-05-10 23:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Gauged and inspected bit and BHA. Upper stabilizer had 1/32'' wear. In addition it was ringed out with a 4cm high and 2-3mm deep cut all around the stab approximately 1/3 from the bottom of it. The hard facing was still in place. The lower stab was worn 1/16''. Also here the hard facing was in place. Bit grading: 2-2-WT-S-IN-HC, some wear also on bit body. B/O bit and M/U new 12 1/4"" bit.",1.0 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-10 23:45:00+00:00,2009-05-11 01:15:00+00:00,178.0,m,fixed,drilling -- trip,ok,success,"RIH with 12 1/4"" BHA from surface to 178 m.",1.5 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 01:15:00+00:00,2009-05-11 01:45:00+00:00,178.0,m,fixed,drilling -- trip,ok,success,Removed master bushing and installed PS-21 slips.,0.5 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 01:45:00+00:00,2009-05-11 04:00:00+00:00,1992.0,m,fixed,drilling -- trip,ok,success,"RIH with 12 1/4"" BHA on 5 1/2"" DP from 178 m to 1992 m. Filled pipe every 600 m.",2.25 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 04:00:00+00:00,2009-05-11 05:00:00+00:00,2598.0,m,fixed,drilling -- trip,ok,success,"RIH with 12 1/4"" BHA on 5 1/2"" DP from 1992 m to 2598 m. Filled pipe every 600 m.",1.0 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 05:00:00+00:00,2009-05-11 05:30:00+00:00,2598.0,m,fixed,drilling -- bop activities,ok,success,Function test BOP rams. Flushed kill and choke lines inside shoe at 2598 m. Recorded up and down weight prior to RIH to OH; 170 ton/ 135 ton.,0.5 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 05:30:00+00:00,2009-05-11 06:15:00+00:00,2854.0,m,fixed,drilling -- trip,ok,success,"RIH with 12 1/4"" BHA on 5 1/2"" DP from 2598 m to 2854 m. Took weight at 2854 m, 20 ton down weight.",0.75 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 06:15:00+00:00,2009-05-11 08:00:00+00:00,2850.0,m,fixed,drilling -- ream,ok,success,"Washed/ reamed down from 2854 m to 2882 with 1000 lpm/ 25 bar - 50 RPM/ 14-23 kNm. Worked tight spots. Increased pumprate to 2900 lpm/ 166 bar. Backreamed stand to 2857 m and observed a pressure peak to 195 bar and packed off the hole. Resiprocated string and attempted to stage up flowrate slowly with 10 SPM, no return seen. Dry reamed out from 2857 m to 2850 m. Lost 2,5 m3 to formation.",1.75 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 08:00:00+00:00,2009-05-11 09:15:00+00:00,2850.0,m,fixed,drilling -- trip,ok,success,"Monitored well on triptank. Initial loss rate 12 m3/ hr and decreased to 1,1 m3/ hr. Total loss 8.2 m3.",1.25 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 09:15:00+00:00,2009-05-11 10:30:00+00:00,2850.0,m,fixed,drilling -- trip,ok,success,"Pumped and displaced 11 m3 LCM pill at 2850 m with 780 lpm/ 20 bar. Lost 6,5 m3 to formation while pumping LCM pill.",1.25 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 10:30:00+00:00,2009-05-11 11:00:00+00:00,2850.0,m,fixed,drilling -- trip,ok,success,Flowchecked well on triptank. Observed losses 400 l/ hr static losses.,0.5 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 11:00:00+00:00,2009-05-11 11:45:00+00:00,2676.0,m,fixed,drilling -- trip,ok,success,"POOH with 12 1/4"" BHA on 5 1/2"" DP from 2850 m to 2676 m.",0.75 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 11:45:00+00:00,2009-05-11 13:30:00+00:00,2676.0,m,fixed,drilling -- circulating conditioning,ok,success,"Established circulation at 2676 m. Increased flowrate slowly to 3500 lpm/ 220 bar, observed no loss to formation.",1.75 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 13:30:00+00:00,2009-05-11 14:15:00+00:00,2889.0,m,fixed,drilling -- trip,ok,success,"RIH with 12 1/4"" BHA on 5 1/2"" DP from 2676 m to 2889 m. Took 20 ton down weight at 2889 m.",0.75 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 14:15:00+00:00,2009-05-11 14:30:00+00:00,2900.0,m,fixed,drilling -- ream,ok,success,Reamed without pumping from 2889 m to 2900 m with 30 RPM. String torqued up and took weight.,0.25 +15_9_F_10_2009_05_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-11T00:00:00+02:00,2009-05-12T00:00:00+02:00,2009-05-11 14:30:00+00:00,2009-05-11 22:00:00+00:00,2995.0,m,fixed,drilling -- ream,ok,success,"Washed and reamed in hole from 2900 m to 2995 m. Parameters: 3500 lpm/ 224 bar. 30-60 RPM/ 20-25 kNm. Max torque 40 kNm. Staged pumps up slowly after each connection. Had several areas through claystone stringers with packing off tendency. Max standpipe pressure observed 230 bar. Claystone stringer from 2932 m to 2936 m, 2971 m to 2973 m.",7.5 +15_9_F_10_2009_05_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-12T00:00:00+02:00,2009-05-13T00:00:00+02:00,2009-05-11 22:00:00+00:00,2009-05-12 01:00:00+00:00,3025.0,m,fixed,drilling -- ream,ok,success,Washed and reamed in hole from 2995 m to 3025 m. Parameters: 3500 lpm/ 224 bar. 30-60 RPM/ 20-25 kNm. Max torque 40 kNm. Staged pumps up slowly after each connection. Had several areas through claystone stringers with packing off tendency. Max standpipe pressure observed 230 bar. Claystone stringer from 2999 m to 3001 m and from 3009 m to 3011 m.,3.0 +15_9_F_10_2009_05_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-12T00:00:00+02:00,2009-05-13T00:00:00+02:00,2009-05-12 01:00:00+00:00,2009-05-12 04:00:00+00:00,3139.0,m,fixed,drilling -- ream,ok,success,"Observed better hole condition from 3025 m. Washed and reamed in hole from 3025 m to 3139 m. Parameters: 3500 lpm/ 223 -225 bar, 50 RPM/ 14-21 kNm. Attempted to wash down without rotation at 3123 m, no go.",3.0 +15_9_F_10_2009_05_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-12T00:00:00+02:00,2009-05-13T00:00:00+02:00,2009-05-12 04:00:00+00:00,2009-05-12 09:00:00+00:00,3319.0,m,fixed,drilling -- ream,ok,success,"Washed and reamed in hole from 3129 mMD to 3319 mMD and tagged bottom. Parameters: 3500 lpm/ 223 -225 bar, 60 RPM/ 16-23 kNm.",5.0 +15_9_F_10_2009_05_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-12T00:00:00+02:00,2009-05-13T00:00:00+02:00,2009-05-12 09:00:00+00:00,2009-05-12 09:15:00+00:00,3319.0,m,fixed,drilling -- drill,ok,success,"Performed SCR readings at 3319 mMD/ 2642 mTVD with MW 1,30 sg. MP#2: 20 SPM/10 Bar - 30 SPM/ 14 Bar - 40 SPM/ 20 bar. MP#3: 20 SPM/ 9 Bar - 30 SPM/ 14 Bar - 40 SPM/ 20 Bar.",0.25 +15_9_F_10_2009_05_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-12T00:00:00+02:00,2009-05-13T00:00:00+02:00,2009-05-12 09:15:00+00:00,2009-05-12 22:00:00+00:00,3422.0,m,fixed,drilling -- drill,ok,success,"Established drilling parameters and drilled 12 1/4"" hole from 3319 m to 3422 m. Parameters: 3500 lpm/ 228 - 230 bar, 170 RPM/ 21-25 kNm, WOB: 7-13 ton, ROP: 5-13 m/hr, ECD: 1,34-1,35 sg.",12.75 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-12 22:00:00+00:00,2009-05-13 04:00:00+00:00,3433.0,m,fixed,drilling -- drill,ok,success,"Continued drilling 12 1/4"" hole from 3422 m to 3433 m. Parameters: 3500 lpm/ 225-232 bar, 170 RPM/ 21-30 kNm, WOB: 7-13 ton, ROP: 8-13 m/hr, ECD: 1,33-1,34 sg. +Note: Hard stringer at 3422 m and from 3428 m to 3433 m. ROP at stringer 1-3 m/hr.",6.0 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 04:00:00+00:00,2009-05-13 08:15:00+00:00,3437.0,m,fixed,drilling -- drill,ok,success,"Continued drilling 12 1/4"" hole from 3433 m to 3437 m. Parameters: 3500 lpm/ 229 bar, 170 - 190 RPM/ 17-22 kNm, WOB: 4-10 ton, ROP: 1-3 m/hr, ECD: 1,33 sg. Observed problem with mudpumps. +Note: Hard formation from 3433 m to 3437 m.",4.25 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 08:15:00+00:00,2009-05-13 09:45:00+00:00,3437.0,m,fixed,interruption -- maintain,ok,equipment failure,Troubleshot problems with mud pumps #1 and #2. Repaired liner spray.,1.5 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 09:45:00+00:00,2009-05-13 11:30:00+00:00,3442.0,m,fixed,drilling -- drill,ok,success,"Continued drilling 12 1/4"" hole from 3437 m to 3442 m, TD of section. Parameters: 3500 lpm/ 229 bar, 170 - 190 RPM/ 17-22 kNm, WOB: 4-10 ton, ROP: 1-4 m/hr, ECD: 1,33 sg. Observed softer formation from 3339 m and increased ROP from 1 m/hr to 4 m/hr. +Note: Hard formation from 3437 m to 3439 m.",1.75 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 11:30:00+00:00,2009-05-13 11:45:00+00:00,3442.0,m,fixed,drilling -- survey,ok,success,"Took survey at 3442 mMD, TD of section. Survey depth: 3426,62 mMD/ 2652,73 mTVD. Inc 85,4dgr - Az 121,89 dgr. Compared to plan: 3,8 m left/ 1,0 m high.",0.25 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 11:45:00+00:00,2009-05-13 13:30:00+00:00,3442.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated hole clean while resiprocated string at 3342 m. Parameters: 3500 lpm/ 235 bar, 80 RPM up and 160 RPM down/ 15-19 kNm.",1.75 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 13:30:00+00:00,2009-05-13 14:00:00+00:00,3442.0,m,fixed,drilling -- trip,ok,success,Flowchecked well on trip tank - static.,0.5 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 14:00:00+00:00,2009-05-13 14:15:00+00:00,3442.0,m,fixed,drilling -- trip,ok,success,Took up/ down WT and torque readings at 3432 m: 185 ton up/ 127 ton down. Torque: 22 kNm/ 10 RPM and 152 ton rot. WT.,0.25 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 14:15:00+00:00,2009-05-13 15:00:00+00:00,3243.0,m,fixed,drilling -- trip,ok,success,"POOH wet with 12 1/4"" BHA on 5 1/2"" DP from 3442 m to 3243 m.",0.75 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 15:00:00+00:00,2009-05-13 15:15:00+00:00,3243.0,m,fixed,drilling -- trip,ok,success,"Flowchecked well on trip tank, had initial losses 480 l/hr, but decreasing trend to 360 l/hr.",0.25 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 15:15:00+00:00,2009-05-13 15:45:00+00:00,3243.0,m,fixed,drilling -- trip,ok,success,"Dropped 3"" drift for 5 1/2"" DP. Pumped same down with 2000 lpm/ 87 bar and landed off with 136 bar.",0.5 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 15:45:00+00:00,2009-05-13 16:00:00+00:00,3243.0,m,fixed,drilling -- trip,ok,success,"Pumped and chased 5 m3 1,56 sg slug.",0.25 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 16:00:00+00:00,2009-05-13 17:00:00+00:00,2907.0,m,fixed,drilling -- trip,ok,success,"POOH with 12 1/4"" BHA on 5 1/2"" DP from 3243 m to 2907 m. Encountered tight spot at 2907 m, max OP 20 ton.",1.0 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 17:00:00+00:00,2009-05-13 18:00:00+00:00,2907.0,m,fixed,drilling -- ream,ok,success,"Attempted to rotate through tight spot at 2907 m, no go. Attempted to ream through with 500 lpm/ 10 bar, 20 RPM/ 14-30 kNm, no go. Observed signs of packing off.",1.0 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 18:00:00+00:00,2009-05-13 19:15:00+00:00,2880.0,m,fixed,drilling -- ream,ok,success,"Run in hole to 2920 m. Attempted to stage pumps up to 3500 lpm, no go. Observed 204 bar with 2500 lpm, previously had 136 bar with 2500 lpm. Probable due to drift in string. Reamed out of hole from 2920 m to 2880 m with 2750 lpm/ 244 bar, 30 RPM/ 15-18 kNm.",1.25 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 19:15:00+00:00,2009-05-13 20:45:00+00:00,2840.0,m,fixed,drilling -- ream,ok,success,"Attempted to pull on elevator from 2880 m, no go. Encountered tight spot at 2872 m, max OP 25 ton. Run in hole to 2880 m and M/U TDS. Attempted to rotate through tight spot at 2872 m, no go. Attempted to ream through with 500 lpm/ 18 bar, 20 RPM/ 14-30 kNm, no go. Reamed out of hole from 2880 m to 2840 m with 2750 lpm/ 245 bar, 30 RPM/ 15-25 kNm.",1.5 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 20:45:00+00:00,2009-05-13 21:30:00+00:00,2598.0,m,fixed,drilling -- trip,ok,success,"POOH wet with 12 1/4"" BHA on 5 1/2"" DP from 2840 m to 2598 m and into the 13 3/8"" shoe. No restriction observed in rest of OH or shoe area.",0.75 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 21:30:00+00:00,2009-05-13 21:45:00+00:00,2598.0,m,fixed,drilling -- trip,ok,success,"Flowchecked well on trip tank, static.",0.25 +15_9_F_10_2009_05_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-13T00:00:00+02:00,2009-05-14T00:00:00+02:00,2009-05-13 21:45:00+00:00,2009-05-13 22:00:00+00:00,2598.0,m,fixed,drilling -- trip,ok,success,"Took up/ down WT and torque readings at 2598 m: 172 ton up/ 136 ton down. Torque: 11-13 kNm/ 10 RPM, 10-14 kNm/ 20 RPM and 154 ton rot. WT.",0.25 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-13 22:00:00+00:00,2009-05-13 22:15:00+00:00,2598.0,m,fixed,drilling -- trip,ok,success,"Pumped and chased 5 m3 1,6 sg slug.",0.25 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-13 22:15:00+00:00,2009-05-13 23:45:00+00:00,2598.0,m,fixed,interruption -- wait,ok,success,Monitored well on trip tank while repairing ESD system on rig. Initial losses 100 l/hr.,1.5 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-13 23:45:00+00:00,2009-05-14 00:30:00+00:00,2598.0,m,fixed,drilling -- trip,ok,success,Serviced PRS and TDS.,0.75 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 00:30:00+00:00,2009-05-14 03:00:00+00:00,178.0,m,fixed,drilling -- trip,ok,success,"POOH with 12 1/4"" BHA on 5 1/2"" DP from 2598 m to 178 m.",2.5 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 03:00:00+00:00,2009-05-14 04:00:00+00:00,178.0,m,fixed,drilling -- trip,ok,success,"Flowchecked well on triptank prior to POOH with BHA, had initial losses 200 l/hr. Meanwhile removed PS-21 slips and installed master bushing. Rearranged pipe in derrick.",1.0 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 04:00:00+00:00,2009-05-14 06:45:00+00:00,178.0,m,fixed,interruption -- rig up/down,ok,equipment failure,"When rearranged drill collar stand in derrick, drill collar stand went stuck in the fingerboard. Troubleshot on same and sorted out the problem. Removed the stand.",2.75 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 06:45:00+00:00,2009-05-14 07:00:00+00:00,178.0,m,fixed,drilling -- trip,ok,success,"TBT prior to POOH with BHA with focus on manual handling, working in red zones and hand injuries.",0.25 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 07:00:00+00:00,2009-05-14 10:45:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"POOH with 12 1/4"" BHA from 178 m to surface. Racked HWDP and DC in derrick. Laid out remaining BHA components.",3.75 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 10:45:00+00:00,2009-05-14 11:00:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Inspected TDS for loose items, cleaned and cleared rig floor.",0.25 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 11:00:00+00:00,2009-05-14 11:15:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"TBT prior to R/U for running 9 5/8"" liner with focus on heavy lifts, pinch points and hand injuries.",0.25 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 11:15:00+00:00,2009-05-14 13:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"R/U to run 9 5/8"" liner. Meanwhile pressure tested CRI hose to 200 bar/ 10 min.",1.75 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 13:00:00+00:00,2009-05-14 13:15:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"TBT prior to run 9 5/8"" liner with focus on falling objects, barriers, red zones and M/U torque.",0.25 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 13:15:00+00:00,2009-05-14 19:45:00+00:00,911.0,m,fixed,drilling -- casing,ok,success,"RIH with 9 5/8"" liner from surface to 923 m. Floats tested in shoe joint. Filled every stand. Checked PRS and slip dies every 10 stands. Running speed: 142 m/ hr.",6.5 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 19:45:00+00:00,2009-05-14 20:00:00+00:00,911.0,m,fixed,drilling -- casing,ok,success,Hold tool box meeting with crew prior to P/U hanger.,0.25 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 20:00:00+00:00,2009-05-14 20:15:00+00:00,911.0,m,fixed,drilling -- casing,ok,success,Removed auto slips and installed master bushing.,0.25 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 20:15:00+00:00,2009-05-14 21:00:00+00:00,923.0,m,fixed,drilling -- casing,ok,success,"RIH with 9 5/8"" liner from 911 m to 923 m. Changed BX elevator to 6 5/8"" elevators.",0.75 +15_9_F_10_2009_05_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-14T00:00:00+02:00,2009-05-15T00:00:00+02:00,2009-05-14 21:00:00+00:00,2009-05-14 22:00:00+00:00,923.0,m,fixed,drilling -- casing,ok,success,"P/U 9 5/8"" hanger assy. Run MX ball seat assy into 9 5/8"" liner. Land off on C plate. M/U MX assy to running tool.",1.0 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-14 22:00:00+00:00,2009-05-14 23:30:00+00:00,923.0,m,fixed,drilling -- casing,ok,success,Performed pull test of hanger assy and running tool. Filled PBR with hi vis pill. Liner weight 55 ton.,1.5 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-14 23:30:00+00:00,2009-05-15 00:30:00+00:00,940.0,m,fixed,drilling -- casing,ok,success,Ran hanger assy through rotary. R/D casing tong and manual elevators.,1.0 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 00:30:00+00:00,2009-05-15 00:45:00+00:00,940.0,m,fixed,drilling -- casing,ok,success,M/U x-over and pup to running tool.,0.25 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 00:45:00+00:00,2009-05-15 01:15:00+00:00,940.0,m,fixed,drilling -- casing,ok,success,Changed out elevators and installed elevator rotator.,0.5 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 01:15:00+00:00,2009-05-15 01:45:00+00:00,940.0,m,fixed,drilling -- casing,ok,success,Made up DP stand to pup. Installed auto slips.,0.5 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 01:45:00+00:00,2009-05-15 04:00:00+00:00,1867.0,m,fixed,drilling -- casing,ok,success,"RIH with 9 5/8"" liner on 5 1/2"" DP from 940 m to 1867 m. Filled every 5 stands. Running speed 412 m/ hr. Total losses while RIH with 9 5/8"" liner from surface to 1867 m; 7,6 m3. Losstrend is decreasing.",2.25 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 04:00:00+00:00,2009-05-15 06:00:00+00:00,2595.0,m,fixed,drilling -- casing,ok,success,"RIH with 9 5/8"" liner on 5 1/2"" DP from 1867 m to 2595 m. Filled every 5 stands. Running speed 364 m/ hr. Took up and down weight inside shoe at 2595 m, 185 ton/ 138 ton.",2.0 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 06:00:00+00:00,2009-05-15 06:45:00+00:00,2595.0,m,fixed,drilling -- casing,ok,success,At 2595 m broke circulation and increased flowrate stepwise to 2000 lpm/ 46 bar. Meanwhile serviced Iron roughneck.,0.75 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 06:45:00+00:00,2009-05-15 07:15:00+00:00,2595.0,m,fixed,interruption -- other,ok,equipment failure,Repaired hydraulic leak on aft iron roughneck. Meanwhile continued circulated with 1500 lpm/ 31 bar. Total pumped in shoe: 88 m3.,0.5 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 07:15:00+00:00,2009-05-15 08:15:00+00:00,2863.0,m,fixed,drilling -- casing,ok,success,"RIH with 9 5/8 liner on 5 1/2"" DP from 2595 m to 2863 m. Took weight at 2863 m, max down weight 40 ton.",1.0 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 08:15:00+00:00,2009-05-15 11:15:00+00:00,2865.0,m,fixed,drilling -- casing,ok,success,"Attempted to wash through tight spot at 2863 m, no go.Parameters: 500 - 750 lpm/ 20 bar. Washed/ rotated liner down from 2863 m to 2865 m. Parameters: 1000 lpm/ 21 bar - 15 RPM/ 15-30 kNm.",3.0 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 11:15:00+00:00,2009-05-15 13:00:00+00:00,3401.0,m,fixed,drilling -- casing,ok,success,"RIH with 9 5/8"" liner on 5 1/2"" DP from 2865 m to 3401 m.",1.75 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 13:00:00+00:00,2009-05-15 13:30:00+00:00,3440.0,m,fixed,drilling -- casing,ok,success,Washed down last stand from 3401 m to 3440 m with 400 lpm/ 17 bar. Recorded up and down weight at setting depth; 195 ton/ 134 ton.,0.5 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 13:30:00+00:00,2009-05-15 13:45:00+00:00,3440.0,m,fixed,drilling -- casing,ok,success,P/U and M/U cement head.,0.25 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 13:45:00+00:00,2009-05-15 14:00:00+00:00,3440.0,m,fixed,drilling -- casing,ok,success,"Washed in hole to TD at 3442 m with 400 lpm. Set down 10 ton. Pulled out to up weight and additional 2 m to 3439 m. Estimated loss of 14 m3, while RIH with 9 5/8"" liner from surface to TD.",0.25 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 14:00:00+00:00,2009-05-15 16:00:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,"Circulated at setting depth of the liner at 3439 m. Increased flowrate stepwise to 1200 lpm/ 35 bar, and loss free rate. Total pumped 100 m3, one OH volume.",2.0 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 16:00:00+00:00,2009-05-15 17:00:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,"Dropped ball from the cement head and chased the ball down with 500 lpm/ 14 bar. Ball landed in ball seat with 166 bar and after pumped 13,5 m3. Verified hanger set by slacking off to 30 ton down weight. Bleed off pressure. Pulled up and left 10 ton weight on RT.",1.0 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 17:00:00+00:00,2009-05-15 17:30:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,Released running tool with 11 turns clockwise. P/U to free weight and 1 additional meter to check that running tool was free and activated MX ball seat. Slacked off 20 ton to shear out ball seat.,0.5 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 17:30:00+00:00,2009-05-15 18:45:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,Staged up pumps to 2000 lpm/ 63 bar without losses.,1.25 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 18:45:00+00:00,2009-05-15 20:45:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,"Reduced flowrate to 500 lpm, 16 bar. Established rotation 20 RPM/ 19-23 kNm. Increased flowrate to 2000 lpm/ 65 bar. Circulated BU with loss free circulation. Meanwhile held TBT with focus on cement job.",2.0 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 20:45:00+00:00,2009-05-15 21:00:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,"Pumped 15 m3 0,83 sg base oil with rig pump.",0.25 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 21:00:00+00:00,2009-05-15 21:45:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,"Pumped 20 m3 1,3 sg Spacer with rig pump. Chased spacer with 3 m3 OBM, which meant 1,5 m3 spacer behind cement.",0.75 +15_9_F_10_2009_05_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-15T00:00:00+02:00,2009-05-16T00:00:00+02:00,2009-05-15 21:45:00+00:00,2009-05-15 22:00:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,Dropped lower SSR dart for bottom wiper plug. Confirmed same with flag.,0.25 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-15 22:00:00+00:00,2009-05-15 23:00:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,"Mixed and pumped 38 m3 1,90 sg cement slurry with 800 lpm/ 49-36 bar, 20 RPM/ 17-30 kNm. Displaced cement to rig floor with 890 liter fresh water. Dropped upper SSR dart for top wiper plug. Confirmed same with flag.",1.0 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-15 23:00:00+00:00,2009-05-16 00:00:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,"Displaced cement with OBM. Pumped with 2000 lpm - 20 rpm/ 28-42 kNm. Observed top dart at wiper plug at 1290 strokes, calculated stroke with 96 % efficiency were 1227 stroke. Top dart sheared out at 216 bar. No bump observed after 2770 strokes. Pumped totally 60,7 m3. Total losses during cement job 8,5 m3. Unable to rotate string after 2000 strokes displaced volume. Bleed off and checked for back flow, none observed.",1.0 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 00:00:00+00:00,2009-05-16 00:45:00+00:00,3439.0,m,fixed,drilling -- casing,ok,success,"Set TSP packer according to Weatherford prosedure. Closed annular, and pressure up annulus to 200 bar for 5 min and tested TSP packer.",0.75 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 00:45:00+00:00,2009-05-16 01:15:00+00:00,2508.0,m,fixed,drilling -- casing,ok,success,Pressured up to 25 bar. Released RSM by pulling out 16 m with running tool.,0.5 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 01:15:00+00:00,2009-05-16 02:30:00+00:00,2508.0,m,fixed,drilling -- casing,ok,success,Circulated out excess cement with 3000 lpm/ 90 bar. Observed spacer but no cement in return.,1.25 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 02:30:00+00:00,2009-05-16 03:15:00+00:00,2508.0,m,fixed,drilling -- casing,ok,success,B/O cement head. Observed backflow from string. Reinstalled cement head on string.,0.75 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 03:15:00+00:00,2009-05-16 04:00:00+00:00,2508.0,m,fixed,drilling -- casing,ok,success,Continued circulating to prevent backflow 3000 lpm/ 91 bar.,0.75 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 04:00:00+00:00,2009-05-16 05:30:00+00:00,2508.0,m,fixed,drilling -- casing,ok,success,"Circulated and conditioned mud with RT inside PBR at 2508 m. 3000 lpm/ 90 bar. Observed for backflow, none.",1.5 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 05:30:00+00:00,2009-05-16 05:45:00+00:00,2508.0,m,fixed,drilling -- casing,ok,success,B/O cement head and single and loaded sponge balls.,0.25 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 05:45:00+00:00,2009-05-16 06:15:00+00:00,2508.0,m,fixed,drilling -- casing,ok,success,Pumped down sponge balls to clean DP with 3000 lpm/ 90 bar.,0.5 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 06:15:00+00:00,2009-05-16 06:30:00+00:00,2508.0,m,fixed,drilling -- casing,ok,success,"Flow checked well, static.",0.25 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 06:30:00+00:00,2009-05-16 06:45:00+00:00,2508.0,m,fixed,drilling -- casing,ok,success,"Pumped 5 m3 1,60 sg slug, chased with OBM.",0.25 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 06:45:00+00:00,2009-05-16 08:15:00+00:00,2461.0,m,fixed,drilling -- casing,ok,success,"L/D cement head with one single on catwalk, disconnected hoses on same. POOH and racked back one stand with 5 1/2"" DP. P/U cement head and 1single from catwalk. RIH with single DP, B/O and L/D cement head.",1.5 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 08:15:00+00:00,2009-05-16 10:15:00+00:00,38.0,m,fixed,drilling -- casing,ok,success,"POOH with liner hanger RT on 5 1/2"" DP from 2461 m to 38 m. (1212 m/ hr.)",2.0 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 10:15:00+00:00,2009-05-16 10:30:00+00:00,38.0,m,fixed,drilling -- casing,ok,success,Removed PS-21 slips and installed master bushing.,0.25 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 10:30:00+00:00,2009-05-16 11:30:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,POOH with liner hanger RT from 38 m to surface. L/D liner hanger RT.,1.0 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 11:30:00+00:00,2009-05-16 11:45:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Cleaned and cleared rig floor.,0.25 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 11:45:00+00:00,2009-05-16 12:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Held TBT prior to RIH with jet sub and test plug.,0.25 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 12:00:00+00:00,2009-05-16 13:45:00+00:00,180.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"RIH with jetsub and 1 std 5 1/2"" DP. MU testplug on top of stand and RIH to 139 m. Jetted wearbushing and landed off test plug at 139 m, jetsub depth 180 m.",1.75 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 13:45:00+00:00,2009-05-16 15:45:00+00:00,180.0,m,fixed,drilling -- bop activities,ok,equipment failure,"Attempted to pressure test 18 3/4"" BOP, no go. Had leakage at cement unit. Greased up valves at cement unit.",2.0 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 15:45:00+00:00,2009-05-16 21:30:00+00:00,180.0,m,fixed,drilling -- bop activities,ok,success,Pressure tested 18 3/4 BOP to 30 bar/ 5 min - 345 bar/ 10 min. Meanwhile drifted DP in derrick.,5.75 +15_9_F_10_2009_05_17.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-16T00:00:00+02:00,2009-05-17T00:00:00+02:00,2009-05-16 21:30:00+00:00,2009-05-16 22:00:00+00:00,100.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,POOH with jetsub/ testplug from 180 m to 100 m.,0.5 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-16 22:00:00+00:00,2009-05-16 23:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,POOH with testplug assy from 100 m to surface. L/D testplug and jetsub.,1.0 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-16 23:00:00+00:00,2009-05-17 00:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Held TBT prior to test 9 5/8"" liner. Attempted to test 9 5/8"" liner to 300 bar, no go. Pressured up to 240 bar. Pressure seemed to start leaking at 180 bar. After pressured up to 240 bar, pressure dropped to 231 bar in 2 min. Bleed off pressure. +Meanwhile continued drifting DP in derrick and preparing 8 1/2"" BHA.",1.0 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 00:00:00+00:00,2009-05-17 04:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,Continued WOC for testing of liner. Meanwhile changed washpipe and saversub on TDS. Leak tested washpipe to 200 bar.,4.0 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 04:00:00+00:00,2009-05-17 09:00:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Continued WOC for pressure testing entire well. Meanwhile changed saversub on TDS. Rearranged fingerboard and M/U jar and accelerator on 5"" HWDP. Racked same in derrick.",5.0 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 09:00:00+00:00,2009-05-17 09:15:00+00:00,0.0,m,fixed,drilling -- casing,ok,success,"Held TBT prior to pressure test of 9 5/8"" liner. Confirmed line up and flushed lines.",0.25 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 09:15:00+00:00,2009-05-17 10:30:00+00:00,0.0,m,fixed,drilling -- casing,ok,operation failed,"Attempted to pressure test entire well to 300 bar, no go. Pressured up to 250 bar. Observed a steady leakrate of 5 bar/ min. Total pumped 5 m3/ bled back 3,5 m3.",1.25 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 10:30:00+00:00,2009-05-17 11:00:00+00:00,0.0,m,fixed,interruption -- other,ok,operation failed,"Prepared RTTS assy. Performed TBT prior to P/U and M/U 9 5/8"" RTTS assy.",0.5 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 11:00:00+00:00,2009-05-17 12:00:00+00:00,19.0,m,fixed,interruption -- other,ok,operation failed,"P/U and M/U 9 5/8"" RTTS assy with 5 1/2"" pup and drift sub. RIH with same from surface to 19 m. Confirmed and lock circ tool in open position.",1.0 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 12:00:00+00:00,2009-05-17 12:15:00+00:00,19.0,m,fixed,interruption -- other,ok,operation failed,Removed master bushing and installed PS-21 slips.,0.25 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 12:15:00+00:00,2009-05-17 15:00:00+00:00,2078.0,m,fixed,interruption -- other,ok,operation failed,"RIH with 9 5/8"" RTTS assy on 5 1/2"" DP from 19 m to 2078 m. ( 748 m/ hr)",2.75 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 15:00:00+00:00,2009-05-17 15:15:00+00:00,2078.0,m,fixed,interruption -- other,ok,operation failed,Broke circulation with 500 lpm/ 11 bar.,0.25 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 15:15:00+00:00,2009-05-17 18:00:00+00:00,3306.0,m,fixed,interruption -- other,ok,operation failed,"RIH with 9 5/8"" RTTS assy on 5 1/2"" DP from 2078 m to 3306 m. Reduced speed inside 9 5/8"" liner - 3 min/ std.",2.75 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 18:00:00+00:00,2009-05-17 19:15:00+00:00,3306.0,m,fixed,interruption -- other,ok,operation failed,"Took up and down weight at RTTS setting depth, up 164 ton/ down 136 ton. Circulated and cleaned setting area with 800 lpm/ 20 bar. Run in 3 meters to 3309 m and pulled back to setting depth 3306 m/ RTTS packer depth 3298 m. Rotated clockwise and slacked off weight, released torque and had 15 ton down weight to set RTTS packer. Closed MPR at BOP and confirmed line up.",1.25 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 19:15:00+00:00,2009-05-17 20:30:00+00:00,3306.0,m,fixed,drilling -- casing,ok,success,Pressure tested entire well to 300 bar/ 10 min. Pumped volume 3690 l/ Bled back 3680 l.,1.25 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 20:30:00+00:00,2009-05-17 21:30:00+00:00,3287.0,m,fixed,interruption -- other,ok,operation failed,Opened BOP. Picked up with 25 ton OP and released packer. Retracted packerelements. Pulled out to 3287 m and racked back stand in derrick.,1.0 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 21:30:00+00:00,2009-05-17 21:45:00+00:00,3287.0,m,fixed,drilling -- casing,ok,success,"Installed 3"" drift in string. Chased drift down string with 2500 lpm/ 98 bar.",0.25 +15_9_F_10_2009_05_18.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-17T00:00:00+02:00,2009-05-18T00:00:00+02:00,2009-05-17 21:45:00+00:00,2009-05-17 22:00:00+00:00,3287.0,m,fixed,interruption -- other,ok,operation failed,Flow checked well on trip tank.,0.25 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-17 22:00:00+00:00,2009-05-17 22:30:00+00:00,3287.0,m,fixed,interruption -- other,ok,operation failed,"Pumped 5 m3 1,6 sg slug. Chased and allowed to settle.",0.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-17 22:30:00+00:00,2009-05-18 00:00:00+00:00,2506.0,m,fixed,interruption -- other,ok,operation failed,"POOH with 9 5/8"" RTTS on 5 1/2"" DP from 3287 m to 2506 m. Reduced speed while POOH with packer in 9 5/8"" liner.",1.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 00:00:00+00:00,2009-05-18 03:00:00+00:00,19.0,m,fixed,interruption -- other,ok,operation failed,"POOH with 9 5/8"" RTTS on 5 1/2"" DP from 2506 m to 19 m. (829 m/ hr)",3.0 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 03:00:00+00:00,2009-05-18 03:30:00+00:00,19.0,m,fixed,interruption -- other,ok,operation failed,Removed PS-21 slips and installed master bushed. Racked back last stand in derrick.,0.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 03:30:00+00:00,2009-05-18 04:00:00+00:00,0.0,m,fixed,interruption -- other,ok,operation failed,POOH and LD RTTS assy from 19 m to surface.,0.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 04:00:00+00:00,2009-05-18 04:15:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Cleaned and cleared rig floor and prepared P/U 8 1/2"" BHA.",0.25 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 04:15:00+00:00,2009-05-18 06:45:00+00:00,42.0,m,fixed,drilling -- trip,ok,success,"PU and RIH with 8 1/2"" BHA from surface to 42 m. Checked communication resistance in telescope and evaluated readings. BHA consist of: PD Exceed, Ecoscope, Telescope, Sonicvisjon and Stethoscope.",2.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 06:45:00+00:00,2009-05-18 07:15:00+00:00,42.0,m,fixed,drilling -- trip,ok,success,TBT prior to radio active source activity. Loaded radioactive source in ecoscope tool.,0.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 07:15:00+00:00,2009-05-18 07:45:00+00:00,138.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" BHA from 42 m to 138 m of which, 8x 5"" HWDP, Jar and Accelerator. Installed totco ring on top of last 5"" HWDP at 138 m. Weight below jar; 7,5 ton - Total BHA weight: 10,5 ton.",0.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 07:45:00+00:00,2009-05-18 08:00:00+00:00,138.0,m,fixed,drilling -- drill,ok,success,Removed master bushing and installed PS-21 slips.,0.25 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 08:00:00+00:00,2009-05-18 09:00:00+00:00,464.0,m,fixed,drilling -- trip,ok,success,"RIH with 5"" DP from 138 m to 464 m of which, 3 stand from derrick and 15 singles P/U from cantilever.",1.0 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 09:00:00+00:00,2009-05-18 09:15:00+00:00,627.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" BHA on 5"" DP from 464 m to 627 m. (652 m/ hr)",0.25 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 09:15:00+00:00,2009-05-18 10:00:00+00:00,627.0,m,fixed,drilling -- drill,ok,success,"Filled pipe and tested MWD at 627 m. Test parameters: 1500 lpm/ 53 bar - 2000 lpm/ 85 bar, 30 RPM/ 1-3 kNm.",0.75 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 10:00:00+00:00,2009-05-18 10:30:00+00:00,627.0,m,fixed,drilling -- drill,ok,success,Serviced TDS.,0.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 10:30:00+00:00,2009-05-18 12:00:00+00:00,1808.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" BHA on 5"" DP from 627 m to 1808 m. Filled pipe every 600 m. (787 m/ hr)",1.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 12:00:00+00:00,2009-05-18 14:00:00+00:00,1808.0,m,fixed,interruption -- maintain,ok,success,TBT with focus on slip and cut. Slipped and cut drilling line. Calibrated block.,2.0 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 14:00:00+00:00,2009-05-18 14:30:00+00:00,2174.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" BHA on 5"" DP from 1808 m to 2174 m. (732 m/ hr)",0.5 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 14:30:00+00:00,2009-05-18 14:45:00+00:00,2174.0,m,fixed,drilling -- drill,ok,success,"Changed handling equipment from 5"" DP to 5 1/2"" DP.",0.25 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 14:45:00+00:00,2009-05-18 16:30:00+00:00,3305.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" BHA on 5"" DP from 2174 m to 3305 m. Filled pipe every 600 m. (646 m/ hr)",1.75 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 16:30:00+00:00,2009-05-18 18:15:00+00:00,3394.0,m,fixed,drilling -- drill,ok,success,"Washed down in hole from 3305 m to 3394 m. Parameters: 1800 lpm/ 125 bar, 30 RPM/ 10-14 kNm. Took weight and tag top plug/ cement with 7 ton WOB at 3394 m.",1.75 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 18:15:00+00:00,2009-05-18 19:00:00+00:00,3395.0,m,fixed,drilling -- casing,ok,success,Drilled top plug/ cement from 3394 m to 3395 m. Parameters: 2000 lpm/ 150-170 bar. 30 RPM/ 11-16 kNm. WOB: 4-7 ton. ROP: 1-2 m/hr. Pulled back to 3385 m for chokedrill.,0.75 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 19:00:00+00:00,2009-05-18 19:45:00+00:00,3385.0,m,fixed,drilling -- casing,ok,success,Performed choke drill with involved personnel at 3385 m.,0.75 +15_9_F_10_2009_05_19.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-18T00:00:00+02:00,2009-05-19T00:00:00+02:00,2009-05-18 19:45:00+00:00,2009-05-18 22:00:00+00:00,3401.0,m,fixed,drilling -- casing,ok,success,"RIH to 3395 m. Drilled top plug/ soft cement from 3394 m to 3401 m. Parameters on top plug: 1800 - 2000 lpm/ 120 -180 bar. RPM 50/ 11-16 kNm. WOB: 2-7 ton. ROP: 0,5 - 1m/ hr. Parameters on cement: 2000 lpm/ 150-160 bar. 40 RPM/ 11-14 kNm. WOB: 2-3 ton. ROP: 20 -25 m/hr.",2.25 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-18 22:00:00+00:00,2009-05-18 22:45:00+00:00,3413.0,m,fixed,drilling -- casing,ok,success,Drilled soft cement from 3401 m to 3413 m. Parameters: 2000 lpm/ 150-160 bar. 40 RPM/ 11-14 kNm. WOB: 2-3 ton. ROP: 20-25 m/hr.,0.75 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-18 22:45:00+00:00,2009-05-19 02:30:00+00:00,3414.0,m,fixed,drilling -- casing,ok,success,"Drilled bottom plug and landing collar from 3413 m to 3414 m. Parameters: 1800 - 2000 lpm/ 120 -170 bar. RPM: 30 - 50/ 11-16 kNm. WOB: 7-10 ton. ROP: 0,5 - 1m/ hr.",3.75 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 02:30:00+00:00,2009-05-19 04:00:00+00:00,3434.0,m,fixed,drilling -- casing,ok,success,Drilled soft cement in shoe track from 3414 m to 3434 m. Parameters: 2000 lpm/ 148-150 bar. 50 RPM/ 11-14 kNm. WOB: 2-4 ton. ROP: 25 -30 m/hr.,1.5 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 04:00:00+00:00,2009-05-19 04:30:00+00:00,3440.0,m,fixed,drilling -- casing,ok,success,Drilled cement in shoe track from 3434 m to 3440 m. Parameters: 2000 lpm/ 147-150 bar. 50 RPM/ 12-14 kNm. WOB: 2-4 ton. ROP: 25 -30 m/hr.,0.5 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 04:30:00+00:00,2009-05-19 06:00:00+00:00,3441.0,m,fixed,drilling -- casing,ok,success,"Drilled 9 5/8"" reamer shoe from 3440 m to 3441 m. Parameters: 2000 - 2200 lpm/ 147-185 bar. 50 RPM/ 12-17 kNm. WOB: 0-2 ton. ROP: 0,5-2 m/hr. String stalled out several times and pressure increased with 20-30 bar.",1.5 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 06:00:00+00:00,2009-05-19 08:15:00+00:00,3442.0,m,fixed,drilling -- casing,ok,success,"Timedrilled rest of shoe with steady parameters from 3441 m to 3442 m. Parameters: 2200 lpm/ 180 bar, 60 RPM/ 12-18 kNm. WOB: 0-2 ton. Had no clear indication of going out of shoe. Checked shoe/ rathole twice, OK.",2.25 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 08:15:00+00:00,2009-05-19 10:45:00+00:00,3446.0,m,fixed,drilling -- drill,ok,success,"Drilled 4 m new formation and 8 1/2"" hole from 3442 m to 3446 m. Parameters: 2200 lpm/ 172 - 176 bar, 60 RPM/ 12-17 kNm, WOB: 1-2 ton. ROP: 1-3 m/hr.",2.5 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 10:45:00+00:00,2009-05-19 11:00:00+00:00,3446.0,m,fixed,drilling -- drill,ok,success,"Checked rathole / shoe with and without rotation, OK.",0.25 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 11:00:00+00:00,2009-05-19 11:45:00+00:00,3446.0,m,fixed,drilling -- drill,ok,success,Pumped 4 m3 LCM pill and displaced same as balanced pill. Parameters: 1000 lpm in DP and 800 lpm through BHA.,0.75 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 11:45:00+00:00,2009-05-19 12:30:00+00:00,3332.0,m,fixed,drilling -- drill,ok,success,POOH slowly from 3446 m to 3332 m. Meanwhile pressure tested surface lines prior to FIT.,0.75 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 12:30:00+00:00,2009-05-19 12:45:00+00:00,3332.0,m,fixed,drilling -- drill,ok,success,Pumped 1 m3 OBM to clear MWD tools of any LCM.,0.25 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 12:45:00+00:00,2009-05-19 13:00:00+00:00,3332.0,m,fixed,formation evaluation -- rft/fit,ok,success,"R/U for FIT, checked line up and flushed lines.",0.25 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 13:00:00+00:00,2009-05-19 13:30:00+00:00,3332.0,m,fixed,formation evaluation -- rft/fit,ok,success,"Performed FIT to 1,55 sg EMW by pressuring up to 68 bar at cement unit. Volume pumped: 919 l/ Bled back: 900 l. Meanwhile changed out drill line guide.",0.5 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 13:30:00+00:00,2009-05-19 13:45:00+00:00,3332.0,m,fixed,formation evaluation -- rft/fit,ok,success,R/D FIT equipment.,0.25 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 13:45:00+00:00,2009-05-19 14:15:00+00:00,3332.0,m,fixed,interruption -- maintain,ok,success,Planned maintenance - continued changed out drill line guide.,0.5 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 14:15:00+00:00,2009-05-19 14:45:00+00:00,3332.0,m,fixed,drilling -- survey,ok,success,"Performed static pressure survey to 1,57 sg to check FIT.",0.5 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 14:45:00+00:00,2009-05-19 15:00:00+00:00,3446.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" BHA from 3332 m to 3446 m.",0.25 +15_9_F_10_2009_05_20.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-19T00:00:00+02:00,2009-05-20T00:00:00+02:00,2009-05-19 15:00:00+00:00,2009-05-19 22:00:00+00:00,3461.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole from 3446 m to 3461 m. Parameters: 2366 lpm/ 195 bar, 80 RPM/ 14-17 kNm, WOB: 6-7 ton. ROP: 2-4 m/hr. ECD: 1,37 sg +Note: Used max 80-90 RPM until top stabilizer out of shoe. + Verified 9 5/8"" shoe depth with logging tool to 3441 mMD.",7.0 +15_9_F_10_2009_05_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-20T00:00:00+02:00,2009-05-21T00:00:00+02:00,2009-05-19 22:00:00+00:00,2009-05-20 00:15:00+00:00,3465.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole from 3461 m to 3465 m. Parameters: 2366 lpm/ 192 bar, 80 RPM/ 13-16 kNm, WOB: 5-7 ton. ROP: 2-4 m/hr. ECD: 1,37 sg",2.25 +15_9_F_10_2009_05_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-20T00:00:00+02:00,2009-05-21T00:00:00+02:00,2009-05-20 00:15:00+00:00,2009-05-20 00:30:00+00:00,3465.0,m,fixed,drilling -- drill,ok,success,"Performed SCR readings at 3465 mMD/ 2655 mTVD with MW 1,30 sg. MP#1: 30 SPM/24 Bar - 40 SPM/ 34 Bar - 50 SPM/ 46 bar. MP#3: 30 SPM/23 Bar - 40 SPM/ 34 Bar - 50 SPM/ 46 Bar.",0.25 +15_9_F_10_2009_05_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-20T00:00:00+02:00,2009-05-21T00:00:00+02:00,2009-05-20 00:30:00+00:00,2009-05-20 04:00:00+00:00,3471.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole from 3465 m to 3471 m. Parameters: 2366 lpm/ 192 bar, 80-90 RPM/ 13-16 kNm, WOB: 4-6 ton. ROP: 2-4 m/hr. ECD: 1,37 sg",3.5 +15_9_F_10_2009_05_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-20T00:00:00+02:00,2009-05-21T00:00:00+02:00,2009-05-20 04:00:00+00:00,2009-05-20 17:15:00+00:00,3506.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole from 3471 m to 3506 m. Parameters: 2366 lpm/ 186-190 bar, 90-180 RPM/ 13-19 kNm, WOB: 2-6 ton. ROP: 2-6 m/hr. ECD: 1,371 sg. +Took survey after connection. +Varied drilling parameters to optimise ROP.",13.25 +15_9_F_10_2009_05_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-20T00:00:00+02:00,2009-05-21T00:00:00+02:00,2009-05-20 17:15:00+00:00,2009-05-20 17:30:00+00:00,3506.0,m,fixed,drilling -- drill,ok,success,"Performed SCR readings at 3506 mMD/ 2659 mTVD with MW 1,30 sg. MP#1: 30 SPM/24 Bar - 40 SPM/ 33 Bar - 50 SPM/ 46 bar. MP#2: 30 SPM/23 Bar - 40 SPM/ 33 Bar - 50 SPM/ 46 Bar.",0.25 +15_9_F_10_2009_05_21.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-20T00:00:00+02:00,2009-05-21T00:00:00+02:00,2009-05-20 17:30:00+00:00,2009-05-20 22:00:00+00:00,3522.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole from 3506 m to 3522 m. Parameters: 2366 lpm/ 186-190 bar, 140 RPM/ 14-17 kNm, WOB: 5-6 ton. ROP: 4-6 m/hr. ECD: 1,371 sg. +Varied drilling parameters to optimise ROP. +At 3510 m lost the PNG funtionality from Ecoscope tool.",4.5 +15_9_F_10_2009_05_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-21T00:00:00+02:00,2009-05-22T00:00:00+02:00,2009-05-20 22:00:00+00:00,2009-05-21 04:00:00+00:00,3542.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole from 3522 m to 3542 m. Parameters: 2385 lpm/ 188-190 bar, 140-150 RPM/ 14-18 kNm, WOB: 5-6 ton. ROP: 3-7 m/hr. ECD: 1,372 sg. +Varied drilling parameters to optimise ROP.",6.0 +15_9_F_10_2009_05_22.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-21T00:00:00+02:00,2009-05-22T00:00:00+02:00,2009-05-21 04:00:00+00:00,2009-05-21 22:00:00+00:00,3588.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 3542 m to 3588 m MD. Drilling parameters : Flow 2400 lpm / SPP ~185 bar / 140-160 RPM / WOB 2-7 MT / Torque 10-20 kNm / ECD 1,37 / ROP 2-8 m/hrs. Penetration limited by torque and stick/slip. Perfomed MWD survey on connections.",18.0 +15_9_F_10_2009_05_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-22T00:00:00+02:00,2009-05-23T00:00:00+02:00,2009-05-21 22:00:00+00:00,2009-05-22 04:00:00+00:00,3600.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 3588 m to 3600 m MD. Drilling parameters : Flow 2400 lpm / SPP ~185 bar / 160-200 RPM / WOB 5-8 MT / Torque 10-20 kNm / ECD 1,37 / ROP 1-3 m/hrs. Penetration limited by torque and stick/slip.",6.0 +15_9_F_10_2009_05_23.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-22T00:00:00+02:00,2009-05-23T00:00:00+02:00,2009-05-22 04:00:00+00:00,2009-05-22 22:00:00+00:00,3653.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 3600 m to 3653 m MD. Drilling parameters : Flow 2400 lpm / SPP ~185 bar / 160-200 RPM / WOB 4-7 MT / Torque 15-20 kNm / ECD 1,36-1,37 / ROP 2-10 m/hrs. Penetration limited by torque and stick/slip. Performed MWD survey on connection.",18.0 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-22 22:00:00+00:00,2009-05-23 04:00:00+00:00,3675.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 3653 m to 3675 m MD. Drilling parameters : Flow 2400 lpm / SPP ~187 bar / 200 RPM / WOB 6-7 MT / Torque 15-20 kNm / ECD 1,36-1,37 / ROP 2-10 m/hrs. Penetration limited by torque and stick/slip. Performed MWD survey on connection.",6.0 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 04:00:00+00:00,2009-05-23 09:15:00+00:00,3695.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 3675 m to 3695 m MD. Drilling parameters : Flow 2400 lpm / SPP ~187 bar / 200 RPM / WOB 4-9 MT / Torque 15-20 kNm / ECD 1,36-1,37 / ROP 2-8 m/hrs. Penetration limited by torque and stick/slip.",5.25 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 09:15:00+00:00,2009-05-23 09:30:00+00:00,3695.0,m,fixed,drilling -- drill,ok,success,"Observed 0,5 m2 gradual gain in active. Checked pits and shaker and compared to Geoservice sensors. Picked off bottom and flow checked - well static.",0.25 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 09:30:00+00:00,2009-05-23 10:15:00+00:00,3695.0,m,fixed,drilling -- drill,ok,success,Made decision to POOH for changing BHA. Circulated BHA clear of cuttings at 2400 lpm. Downlinked Powerdrive before POOH according to DDs instructions.,0.75 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 10:15:00+00:00,2009-05-23 11:15:00+00:00,3422.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA from 3695 m to 3422 m MD on 5 1/2"" DP. Pulled wet pipe.",1.0 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 11:15:00+00:00,2009-05-23 11:45:00+00:00,3422.0,m,fixed,drilling -- drill,ok,success,"Pumped 5 m3 slug of 1,65 sg OBM. Chased slug to drillfloor and allowed mud level to settle.",0.5 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 11:45:00+00:00,2009-05-23 12:30:00+00:00,3422.0,m,fixed,interruption -- other,ok,equipment failure,Repaired hydraulic leak on aft IR.,0.75 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 12:30:00+00:00,2009-05-23 13:45:00+00:00,2174.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 3422 m to 2174 m MD. Tripping speed 1000 m/hr.",1.25 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 13:45:00+00:00,2009-05-23 14:00:00+00:00,2174.0,m,fixed,drilling -- other,ok,success,"Changed from 5 1/2"" to 5"" handling equipment.",0.25 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 14:00:00+00:00,2009-05-23 16:00:00+00:00,178.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5"" DP from 2174 m to 178 m MD. Tripping speed 1000 m/hr.",2.0 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 16:00:00+00:00,2009-05-23 17:00:00+00:00,178.0,m,fixed,drilling -- other,ok,success,Flowchecked well on triptanks prior to pulling BHA - well static. Removed auto slips and installed masterbushing and bowls in RT.,1.0 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 17:00:00+00:00,2009-05-23 18:30:00+00:00,61.0,m,fixed,drilling -- trip,ok,success,"Held toolbox talk for laying out BHA. Racked back stand of 5"" HWDP. Made up stand of 5"" HWDP to accelerator and racked back in derrick. Broke 5"" HWDP/jar stand and laid out single for inspection. Picked up new 5"" HWDP and made up to stand, racked back stand in derrick.",1.5 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 18:30:00+00:00,2009-05-23 19:00:00+00:00,61.0,m,fixed,drilling -- trip,ok,success,Held toobox talk for handling RA-soruce. Cleared drillfloor of non-essential personnel. Broke connection above Echoscope and removed RA source.,0.5 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 19:00:00+00:00,2009-05-23 20:30:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Broke and laid out Stethoscope, Sonicvison, Telescope and Echoscope. Inspected and gauged stabilizers and bit. Laid out 8 1/2"" Powerdrive exceed.",1.5 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 20:30:00+00:00,2009-05-23 21:00:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,Cleared and tidied drillfloor.,0.5 +15_9_F_10_2009_05_24.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-23T00:00:00+02:00,2009-05-24T00:00:00+02:00,2009-05-23 21:00:00+00:00,2009-05-23 22:00:00+00:00,8.0,m,fixed,drilling -- trip,ok,success,"Held toolbox talk for using manual tongs. Picked up back-up 8 1/2"" Powerdrive exceed. Installed bit and bit breaker in RT. Made up 8 1/2"" bit to Powerdrive exceed using manual tongs. Picked up and made up Telescope/MWD.",1.0 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-23 22:00:00+00:00,2009-05-23 23:45:00+00:00,135.0,m,fixed,drilling -- trip,ok,success,"Picked up and made up 2 x 6 7/8"" NMDC and AST tool. Picked up and made up 2 x 5 1/2"" HWDP singles. Made up stand of jar/5"" HWDP and stand of accelerator/5"" HWDP. Installed totco ring.",1.75 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-23 23:45:00+00:00,2009-05-24 00:00:00+00:00,135.0,m,fixed,drilling -- other,ok,success,Removed master bushing and installed auto slips.,0.25 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 00:00:00+00:00,2009-05-24 01:00:00+00:00,581.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP from 135 m to 581 m MD.",1.0 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 01:00:00+00:00,2009-05-24 01:30:00+00:00,581.0,m,fixed,drilling -- other,ok,success,"Made up TDS. Filled DP with 1,30 sg OBM at 2700 lpm. Tested MWD and Powedrive exceed - ok.",0.5 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 01:30:00+00:00,2009-05-24 02:30:00+00:00,1190.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP from 581 m to 1190 m MD.",1.0 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 02:30:00+00:00,2009-05-24 02:45:00+00:00,1190.0,m,fixed,drilling -- drill,ok,success,"Made up TDS and filled DP with 1,30 sg OBM.",0.25 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 02:45:00+00:00,2009-05-24 03:15:00+00:00,1190.0,m,fixed,drilling -- other,ok,success,Serviced and greased TDS.,0.5 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 03:15:00+00:00,2009-05-24 04:00:00+00:00,1722.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP from 1190 m to 1722 m MD.",0.75 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 04:00:00+00:00,2009-05-24 04:15:00+00:00,1763.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP from 1722 m to 1763 m MD.",0.25 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 04:15:00+00:00,2009-05-24 04:45:00+00:00,1763.0,m,fixed,drilling -- other,ok,success,"Changed from 5"" to 5 1/2"" handling equipment. Made up TDS and filled DP.",0.5 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 04:45:00+00:00,2009-05-24 05:15:00+00:00,2369.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5 1/2"" DP from 1763 to 2369 m MD. Tripping speed 1000 m/hrs. Drawwork stopped by sudden incident.",0.5 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 05:15:00+00:00,2009-05-24 05:30:00+00:00,2369.0,m,fixed,interruption -- other,ok,equipment failure,Investigated hard trip of drawworks.,0.25 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 05:30:00+00:00,2009-05-24 05:45:00+00:00,2369.0,m,fixed,drilling -- other,ok,success,Made up TDS and filled pipe.,0.25 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 05:45:00+00:00,2009-05-24 06:45:00+00:00,2974.0,m,fixed,drilling -- drill,ok,success,"RIH on 5 1/2"" DP from 2369 m to 2974 m MD. Ran carefully across liner top at 2506 m MD. Tripping speed 600 m/hrs",1.0 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 06:45:00+00:00,2009-05-24 07:00:00+00:00,2974.0,m,fixed,drilling -- other,ok,success,Made up TDS and filled pipe.,0.25 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 07:00:00+00:00,2009-05-24 08:00:00+00:00,3618.0,m,fixed,drilling -- drill,ok,success,"RIH on 5 1/2"" DP from 2974 m to 3618 m MD. Tripping speed 650 m/hrs.",1.0 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 08:00:00+00:00,2009-05-24 08:15:00+00:00,3695.0,m,fixed,drilling -- other,ok,success,Made up TDS and filled pipe.,0.25 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 08:15:00+00:00,2009-05-24 09:15:00+00:00,3695.0,m,fixed,drilling -- drill,ok,success,Washed down from 3618 m to 3695 m MD. Parameters : 2400 lpm / SPP 190 bar / 60 RPM / Torque 14 kNm.,1.0 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 09:15:00+00:00,2009-05-24 09:30:00+00:00,3695.0,m,fixed,drilling -- drill,ok,success,Took SCR's before start drilling. Jetted bottom of hole.,0.25 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 09:30:00+00:00,2009-05-24 14:00:00+00:00,3705.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 3695 m to 3705 m MD. Drilling parameters : Flow 2400 lpm / SPP 180-188 bar / 200 RPM / WOB 2-4 MT / Torque 15-20 kNm / ROP 2-3 m/hr. Penetration limited by stick/slip. Perfomed MWD survey on connection.",4.5 +15_9_F_10_2009_05_25.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-24T00:00:00+02:00,2009-05-25T00:00:00+02:00,2009-05-24 14:00:00+00:00,2009-05-24 22:00:00+00:00,3816.0,m,fixed,drilling -- drill,ok,success,"Issued concent to drill ahead under severe stick/slip conditions. Drilled 8 1/2"" hole section from 3705 m to 3816 m MD. Drilling parameters : Flow 2200 lpm / SPP 150-160 bar / 200 RPM / WOB 7-9 MT / Torque 20-30 kNm / ROP 17-20 m/hr. Perfomed MWD survey on connections.",8.0 +15_9_F_10_2009_05_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-25T00:00:00+02:00,2009-05-26T00:00:00+02:00,2009-05-24 22:00:00+00:00,2009-05-24 23:45:00+00:00,3839.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 3816 m to 3839 m MD. Drilling parameters : Flow 2200 lpm / SPP ~150 bar / 200 RPM / WOB 7-9 MT / Torque 20-25 kNm / ROP 17 m/hr. Perfomed MWD survey on connections.",1.75 +15_9_F_10_2009_05_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-25T00:00:00+02:00,2009-05-26T00:00:00+02:00,2009-05-24 23:45:00+00:00,2009-05-25 00:15:00+00:00,3839.0,m,fixed,drilling -- drill,ok,success,"Due to 0,6 m3 gain in active, picked off bottom. Lined up trip tanks and flowchecked - well static.",0.5 +15_9_F_10_2009_05_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-25T00:00:00+02:00,2009-05-26T00:00:00+02:00,2009-05-25 00:15:00+00:00,2009-05-25 02:15:00+00:00,3863.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 3839 m to 3863 m MD. Drilling parameters : Flow 2200 lpm / SPP 155 bar / 200 RPM / WOB 7-9 MT / Torque 20-25 kNm / ROP 17 m/hr. Picked off bottom and recessed operation for repair of TDS blower hose (air cooling system).",2.0 +15_9_F_10_2009_05_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-25T00:00:00+02:00,2009-05-26T00:00:00+02:00,2009-05-25 02:15:00+00:00,2009-05-25 04:00:00+00:00,3863.0,m,fixed,interruption -- other,ok,equipment failure,Made temporary repair on buckled air blower hose on TDS. Meanwhile circulated at 1500 lpm / SPP 81 bar while rotating at 20 RPM.,1.75 +15_9_F_10_2009_05_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-25T00:00:00+02:00,2009-05-26T00:00:00+02:00,2009-05-25 04:00:00+00:00,2009-05-25 04:15:00+00:00,3863.0,m,fixed,interruption -- other,ok,equipment failure,Made temporary repair on buckled air blower hose on TDS.,0.25 +15_9_F_10_2009_05_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-25T00:00:00+02:00,2009-05-26T00:00:00+02:00,2009-05-25 04:15:00+00:00,2009-05-25 20:30:00+00:00,4159.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 3863 m to 4159 m MD. Drilling parameters : Flow 2200-2500 lpm / SPP 190-208 bar / 200 RPM / WOB 9-13 MT / Torque 20-25 kNm / ROP 18-28 m/hrs. Performed MWD survey on connections. Downlinked Powerdrive according to DD instructions.",16.25 +15_9_F_10_2009_05_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-25T00:00:00+02:00,2009-05-26T00:00:00+02:00,2009-05-25 20:30:00+00:00,2009-05-25 21:15:00+00:00,4167.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4159 m to 4167 m MD. Observed continuos left hand tendency of Powerdrive despite 20% right setting. Reduced ROP to 10 m/hrs and attempted to set Powerdrive to 60% right - still observed left hand tendency. Picked off bottom and reamed stand while confering with Schulmberger support centre.",0.75 +15_9_F_10_2009_05_26.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-25T00:00:00+02:00,2009-05-26T00:00:00+02:00,2009-05-25 21:15:00+00:00,2009-05-25 22:00:00+00:00,4168.0,m,fixed,drilling -- drill,ok,success,"As recommended by support centre, sent 3 consecutive downlinks to Powerdrive : 1.Reset / 2.Hold / 3.60% right.",0.75 +15_9_F_10_2009_05_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-26T00:00:00+02:00,2009-05-27T00:00:00+02:00,2009-05-25 22:00:00+00:00,2009-05-25 22:15:00+00:00,4170.0,m,fixed,drilling -- drill,ok,success,"Drilled 2-3 m 8 1/2"" hole to 4170 m MD. Observed no right hand response on Powerdrive with 60% right setting.",0.25 +15_9_F_10_2009_05_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-26T00:00:00+02:00,2009-05-27T00:00:00+02:00,2009-05-25 22:15:00+00:00,2009-05-26 00:30:00+00:00,4205.0,m,fixed,drilling -- drill,ok,success,"Downlinked Powerdrive to 80% right hand setting. Drilled 8 1/2"" hole section from 4170 m to 4205 m MD. Drilling parameters : Flow 2500 lpm / SPP ~205 bar / 200 RPM / WOB 7-9 MT / Torque 20-22 kNm / ROP 20 m/hrs. Obtained right hand movement and change in azimuth from 113 to 117 deg.",2.25 +15_9_F_10_2009_05_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-26T00:00:00+02:00,2009-05-27T00:00:00+02:00,2009-05-26 00:30:00+00:00,2009-05-26 04:00:00+00:00,4266.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4205 m to 4266 m MD. Drilling parameters : Flow 2500 lpm / SPP ~207-210 bar / 200 RPM / WOB 9-11 MT / Torque 20-25 kNm / ROP 20-25 m/hrs. Performed MWD survey on connections. Downlinked powerdrive according to DDs instructions.",3.5 +15_9_F_10_2009_05_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-26T00:00:00+02:00,2009-05-27T00:00:00+02:00,2009-05-26 04:00:00+00:00,2009-05-26 06:30:00+00:00,4306.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4266 m to 4306 m MD. Drilling parameters : Flow 2500 lpm / SPP ~213 bar / 200 RPM / WOB 10-12 MT / Torque 20-26 kNm / ROP 25-28 m/hrs. Performed MWD survey on connection. Downlinked powerdrive according to DDs instructions.",2.5 +15_9_F_10_2009_05_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-26T00:00:00+02:00,2009-05-27T00:00:00+02:00,2009-05-26 06:30:00+00:00,2009-05-26 07:00:00+00:00,4306.0,m,fixed,drilling -- other,ok,success,"Inspected, serviced and greased TDS.",0.5 +15_9_F_10_2009_05_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-26T00:00:00+02:00,2009-05-27T00:00:00+02:00,2009-05-26 07:00:00+00:00,2009-05-26 17:00:00+00:00,4482.0,m,fixed,drilling -- other,ok,success,"Drilled 8 1/2"" hole section from 4306 m to 4482 m MD. Drilling parameters : Flow 2800 lpm / SPP ~240 bar / 200 RPM / WOB 9-12 MT / Torque 21-23 kNm / ROP 20-25 m/hrs. Performed MWD survey on connection. Downlinked powerdrive according to DDs instructions. + +Attmepted to reduce torque by adding Baralube to the mud, obtained no recordable difference.",10.0 +15_9_F_10_2009_05_27.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-26T00:00:00+02:00,2009-05-27T00:00:00+02:00,2009-05-26 17:00:00+00:00,2009-05-26 22:00:00+00:00,4523.0,m,fixed,drilling -- drill,ok,success,"Got problems with DCI system not processing cuttings properly. Picked off bottom and shut down pumps. Discussed situation and decided to continue drilling routing cuttings to skips. Routed cuttings to skips on deck. Continued drilling 8 1/2"" hole section from 4482 m to 4523 m MD with reduced penetration rate. Drilling parameters : Flow 2800 lpm / SPP 255-260 bar / 200 RPM / WOB ~7 MT / Torque 18-22 kNm / ROP 10 m/hrs. Performed MWD survey on connection. + +Meanwhile changed impellers on DCI pumps.",5.0 +15_9_F_10_2009_05_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-27T00:00:00+02:00,2009-05-28T00:00:00+02:00,2009-05-26 22:00:00+00:00,2009-05-27 00:30:00+00:00,4549.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4523 m to 4549 m MD with reduced penetration rate. Drilling parameters : Flow 2800 lpm / SPP ~260 bar / 200 RPM / WOB ~7 MT / Torque ~20 kNm / ROP 10-15 m/hrs. + +Tested DCI system after impeller change out. Observed escalating leakage on end hub of DCI manifold. Skips about to be filled - unable to drill ahead.",2.5 +15_9_F_10_2009_05_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-27T00:00:00+02:00,2009-05-28T00:00:00+02:00,2009-05-27 00:30:00+00:00,2009-05-27 04:00:00+00:00,4549.0,m,fixed,interruption -- other,ok,equipment failure,Traced spare flange adapter to be in Dusavik base due out on Wednesday boat. Called town and arranged for heli transport of required parts. Circulated hole clean while reciprocating stand. Parameters : Flow 2500-2800 lpm / SPP 213-263 bar / 160-200 RPM / Torque 14-16 kNm.,3.5 +15_9_F_10_2009_05_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-27T00:00:00+02:00,2009-05-28T00:00:00+02:00,2009-05-27 04:00:00+00:00,2009-05-27 08:00:00+00:00,4182.0,m,fixed,interruption -- other,ok,equipment failure,Waited on spare parts for DCI to arrive on helicopter. Meanwhile POOH to 4102 m MD to check hole condition.,4.0 +15_9_F_10_2009_05_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-27T00:00:00+02:00,2009-05-28T00:00:00+02:00,2009-05-27 08:00:00+00:00,2009-05-27 08:30:00+00:00,4102.0,m,fixed,drilling -- other,ok,success,Serviced TDS.,0.5 +15_9_F_10_2009_05_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-27T00:00:00+02:00,2009-05-28T00:00:00+02:00,2009-05-27 08:30:00+00:00,2009-05-27 14:00:00+00:00,4549.0,m,fixed,interruption -- other,ok,equipment failure,"Replaced DCI flange adapter and tested system. Meanwhile reamed back in with 8 1/2"" drilling BHA on 5 1/2"" DP from 4102 to 4549 m MD. Parameters : Flow 2000-2800 lpm / SPP145-270 bar / 60 RPM / Torque ~15 kNm.",5.5 +15_9_F_10_2009_05_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-27T00:00:00+02:00,2009-05-28T00:00:00+02:00,2009-05-27 14:00:00+00:00,2009-05-27 20:00:00+00:00,4633.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4549 m to 4633 m MD. Drilling parameters : Flow 2800 lpm / SPP 262-266 bar / 200 RPM / WOB 7-11 MT / Torque ~21 kNm / ROP 15-25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions. Got liner spray alarm on mudpump#2.",6.0 +15_9_F_10_2009_05_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-27T00:00:00+02:00,2009-05-28T00:00:00+02:00,2009-05-27 20:00:00+00:00,2009-05-27 20:30:00+00:00,4633.0,m,fixed,interruption -- other,ok,equipment failure,Checked out liner spary alarm on mudpump#2. Meanwhile reciprocated stand pumping at 1800 lpm.,0.5 +15_9_F_10_2009_05_28.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-27T00:00:00+02:00,2009-05-28T00:00:00+02:00,2009-05-27 20:30:00+00:00,2009-05-27 22:00:00+00:00,4670.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4633 m to 4670 m MD. Drilling parameters : Flow 2800 lpm / SPP 262-266 bar / 200 RPM / WOB 7-11 MT / Torque ~23 kNm / ROP 15-25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions.",1.5 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-27 22:00:00+00:00,2009-05-28 01:15:00+00:00,4720.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4670 m to 4720 m MD. Drilling parameters : Flow 2800 lpm / SPP 256-264 bar / 200 RPM / WOB 10-12 MT / Torque 20-25 kNm / ROP 15-25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions.",3.25 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 01:15:00+00:00,2009-05-28 01:30:00+00:00,4720.0,m,fixed,interruption -- other,ok,equipment failure,Checked out liner spary alarm on mudpump#2. Meanwhile reciprocated stand pumping at 1800 lpm.,0.25 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 01:30:00+00:00,2009-05-28 02:45:00+00:00,4750.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4670 m to 4750 m MD. Drilling parameters : Flow 2800 lpm / SPP 256-264 bar / 200 RPM / WOB 10-12 MT / Torque 21-23 kNm / ROP 15-25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions.",1.25 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 02:45:00+00:00,2009-05-28 03:45:00+00:00,4750.0,m,fixed,drilling -- other,ok,success,Inspected and service fwd/aft PRS. Checked oil on TDS gearbox.,1.0 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 03:45:00+00:00,2009-05-28 04:00:00+00:00,4750.0,m,fixed,drilling -- drill,ok,success,Made connection and MWD survey.,0.25 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 04:00:00+00:00,2009-05-28 06:00:00+00:00,4790.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4750 m to 4790 m MD. Drilling parameters : Flow 2800 lpm / SPP ~266 bar / 200 RPM / WOB ~10 MT / Torque 20-23 kNm / ROP 20-25 m/hr. Performed MWD survey on connections. Downlinked Powerdrive according to DDs instructions. + +Recessed operation for changing TDS gearbox oil.",2.0 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 06:00:00+00:00,2009-05-28 06:45:00+00:00,4790.0,m,fixed,interruption -- other,ok,equipment failure,Changed oil in TDS gearbox due to traces of water in oil sample. Meanwhile circulated at 1000 lpm.,0.75 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 06:45:00+00:00,2009-05-28 08:30:00+00:00,4820.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4790 m to 4820 m MD. Drilling parameters : Flow 2800 lpm / SPP ~267 bar / 200 RPM / WOB ~10 MT / Torque 20-23 kNm / ROP 25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions.",1.75 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 08:30:00+00:00,2009-05-28 08:45:00+00:00,4820.0,m,fixed,drilling -- drill,ok,success,"Due to no reduction in active when drilling last stand, lined up to triptanks and flowchecked - well static.",0.25 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 08:45:00+00:00,2009-05-28 13:30:00+00:00,4911.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4820 m to 4911 m MD. Drilling parameters : Flow 2800 lpm / SPP ~272 bar / 200 RPM / WOB ~7 MT / Torque 20-24 kNm / ROP 25 m/hr. Perfomed MWD survey on connections. Downlinked Powerdrive according to DDs instructions.",4.75 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 13:30:00+00:00,2009-05-28 14:00:00+00:00,4911.0,m,fixed,drilling -- drill,ok,success,"Performed MWD survey. Downlinked Powerdrive and set in neutral. Broke and laid out 5 1/2"" single.",0.5 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 14:00:00+00:00,2009-05-28 17:00:00+00:00,4898.0,m,fixed,drilling -- circulating conditioning,ok,success,Circulated hole clean while reciprocating stand. Parameters : Flow 1500-2800 lpm / SPP 97-270 bar / 60-200 RPM / Torque ~18 kNm. Circulated two times bottoms up. Verified clean shakers.,3.0 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 17:00:00+00:00,2009-05-28 17:30:00+00:00,4898.0,m,wire line,workover -- rig up/down,ok,success,Held toolbox talk for running WL gyro. Lined up well on trip tank.,0.5 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 17:30:00+00:00,2009-05-28 19:15:00+00:00,4898.0,m,wire line,workover -- rig up/down,ok,success,Hung off stringin slips with 130 MT downweight. Suspended upper WL sheave in elevator. Suspended lower WL sheave in tugger and slings to samson posts. Made up stuffing box to pump in sub. Set WL depth relative to RT. Stabbed gyro toolstring. Made up FOSV/pump-in sub/stuffing box to DP using IR. Made up cement hose to pump in sub.,1.75 +15_9_F_10_2009_05_29.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-28T00:00:00+02:00,2009-05-29T00:00:00+02:00,2009-05-28 19:15:00+00:00,2009-05-28 22:00:00+00:00,4898.0,m,wire line,workover -- wire line,ok,success,"RIH with gyro on 5/16"" EWL from surface to 360 m MD. Initialized gyro and CLL according to Scientific procedures. RIH with 5/16"" EWL to 1300 m MD.",2.75 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-28 22:00:00+00:00,2009-05-29 01:15:00+00:00,4898.0,m,wire line,workover -- wire line,ok,success,"RIH/pumped gyro on 5/16"" EWL from 1300 to 4760 m MD (top of totco ring in BHA). Pumprate 600-1500 lpm, SPP 33-109 bar. Observed pressure build up to 115 bar when landing in totco ring.",3.25 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 01:15:00+00:00,2009-05-29 04:00:00+00:00,4898.0,m,wire line,workover -- wire line,ok,success,"Lined up well on trip tank. POOH with gyro on 5/16"" EWL from 4760 m to 800 m MD. Logged survey data according to Scientific procedure.",2.75 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 04:00:00+00:00,2009-05-29 05:00:00+00:00,4898.0,m,wire line,workover -- wire line,ok,success,"POOH with gyro on 5/16"" EWL from 800 m MD to surface. Logged survey data according to Scientific procedure. Performed tie-in pass to seabed. POOH with gyro to surface.",1.0 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 05:00:00+00:00,2009-05-29 05:15:00+00:00,4898.0,m,wire line,workover -- rig up/down,ok,success,Held toolbox talk prior to rigging down WL.,0.25 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 05:15:00+00:00,2009-05-29 06:45:00+00:00,4898.0,m,wire line,workover -- rig up/down,ok,success,Cleaned drillfloor for OBM spills. Unhooked cement hose. Broke FOSV/side-entry/pack box using IR and lifted same with tugger whilst comming out with WL toolstring. Laid down toolstring. Rigged down sheaves. Cleared and tidied drillfloor.,1.5 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 06:45:00+00:00,2009-05-29 07:00:00+00:00,4898.0,m,wire line,workover -- rig up/down,ok,success,"Picked up and made up 5 1/2"" space out single from deck. Took upweight with high overpull > 20 MT.",0.25 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 07:00:00+00:00,2009-05-29 09:00:00+00:00,4911.0,m,fixed,drilling -- circulating conditioning,ok,success,Stepped up pumprate in increments to 2800 lpm / SPP 293 bar. Reciprocated stand at 60/200 RPM. Circulated bottoms up. Removed master bushing and installed automatic slips.,2.0 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 09:00:00+00:00,2009-05-29 11:15:00+00:00,4710.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA from 4911 m to 4859 m MD, took >20 MT overpull. Pumped out of hole with 5 stands of 5 1/2"" DP to 4710 m MD at 1500 lpm / 30 RPM.",2.25 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 11:15:00+00:00,2009-05-29 13:45:00+00:00,3985.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 4710 m to 3985 m MD. Pulled wet pipe.",2.5 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 13:45:00+00:00,2009-05-29 14:00:00+00:00,3985.0,m,fixed,drilling -- drill,ok,success,"Pumped 5,5 m3 1,60 sg slug at 1200 lpm and chased to drillfloor. Allowed mud levels to settle.",0.25 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 14:00:00+00:00,2009-05-29 16:00:00+00:00,3420.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 3985 m to 3420 m MD.",2.0 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 16:00:00+00:00,2009-05-29 16:30:00+00:00,3420.0,m,fixed,drilling -- drill,ok,success,Lined up tritanks and flowchecked in shoe - well static.,0.5 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 16:30:00+00:00,2009-05-29 17:00:00+00:00,3420.0,m,fixed,interruption -- other,ok,equipment failure,Changed filters on TDS gearbox.,0.5 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 17:00:00+00:00,2009-05-29 17:30:00+00:00,3255.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 3420 m to 3255 m MD.",0.5 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 17:30:00+00:00,2009-05-29 18:00:00+00:00,3255.0,m,fixed,drilling -- drill,ok,success,Pumped slug. Allowed mud levels to settle.,0.5 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 18:00:00+00:00,2009-05-29 20:00:00+00:00,1756.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 3255 m to 1756 m MD. Tripping speed 750 m/hrs.",2.0 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 20:00:00+00:00,2009-05-29 20:45:00+00:00,1756.0,m,fixed,drilling -- other,ok,success,"Changed from 5 1/2"" to 5"" handling gear. Dropped 3"" drift in 5"" DP.",0.75 +15_9_F_10_2009_05_30.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-29T00:00:00+02:00,2009-05-30T00:00:00+02:00,2009-05-29 20:45:00+00:00,2009-05-29 22:00:00+00:00,746.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5"" DP from 1756 m to 746 m MD. Tripping speed 800 m/hrs.",1.25 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-29 22:00:00+00:00,2009-05-29 23:00:00+00:00,296.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5"" DP from 746 m to 296 m MD.",1.0 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-29 23:00:00+00:00,2009-05-29 23:45:00+00:00,296.0,m,fixed,drilling -- other,ok,success,Flowchecked well before pulling BHA - well static. Removed auto slips and installed masterbushing and bowl.,0.75 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-29 23:45:00+00:00,2009-05-30 02:00:00+00:00,16.0,m,fixed,drilling -- trip,ok,success,"Recovered totco and 3"" drift. Broke and racked back stand of 5"" HWDP/accelerator. Broke and laid out 2 x 5"" HWDP singles. Broke and racked back stand of 5""HWDP/jar. Broke and laid out AST and 2 x NMDC.",2.25 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 02:00:00+00:00,2009-05-30 02:30:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"POOH with Telescope and 8 1/2"" Powerdrive. Inspected bit and found good for reuse. Broke bit using bit breaker wrench and easytorque.",0.5 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 02:30:00+00:00,2009-05-30 03:15:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Broke and laid out Telescope and 8 1/2"" Powerdrive Xceed.",0.75 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 03:15:00+00:00,2009-05-30 04:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Brought jet sub to drillfloor and hung off in RT. Brought 18 3/4"" BOP test plug to drillfloor and made up same.",0.75 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 04:00:00+00:00,2009-05-30 05:00:00+00:00,139.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"RIH with 18 3/4"" BOP test plug to 139 m MD.",1.0 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 05:00:00+00:00,2009-05-30 05:45:00+00:00,139.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Held toolbx talk for testing BOP. Washed across wellhead at 3000 lpm / 10 RPM. Landed BOP test plug at 139 m MD.,0.75 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 05:45:00+00:00,2009-05-30 13:15:00+00:00,139.0,m,fixed,drilling -- bop activities,ok,success,"Tested 18 3/4"" BOP and IBOPs to 30/345 bar 5/10 min.",7.5 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 13:15:00+00:00,2009-05-30 14:45:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Broke out test swadge from TDS. POOH with 18 3/4"" BOP test plug from 139 m MD. Broke and laid out test plug and jet sub.",1.5 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 14:45:00+00:00,2009-05-30 20:15:00+00:00,0.0,m,fixed,interruption -- other,ok,equipment failure,"Changed filters on TDS gearbox, still faulty indications. Changed level sensor on TDS gearbox . Meanwhile changed sheared coupling on encoder for drawworks motor #4.",5.5 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 20:15:00+00:00,2009-05-30 20:30:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,Held toolbox talk for making up BHA.,0.25 +15_9_F_10_2009_05_31.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-30T00:00:00+02:00,2009-05-31T00:00:00+02:00,2009-05-30 20:30:00+00:00,2009-05-30 22:00:00+00:00,42.0,m,fixed,drilling -- trip,ok,success,"Picked up 8 1/2"" PD Xceed. Made up 8 1/2"" bit to PD Xceed using bit tong and easytorque. Picked up and made up Echoscope, Telescope, Sonicvison and Stethoscope. Established scribeline to Stethoscope when running in.",1.5 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-30 22:00:00+00:00,2009-05-30 22:45:00+00:00,42.0,m,fixed,drilling -- trip,ok,success,Picked up and prepared Echosope/neutron for service. Installed RA-source in Echoscope.,0.75 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-30 22:45:00+00:00,2009-05-31 00:00:00+00:00,138.0,m,fixed,drilling -- trip,ok,success,"Picked up and made up 5"" HWDP single. Made up stand of jar/HWDP. Picked up and made up 2 x 5"" HWDP singles. Made up stand of accelerator/HWDP. Installed totco ring on top of HWDP.",1.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 00:00:00+00:00,2009-05-31 00:30:00+00:00,138.0,m,fixed,drilling -- other,ok,success,Removed master bushing. Installed auto slips in RT and hooked up hydraulics.,0.5 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 00:30:00+00:00,2009-05-31 01:00:00+00:00,340.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP from 138 m to 340 m MD.",0.5 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 01:00:00+00:00,2009-05-31 01:15:00+00:00,381.0,m,fixed,drilling -- drill,ok,success,"Picked up, made up and RIH with 3 x 5"" DP to replace stand #6 .",0.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 01:15:00+00:00,2009-05-31 01:30:00+00:00,626.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP from 381 m to 626 m MD.",0.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 01:30:00+00:00,2009-05-31 02:00:00+00:00,626.0,m,fixed,drilling -- other,ok,success,"Made up x-over to drillstring. Made up TDS and filled string, confirmed returns.",0.5 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 02:00:00+00:00,2009-05-31 03:15:00+00:00,1237.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP from 626 m to 1237 m MD.",1.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 03:15:00+00:00,2009-05-31 03:45:00+00:00,1237.0,m,fixed,drilling -- other,ok,success,Made up x-over to drillstring. Made up TDS and filled string. Pumped at 2000 lpm / SPP 106 bar and confirmed MWD functional.,0.5 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 03:45:00+00:00,2009-05-31 04:00:00+00:00,1400.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP frpm 1237 m to 1400 m MD.",0.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 04:00:00+00:00,2009-05-31 04:45:00+00:00,1808.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP from 1400 m to 1808 m MD.",0.75 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 04:45:00+00:00,2009-05-31 05:00:00+00:00,1808.0,m,fixed,drilling -- other,ok,success,Made up TDS and filled pipe.,0.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 05:00:00+00:00,2009-05-31 05:30:00+00:00,2171.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5"" DP from 1808 m to 2171 m MD.",0.5 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 05:30:00+00:00,2009-05-31 05:45:00+00:00,2171.0,m,fixed,drilling -- other,ok,success,"Changed from 5"" to 5 1/2"" handling gear.",0.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 05:45:00+00:00,2009-05-31 06:15:00+00:00,2411.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5 1/2"" DP from 2171m to 2411 m MD.",0.5 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 06:15:00+00:00,2009-05-31 06:30:00+00:00,2411.0,m,fixed,drilling -- other,ok,success,Made up TDS and filled pipe.,0.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 06:30:00+00:00,2009-05-31 07:30:00+00:00,2977.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5 1/2"" DP from 2411 m to 2977 m MD.",1.0 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 07:30:00+00:00,2009-05-31 07:45:00+00:00,2977.0,m,fixed,drilling -- other,ok,success,Made up TDS and filled pipe.,0.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 07:45:00+00:00,2009-05-31 08:45:00+00:00,3422.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5 1/2"" DP from 2977 m to 3422 m MD.",1.0 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 08:45:00+00:00,2009-05-31 09:00:00+00:00,3422.0,m,fixed,drilling -- other,ok,success,Made up TDS and filled pipe.,0.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 09:00:00+00:00,2009-05-31 10:30:00+00:00,3985.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5 1/2"" DP from 3422 m to 3985 m MD.",1.5 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 10:30:00+00:00,2009-05-31 10:45:00+00:00,3985.0,m,fixed,drilling -- other,ok,success,Made up TDS and filled pipe.,0.25 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 10:45:00+00:00,2009-05-31 12:15:00+00:00,4393.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5 1/2"" DP from 3985 m to 4393 m MD.",1.5 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 12:15:00+00:00,2009-05-31 17:15:00+00:00,4877.0,m,fixed,drilling -- drill,ok,success,"RIH with 8 1/2"" drilling BHA on 5 1/2"" DP from 4393 m to 4877 m MD. Made up TDS on each stand run and reamed on way in. Parameters : Flow 1000 lpm / SPP 58-62 bar / 20 RPM / Torque ~15 kNm.",5.0 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 17:15:00+00:00,2009-05-31 18:15:00+00:00,4911.0,m,fixed,drilling -- drill,ok,success,"Established drilling parameters when comming down on stand from 4877 m to 4911 m MD. Downlinked PD Xceed for drilling. Parameters : Flow 2500 lpm / SPP 250 bar / 200 RPM / Torque 15-20 kNm / ECD 1,45-1,46 sg.",1.0 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 18:15:00+00:00,2009-05-31 21:00:00+00:00,4935.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section fro 4911 m to 4935 m MD. Drilling parameters : Flow 2050-2500 lpm / SPP 179-247 bar / 200 RPM / Torque 18-22 kNm / ROP 12 m/hrs / ECD 1,44-1,45 sg. Investigated ECD dependency on rate : 1,450 @ 2433 lpm / 1,442 @ 2278 lpm / 1,432 @ 2058 lpm. Performed MWD surevey on connection. Obtained ESD value of 1,354.",2.75 +15_9_F_10_2009_06_01.xml,NO 15/9-F-10,NO 15/9-F-10,2009-05-31T00:00:00+02:00,2009-06-01T00:00:00+02:00,2009-05-31 21:00:00+00:00,2009-05-31 22:00:00+00:00,4958.0,m,fixed,drilling -- drill,ok,success,"Drillied 8 1/2"" hole section from 4935 m to 4958 m MD. Drilling parameters : Flow 2400 lpm / SPP ~250 bar / 200 RPM / Torque 21-23 kNm / ROP 25 m/hrs / ECD 1,45-1,46 sg. Observed severe oil leakage from one of the TDS link tilt cylinders.",1.0 +15_9_F_10_2009_06_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-01T00:00:00+02:00,2009-06-02T00:00:00+02:00,2009-05-31 22:00:00+00:00,2009-06-01 02:00:00+00:00,4958.0,m,fixed,interruption -- other,ok,equipment failure,"Halted drilling operation for repair of TDS link tilt cylinder. Dismounted link tilt cylinder and brought to workshop for repair. Re-mounted link tilit cylinder. Meanwhile circulated in hole at 1300 lpm / SPP 85-89 bar. ECD 1,37-1,38 sg.",4.0 +15_9_F_10_2009_06_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-01T00:00:00+02:00,2009-06-02T00:00:00+02:00,2009-06-01 02:00:00+00:00,2009-06-01 04:00:00+00:00,4994.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4958 m to 4994 m MD. Drilling parameters : Flow 2400 lpm / SPP 240-245 bar / 200 RPM / Torque ~20 kNm / ROP 25 m/hrs / ECD 1,44-1,45 sg.Downlinked PD Xceed according to DDs instructions, had to pick off bottom in order to get downlink accepted. Observed high dropping tendency of BHA.",2.0 +15_9_F_10_2009_06_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-01T00:00:00+02:00,2009-06-02T00:00:00+02:00,2009-06-01 04:00:00+00:00,2009-06-01 19:45:00+00:00,5255.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 4994 m to 5255 m MD. Drilling parameters : Flow 2500 lpm / SPP 250-260 bar / 200 RPM / Torque 18-23 kNm / ROP 25 m/hrs / ECD 1,44-1,48 sg. Performed MWD survey on connections. Downlinked PD Xceed according to DDs instructions.",15.75 +15_9_F_10_2009_06_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-01T00:00:00+02:00,2009-06-02T00:00:00+02:00,2009-06-01 19:45:00+00:00,2009-06-01 20:15:00+00:00,5255.0,m,fixed,drilling -- other,ok,success,"Picked off bottom and circulated cuttings above BHA, Performed sticky test on BHA : 5 min static and then picking up. String came free at 225 MT upweight, last p/u weight 196 MT.",0.5 +15_9_F_10_2009_06_02.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-01T00:00:00+02:00,2009-06-02T00:00:00+02:00,2009-06-01 20:15:00+00:00,2009-06-01 22:00:00+00:00,5255.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated bottoms up while reciprocating string in order to reduce drag in well. Parameters : Flow 2000-2500 lpm / SPP 176-260 bar / 150-200 RPM / Torque 17-19 kNm / ECD 1,48=>1,45 sg.",1.75 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-01 22:00:00+00:00,2009-06-01 23:00:00+00:00,5255.0,m,fixed,formation evaluation -- log,ok,success,"Stopped rotation. Circulated at 2500 lpm. Took p/u weight 196 MT. Performed two sticky tests : 3 min - 198 MT p/u and 8 min 205 MT p/u weight. Downlinked Stethoscope. Positioned string with bit at 5249 m MD / probe depth 5215 m MD. Obtained pressure sample of 87,17 bar at 5215 m MD.",1.0 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-01 23:00:00+00:00,2009-06-02 00:15:00+00:00,5280.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 5255 m to 5280 m MD as adviced by geologist. Drilling parameters : Flow 2500 lpm / SPP 250-260 bar / 200 RPM / Torque 18-23 kNm / ROP 25 m/hrs / ECD 1,47-1,49 sg. Performed MWD survey on connection.",1.25 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 00:15:00+00:00,2009-06-02 01:15:00+00:00,5280.0,m,fixed,formation evaluation -- log,ok,success,"Downlinked Stethoscope. Positioned string with bit at 5264 m MD / probe depth 5230 m MD. P/u weight 205 MT. Obtained pressure sample of 88,07 bar at 5230 m MD.",1.0 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 01:15:00+00:00,2009-06-02 02:15:00+00:00,5300.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 5280 m to 5300 m MD as adviced by geologist. Drilling parameters : Flow 2300 lpm / SPP ~231 bar / 200 RPM / Torque ~22 kNm / ROP 25 m/hrs / ECD 1,48-1,49 sg. Performed MWD survey on connection.",1.0 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 02:15:00+00:00,2009-06-02 03:15:00+00:00,5300.0,m,fixed,formation evaluation -- log,ok,success,"Downlinked Stethoscope. Positioned string with bit at 5287 m MD / probe depth 5253 m MD. P/u weight 197 MT. Obtained pressure sample of 89,51 bar at 5253 m MD. High p/u weight when comming free with string (~230 MT), came down with string, started rotation and came free, no pack off tendency.",1.0 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 03:15:00+00:00,2009-06-02 04:00:00+00:00,5314.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 5300 m to 5314 m MD as adviced by geologist. Drilling parameters : Flow 2300 lpm / SPP ~233 bar / 200 RPM / Torque ~21 kNm / ROP 15-25 m/hrs / ECD 1,48-1,49 sg.",0.75 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 04:00:00+00:00,2009-06-02 05:30:00+00:00,5331.0,m,fixed,drilling -- drill,ok,success,"Drilled 8 1/2"" hole section from 5314 m to TD at 5331 m MD as adviced by geologist. Drilling parameters : Flow 2300 lpm / SPP ~235 bar / 200 RPM / Torque ~20 kNm / ROP 15 m/hrs / ECD 1,49 sg.",1.5 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 05:30:00+00:00,2009-06-02 07:45:00+00:00,5331.0,m,fixed,drilling -- circulating conditioning,ok,success,"Circulated hole clean while reciprocating string between 5331 m and 5320 m MD. Parametes : Flow 2300 lpm / SPP ~235 bar / 150-200 RPM / Torque 17-19 kNm / ECD 1,47-1,48 sg. Downlinked PD Xceed for tripping out.",2.25 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 07:45:00+00:00,2009-06-02 11:30:00+00:00,5320.0,m,fixed,drilling -- circulating conditioning,ok,success,"Set back one stand and continued to circulate well clean reciprocating stand beetween 5320 m and 5380 m MD. Parameters : Flow 2300 lpm / SPP 232-236 bar / 150-200 RPM / Torque ~18 kNm / ECD 1,48 sg.",3.75 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 11:30:00+00:00,2009-06-02 13:00:00+00:00,5215.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 5320 m to 5215 m MD. Parameters : Flow 2200 lpm / SPP 230-240 bar. Took >20 MT overpull at 5215 m MD. Attempted to rotate to move pipe down - negative. Worked string free by comming down with 60 MT downweight and applying 33 kNm - pipe free. Standpipe pressure stable around 235 bar. Washed and reamed upwards 2200 lpm / 20 RPM, took 20-25 MT overpull and string stalled out. Worked string free by setting down full string weight. Washed and reamed through tight area with 2200 lpm / 60-120 RPM.",1.5 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 13:00:00+00:00,2009-06-02 14:30:00+00:00,4960.0,m,fixed,drilling -- drill,ok,success,"Backreamed with 8 1/2"" drilling BHA on 5 1/2"" DP from 5320 m to 4960 m MD. Parameters : Flow 2300 lpm / SPP 239-226 bar / 60 RPM / Torque ~14 kNm / ECD 1,45-1,46 sg.",1.5 +15_9_F_10_2009_06_03.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-02T00:00:00+02:00,2009-06-03T00:00:00+02:00,2009-06-02 14:30:00+00:00,2009-06-02 22:00:00+00:00,4084.0,m,fixed,formation evaluation -- log,ok,success,"Backreamed from 4960 m to 4084 m MD while logging interval. Parameters : Flow 2300 lpm / 226=>207 bar / Rotation 60 RPM / Torque 16=>12 kNm / ECD 1,46=>1.43 sg / Pulling speed 4,5 m/min.",7.5 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-02 22:00:00+00:00,2009-06-03 02:00:00+00:00,3665.0,m,fixed,formation evaluation -- log,ok,success,"Backreamed from 4084 m to 3650 m MD while logging interval. Parameters : Flow 2300 lpm / 207=>192 bar / Rotation 60 RPM / Torque 12=>11 kNm / ECD 1,43=>1.41 sg / Pulling speed 4,5 m/min.",4.0 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 02:00:00+00:00,2009-06-03 02:45:00+00:00,3422.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 3665 m to 3422 m MD inside 9 5/8"" liner shoe. Pulled wet pipe.",0.75 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 02:45:00+00:00,2009-06-03 03:30:00+00:00,3422.0,m,fixed,drilling -- other,ok,success,"Flowchecked - well static. Pumped 5 m3 1,65 sg slug and allowed mud level to settle.",0.75 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 03:30:00+00:00,2009-06-03 04:00:00+00:00,3223.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 3422 m to 3223 m MD.",0.5 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 04:00:00+00:00,2009-06-03 06:15:00+00:00,2175.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5"" DP from 3223 m to 2175 m MD. Tripping speed 465 m/hr.",2.25 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 06:15:00+00:00,2009-06-03 06:45:00+00:00,2175.0,m,fixed,drilling -- other,ok,success,"Changed from 5 1/2"" to 5"" handling equipment. Pumped 5 m3 1,65 sg slug and allowed mud level to settle.",0.5 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 06:45:00+00:00,2009-06-03 09:00:00+00:00,1360.0,m,fixed,drilling -- other,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 2175 m to 1360 m MD. Tripping speed 362 m/hr. Problems with aft PRS claw.",2.25 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 09:00:00+00:00,2009-06-03 09:15:00+00:00,1360.0,m,fixed,interruption -- other,ok,equipment failure,Troubleshot aft PRS claw.,0.25 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 09:15:00+00:00,2009-06-03 11:15:00+00:00,139.0,m,fixed,drilling -- drill,ok,success,"POOH with 8 1/2"" drilling BHA on 5 1/2"" DP from 1360 m to 139 m MD. Tripping speed 542 m/hr.",2.0 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 11:15:00+00:00,2009-06-03 11:30:00+00:00,139.0,m,fixed,drilling -- other,ok,success,Flow checked well prior to pulling BHA - well static. Meanwhile held toolbox talk for handling BHA.,0.25 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 11:30:00+00:00,2009-06-03 12:00:00+00:00,114.0,m,fixed,drilling -- trip,ok,success,"POOH with 8 1/2"" drilling BHA. Racked back stand of 5 1/2"" HWDP. Removed automatic slip. Installed master bushing.",0.5 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 12:00:00+00:00,2009-06-03 15:00:00+00:00,0.0,m,fixed,drilling -- trip,ok,success,"Broke and laid down jar and accelerator. Racked back stand of 5 1/2"" HWDP. Broke and laid down Stethoscope, Sonicvision, Telescope, Echoscope and 8 1/2"" PD exceed. + +Recessed operation due to exhaust fumes on drillfloor (F-99).",3.0 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 15:00:00+00:00,2009-06-03 18:45:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"Resumed operation on F-10 at 19:30. + +Serviced and greased TDS. De-isolated equipment. Dressed IR with 3 1/2"" dies. Installed 3 1/2"" inserts in BX elevator.",3.75 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 18:45:00+00:00,2009-06-03 19:00:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"Held toolbox talk for running 3 1/2"" DP.",0.25 +15_9_F_10_2009_06_04.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-03T00:00:00+02:00,2009-06-04T00:00:00+02:00,2009-06-03 19:00:00+00:00,2009-06-03 22:00:00+00:00,326.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 3 1/2"" DP open ended from surface to 326 m MD. Picked up singles from deck. Drifted DP to 2 1/4"". Observed leakage on PS-21 slips.",3.0 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-03 22:00:00+00:00,2009-06-03 22:30:00+00:00,326.0,m,fixed,interruption -- other,ok,equipment failure,Removed PS-21 from RT. Installed master bushing and bowl.,0.5 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-03 22:30:00+00:00,2009-06-03 23:30:00+00:00,353.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 3 x 3 1/2"" singles to 353 m MD using manual slips. Changed inserts in BX from 3 1/2"" to 5"". Installed and made up 3 1/2"" x 5"" x-over. Picked up stand of 5 1/2"" DP and made up to x-over.",1.0 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-03 23:30:00+00:00,2009-06-04 00:15:00+00:00,353.0,m,fixed,interruption -- other,ok,equipment failure,Removed master bushing and outer ring. Installed PS-30 slips in RT and hooked up same.,0.75 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 00:15:00+00:00,2009-06-04 00:30:00+00:00,353.0,m,fixed,plug abandon -- trip,ok,success,"Dressed PS-30 with 5"" slips inserts.",0.25 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 00:30:00+00:00,2009-06-04 02:45:00+00:00,1010.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 5"" DP from 353 m to 1010 m MD. Got incorrect volume in triptanks, well apparently gaining. Investigated situation, suspected partial plugging of DP. Flowchecked for 15 min - lost 200 liter (pipe filling).",2.25 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 02:45:00+00:00,2009-06-04 03:15:00+00:00,1010.0,m,fixed,plug abandon -- trip,ok,success,Looked down DP when in slips and observed that pipe was not filled properly. Made up TDS and filled pipe with approx 200 liter before pressure build up. Performed pump test - 11 bar SPP @ 500 lpm and 33 bar SPP @ 1000 lpm - good match with hydraulic simulations.,0.5 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 03:15:00+00:00,2009-06-04 04:00:00+00:00,1291.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 5"" DP from 1010 m to 1291 m MD.",0.75 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 04:00:00+00:00,2009-06-04 05:30:00+00:00,2103.0,m,fixed,plug abandon -- trip,ok,success,RIH with cement string from 1291m to 2103m MD.,1.5 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 05:30:00+00:00,2009-06-04 07:00:00+00:00,2103.0,m,fixed,plug abandon -- trip,ok,success,"Emptied trip tank, moved bent 5"" DP in derrick. Changed from 5"" to 5 ½"" DP handling equipment. Broke circulation with 3000 l/min, 300 bar. (2500 l/min, 229 bar.)",1.5 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 07:00:00+00:00,2009-06-04 09:15:00+00:00,3440.0,m,fixed,plug abandon -- trip,ok,success,RIH with cement string from 2103m to 3440m MD.,2.25 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 09:15:00+00:00,2009-06-04 09:30:00+00:00,3440.0,m,fixed,plug abandon -- trip,ok,success,"Broke circulation at 3440m MD, 500 l/min, 30 bar.",0.25 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 09:30:00+00:00,2009-06-04 14:00:00+00:00,5168.0,m,fixed,plug abandon -- trip,ok,success,RIH with cement string from 3440m to 5168m MD.,4.5 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 14:00:00+00:00,2009-06-04 16:00:00+00:00,5331.0,m,fixed,plug abandon -- trip,ok,success,"Washed down from 5168m to tagging depth, 5331m MD. 500 l/min, 35 bar.",2.0 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 16:00:00+00:00,2009-06-04 18:00:00+00:00,5326.0,m,fixed,drilling -- casing,ok,success,"Pulled 5m, staged up pumps, circulated and conditioned mud at 5326m MD, 2400 l/min, 281 bar, 25 rpm, 12-13 kNm. Simultaneously cleaned pit for mixing new spacer for cement job, due to contamination in first spacer.",2.0 +15_9_F_10_2009_06_05.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-04T00:00:00+02:00,2009-06-05T00:00:00+02:00,2009-06-04 18:00:00+00:00,2009-06-04 22:00:00+00:00,5326.0,m,fixed,plug abandon -- other,ok,operation failed,"Cleaned pit for mixing new spacer for cement job, due to contamination in first spacer.",4.0 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-04 22:00:00+00:00,2009-06-04 22:30:00+00:00,5326.0,m,fixed,plug abandon -- other,ok,operation failed,"Continued to clean pit and mixing lines. circulated and conditioned mud at 5326m MD, 2400 l/min, 281 bar, 25 rpm, 12-13 kNm.",0.5 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-04 22:30:00+00:00,2009-06-04 23:00:00+00:00,5326.0,m,fixed,plug abandon -- other,ok,operation failed,"Filled pit with drill water and performed clorine check prior to start mixing cement spacer. Circulated and conditioned mud at 5326m MD, 2400 l/min, 281 bar, 25 rpm, 12-13 kNm.",0.5 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-04 23:00:00+00:00,2009-06-05 02:45:00+00:00,5326.0,m,fixed,plug abandon -- other,ok,operation failed,"Mixed cement spacer according to specifications. Simultaneously removed claw from aft PRS. Held tool box talk prior to cement job. Circulated and conditioned mud at 5326m MD, 2400 l/min, 281 bar, 25 rpm, 12-13 kNm.",3.75 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 02:45:00+00:00,2009-06-05 03:15:00+00:00,5326.0,m,fixed,plug abandon -- trip,ok,success,"Stopped pumps and rotation, took up weight, needed 230 ton to move pipe, than 200 ton up weight. Needed to rotate to come down, 156 ton. No circulation. Performed line test from cement unit to rigfloor 200 bar, 10 min.",0.5 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 03:15:00+00:00,2009-06-05 04:00:00+00:00,5326.0,m,fixed,plug abandon -- other,ok,operation failed,"Mixed cement spacer according to specifications. Circulated with 1000 l/min, 65 bar. 25 rpm, 13-17 kNm.",0.75 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 04:00:00+00:00,2009-06-05 05:30:00+00:00,5329.0,m,fixed,plug abandon -- other,ok,success,"Circulated and conditioned mud at 5329m MD. 1000 l/min, 65 bar.",1.5 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 05:30:00+00:00,2009-06-05 05:45:00+00:00,5329.0,m,fixed,plug abandon -- cement plug,ok,success,Toolbox talk prior to pump cement plug.,0.25 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 05:45:00+00:00,2009-06-05 06:00:00+00:00,5329.0,m,fixed,plug abandon -- cement plug,ok,success,Prepared for pumping spacer. Informed engineer and production. cement room had priority for use of air.,0.25 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 06:00:00+00:00,2009-06-05 06:15:00+00:00,5329.0,m,fixed,plug abandon -- cement plug,ok,success,"Pumped 7m3, 320 strokes 1,47 sg spacer, chased with 0,5m3, 23 strokes OBM. 1000 l/min, 68 bar.",0.25 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 06:15:00+00:00,2009-06-05 06:45:00+00:00,5329.0,m,fixed,plug abandon -- cement plug,ok,success,"Mixed and pumped 12,7m3 1,90 sg Silica cement. Displaced to rigfloor with 892 ltr. drill water.",0.5 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 06:45:00+00:00,2009-06-05 07:30:00+00:00,5329.0,m,fixed,plug abandon -- cement plug,ok,success,"Displaced cement down string, 48m3, 2200 strokes. 1900 l/min, 110 bar. Reduced rate at 43m3. 1000 l/min, 75 bar.",0.75 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 07:30:00+00:00,2009-06-05 09:30:00+00:00,5010.0,m,fixed,plug abandon -- trip,ok,success,"Got back pressure in string while pulling out of cement, connected DDM and pumped 6 strokes, 130 l per stand.",2.0 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 09:30:00+00:00,2009-06-05 10:00:00+00:00,5010.0,m,fixed,plug abandon -- trip,ok,success,"Inserted 2 sponge balls, due to back pressure we had to brake first single below DDM.",0.5 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 10:00:00+00:00,2009-06-05 10:45:00+00:00,4900.0,m,fixed,plug abandon -- trip,ok,success,"Pulled from 5010m to 4900m MD, pumped sponge balls through string. 2500 l/min, 290 bar.",0.75 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 10:45:00+00:00,2009-06-05 11:00:00+00:00,4900.0,m,fixed,plug abandon -- cement plug,ok,success,Flushed stand pipe manifoild after cement job.,0.25 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 11:00:00+00:00,2009-06-05 13:45:00+00:00,3795.0,m,fixed,plug abandon -- trip,ok,success,POOH wet with cement string from 4900m to 3795m MD.,2.75 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 13:45:00+00:00,2009-06-05 14:00:00+00:00,3795.0,m,fixed,plug abandon -- trip,ok,success,Broke circulation and filled trip tank.,0.25 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 14:00:00+00:00,2009-06-05 15:00:00+00:00,3795.0,m,fixed,plug abandon -- trip,ok,success,"Pumped 30m3, 1370 strokes Hi-Vis pill. 1300 l/min, 97 bar. Displaced Hi-Vis pill with 30,5m3, 1396 strokes. 1986 l/min, 194 bar.",1.0 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 15:00:00+00:00,2009-06-05 15:30:00+00:00,3795.0,m,fixed,plug abandon -- trip,ok,success,64 bar backpressure in string after displacement of Hi-Vis pill. Bled back 300 ltr. 0 bar.,0.5 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 15:30:00+00:00,2009-06-05 17:15:00+00:00,3495.0,m,fixed,plug abandon -- trip,ok,success,POOH wet from 3795m to 3495m MD.,1.75 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 17:15:00+00:00,2009-06-05 18:45:00+00:00,3495.0,m,fixed,plug abandon -- cement plug,ok,success,"Established circulation 2750 l/min, 290 bar, 25 rpm, 8-10 kNm. Observed 73 bar with 220 l/min when broke circulation. Meanwhile held toolbox talk prior to cement job. Observed good Hi-Vis return at surface.",1.5 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 18:45:00+00:00,2009-06-05 19:00:00+00:00,3495.0,m,fixed,plug abandon -- cement plug,ok,success,Broke off double DP and dropped CST.,0.25 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 19:00:00+00:00,2009-06-05 20:00:00+00:00,3495.0,m,fixed,plug abandon -- cement plug,ok,success,"Displaced CST with 1000 l/min, 53 bar. Reduced rate to 500 l/min, 22 bar after 29,6m3, 1355 strokes. When CST enters 3 1/2"" DP, observed pressure increase to 26 bar, after 32,7m3, 1492 stroles pumped.",1.0 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 20:00:00+00:00,2009-06-05 20:15:00+00:00,3490.0,m,fixed,plug abandon -- cement plug,ok,success,"Picked up 5m to 3490m MD. pumped 9m3, 410 strokes, 1,47 sg spacer, 1800 l/min, 140 bar.",0.25 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 20:15:00+00:00,2009-06-05 20:45:00+00:00,3490.0,m,fixed,plug abandon -- cement plug,ok,success,"Mixed and pumped 10,3m3 1,92 sg ""G"" cement. 800 l/min, 30 bar from cement unit.",0.5 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 20:45:00+00:00,2009-06-05 21:00:00+00:00,3490.0,m,fixed,plug abandon -- cement plug,ok,success,"Displaced cement with rig pumps, 2000 l/min, 125 bar, 50 rpm, 6-8 kNm. Reduced rate to 1000 l/min, 29 bar.",0.25 +15_9_F_10_2009_06_06.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-05T00:00:00+02:00,2009-06-06T00:00:00+02:00,2009-06-05 21:00:00+00:00,2009-06-05 22:00:00+00:00,2951.0,m,fixed,plug abandon -- trip,ok,success,POOH with cement string from 3490m to 2951m MD.,1.0 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-05 22:00:00+00:00,2009-06-05 22:45:00+00:00,2800.0,m,fixed,plug abandon -- trip,ok,success,Continued POOH with cement string from 2951m to 2800m MD.,0.75 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-05 22:45:00+00:00,2009-06-06 00:30:00+00:00,2800.0,m,fixed,plug abandon -- trip,ok,success,"Flushed manifold and pumped 2 sponge balls. 3000 l/min, 297 bar. 60 rpm, 7 kNm. Meanwhile moved rollers and HTS and prepared for L/D 5"" DP on deck.",1.75 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 00:30:00+00:00,2009-06-06 01:00:00+00:00,2800.0,m,fixed,plug abandon -- trip,ok,success,"Pumped and displaced 4,7m3, slug 1100 l/min, 53 bar. Filled trip tank with rigpumps.",0.5 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 01:00:00+00:00,2009-06-06 02:30:00+00:00,2080.0,m,fixed,plug abandon -- trip,ok,success,POOH from 2800m to 2080m MD.,1.5 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 02:30:00+00:00,2009-06-06 03:15:00+00:00,2080.0,m,fixed,plug abandon -- trip,ok,success,"Changed handling equipment from 5 1/2"" to 5"" DP. Serviced PRS.",0.75 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 03:15:00+00:00,2009-06-06 03:30:00+00:00,2080.0,m,fixed,plug abandon -- trip,ok,success,"Tool Box Talk prior to L/D 5"" DP on deck.",0.25 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 03:30:00+00:00,2009-06-06 03:45:00+00:00,2080.0,m,fixed,plug abandon -- trip,ok,success,Changed inserts in mud bucket.,0.25 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 03:45:00+00:00,2009-06-06 04:00:00+00:00,2080.0,m,fixed,plug abandon -- trip,ok,success,Pumped and displaced slug.,0.25 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 04:00:00+00:00,2009-06-06 05:00:00+00:00,2023.0,m,fixed,plug abandon -- trip,ok,success,"POOH and L/D 5"" DP on deck from 2080m to 2023m MD.",1.0 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 05:00:00+00:00,2009-06-06 05:15:00+00:00,2023.0,m,fixed,plug abandon -- trip,ok,success,"Held Tool Box Talk with on comming shift prior to L/D 5"" DP on deck.",0.25 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 05:15:00+00:00,2009-06-06 13:30:00+00:00,355.0,m,fixed,plug abandon -- trip,ok,success,"POOH and L/D 5"" DP on deck from 2023m to 355m MD.",8.25 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 13:30:00+00:00,2009-06-06 14:00:00+00:00,355.0,m,fixed,plug abandon -- trip,ok,success,"Cleared and cleaned rigfloor. Changed to 3 1/2"" handling equipment.",0.5 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 14:00:00+00:00,2009-06-06 16:30:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"POOH and L/D 1 joint of 3 1/2"" DP. POOH and racked 3 1/2"" DP on setback from 355m to surface.",2.5 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 16:30:00+00:00,2009-06-06 16:45:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,Cleared and cleaned rigfloor.,0.25 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 16:45:00+00:00,2009-06-06 17:30:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,"Serviced TDS, FWD and AFT PRS.",0.75 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 17:30:00+00:00,2009-06-06 17:45:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,Held Tool Box Talk prior to cut & slip drill line.,0.25 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 17:45:00+00:00,2009-06-06 20:15:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,Slipped & cut dril line. Meanwhile held Tool Box Talk and performed line test prior to test of cement plug.,2.5 +15_9_F_10_2009_06_07.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-06T00:00:00+02:00,2009-06-07T00:00:00+02:00,2009-06-06 20:15:00+00:00,2009-06-06 22:00:00+00:00,0.0,m,fixed,plug abandon -- cement plug,ok,success,"Attempted to pressure test cement plug. Pressured up to 50 bar, than in steps of 20 bar. Observed leak of 0,5-1 bar/min. between steps. At 190 bar pressure flattened out with constant pump rate. Stopped pumping, pressure dropped rapidly to 170 bar. Bled off pressure. Discussed further operation with town. Meanwhile crew had Tool Box Talk prior to run EZSV plug.",1.75 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-06 22:00:00+00:00,2009-06-06 23:30:00+00:00,0.0,m,fixed,plug abandon -- mechanical plug,ok,success,Meeting about next operation. Decided to continue as per DOP and run EZSV plug. Meanwhile repaired leak on AFT iron roughneck and serviced TDS.,1.5 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-06 23:30:00+00:00,2009-06-07 00:45:00+00:00,0.0,m,fixed,plug abandon -- mechanical plug,ok,success,"Prepared and made up 9 5/8"" EZSV plug to 3 1/2"" DP.",1.25 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 00:45:00+00:00,2009-06-07 02:15:00+00:00,347.0,m,fixed,plug abandon -- trip,ok,success,"RIH with EZSV plug on 3 1/2"" DP from surface to 347m MD.",1.5 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 02:15:00+00:00,2009-06-07 04:00:00+00:00,715.0,m,fixed,plug abandon -- trip,ok,success,"Changed from 3 1/2"" to 5 1/2"" DP handling equipment. Emptied trip tank. RIH with EZSV plug on 5 1/2"" DP from 347m to 715m MD.",1.75 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 04:00:00+00:00,2009-06-07 05:00:00+00:00,1118.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 9 5/8"" EZSV plug from 715m to 1118m MD.",1.0 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 05:00:00+00:00,2009-06-07 06:00:00+00:00,1118.0,m,fixed,plug abandon -- trip,ok,success,"Moved 17 stands of 5 1/2"" DP, not wiped with sponge ballls.",1.0 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 06:00:00+00:00,2009-06-07 09:00:00+00:00,2467.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 9 5/8"" EZSV plug from 1118m to 2467m MD.",3.0 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 09:00:00+00:00,2009-06-07 09:30:00+00:00,2467.0,m,fixed,plug abandon -- trip,ok,success,"Broke circulation at 2467m MD, 110 l/min, 14 bar. Meanwhile moved rest 11 stands of 5 1/2"" DP not flushed with sponge balls.",0.5 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 09:30:00+00:00,2009-06-07 10:00:00+00:00,2467.0,m,fixed,plug abandon -- trip,ok,success,Flushed and verified line up from cement unit through TDS and BOP kill line for test of cement plug.,0.5 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 10:00:00+00:00,2009-06-07 10:45:00+00:00,2467.0,m,fixed,plug abandon -- trip,ok,success,Attempted to test cement plug to 195 bar. Observed 10 bar drop in 10 min. Than drop increased.,0.75 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 10:45:00+00:00,2009-06-07 11:00:00+00:00,2467.0,m,fixed,plug abandon -- trip,ok,success,"Flushed lines, meanwhile function tested BOP.",0.25 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 11:00:00+00:00,2009-06-07 12:30:00+00:00,2560.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 9 5/8"" EZSV plug from 2467m to 2560m MD.",1.5 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 12:30:00+00:00,2009-06-07 13:15:00+00:00,2560.0,m,fixed,plug abandon -- mechanical plug,ok,success,Set EZSV plug as per Halliburton procedures. Released from and pulled RT out of same.,0.75 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 13:15:00+00:00,2009-06-07 13:30:00+00:00,2555.0,m,fixed,plug abandon -- mechanical plug,ok,success,"Installed TIW and pump in sub, lined up to cement unit.",0.25 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 13:30:00+00:00,2009-06-07 14:15:00+00:00,2555.0,m,fixed,plug abandon -- mechanical plug,ok,success,"Verified line up, performed line test from cement unit, 200 bar, 10 min.",0.75 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 14:15:00+00:00,2009-06-07 15:00:00+00:00,2555.0,m,fixed,plug abandon -- mechanical plug,ok,success,"Pressure tested EZSV plug from above to 165 bar 10 min, OK.",0.75 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 15:00:00+00:00,2009-06-07 15:30:00+00:00,2555.0,m,fixed,plug abandon -- mechanical plug,ok,success,Tool Box Talk prior to cement job.,0.5 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 15:30:00+00:00,2009-06-07 17:00:00+00:00,2555.0,m,fixed,plug abandon -- mechanical plug,ok,success,"With cement unit, mixed and pumped 10,3m3 1,92 sg ""G"" cenent slurry, displaced to rigfloor with 892 ltr. drill water. With rig pumps, displaced cement with 23,1m3, 1057 strokes of 1,32 sg OBM. 1800 l/min. Reduced pump rate to 1000 l/min. after 18m3, 821 strokes.",1.5 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 17:00:00+00:00,2009-06-07 18:30:00+00:00,2300.0,m,fixed,plug abandon -- trip,ok,success,"POOH from 2555m to 2300m MD, dropped 2 x sponge balls. Circulated 1,5 x string volume 33m3, 1505 strokes.",1.5 +15_9_F_10_2009_06_08.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-07T00:00:00+02:00,2009-06-08T00:00:00+02:00,2009-06-07 18:30:00+00:00,2009-06-07 22:00:00+00:00,347.0,m,fixed,plug abandon -- trip,ok,success,POOH with EZSV RT from 2300m to 374m MD. Max. tripping speed 1200 m/hr.,3.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-07 22:00:00+00:00,2009-06-07 23:00:00+00:00,347.0,m,fixed,plug abandon -- trip,ok,success,"Changed handling equipment from 5 1/2"" to 3 1/2"" DP.",1.0 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-07 23:00:00+00:00,2009-06-08 00:30:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"POOH with 9 5/8"" EZSV plug RT on 3 1/2"" DP from 347m to surface.",1.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 00:30:00+00:00,2009-06-08 00:45:00+00:00,0.0,m,fixed,plug abandon -- mechanical plug,ok,success,"Tool Box Talk prior make up and run 13 3/8"" EZSV plug.",0.25 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 00:45:00+00:00,2009-06-08 01:15:00+00:00,0.0,m,fixed,plug abandon -- mechanical plug,ok,success,"Changed to 5"" inserts in elevator. Made up 13 3/8"" EZSV plug to 5"" stand according to Halliburton procedures. Plug set as bridge plug. (closed end)",0.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 01:15:00+00:00,2009-06-08 01:45:00+00:00,0.0,m,fixed,plug abandon -- mechanical plug,ok,success,"Installed 5"" inserts in PS-30 slips. Cleaned and cleared rigfloor.",0.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 01:45:00+00:00,2009-06-08 04:00:00+00:00,530.0,m,fixed,plug abandon -- mechanical plug,ok,success,"RIH with 13 3/8"" EZSV plug from surface to 530m MD.",2.25 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 04:00:00+00:00,2009-06-08 07:30:00+00:00,1590.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 13 3/8"" EZSV packer from 530m to 1590m MD. Filled string every 5 stands.",3.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 07:30:00+00:00,2009-06-08 08:00:00+00:00,1590.0,m,fixed,plug abandon -- mechanical plug,ok,success,"Set 13 3/8"" EZSV plug at 1590m MD according to Halliburton procedure.",0.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 08:00:00+00:00,2009-06-08 08:30:00+00:00,1590.0,m,fixed,plug abandon -- mechanical plug,ok,success,Cleared and cleaned rigfloor prior to POOH.,0.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 08:30:00+00:00,2009-06-08 09:00:00+00:00,1536.0,m,fixed,plug abandon -- trip,ok,success,"POOH with 13 3/8"" EZSV plug RT from 1590m to 1536m MD. Pumped slug, filled trip tank.",0.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 09:00:00+00:00,2009-06-08 10:30:00+00:00,325.0,m,fixed,plug abandon -- trip,ok,success,"POOH with 13 3/8"" EZSV plug RT from 1536m to 325m MD.",1.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 10:30:00+00:00,2009-06-08 11:00:00+00:00,325.0,m,fixed,plug abandon -- trip,ok,success,"Changed from 5 1/2"" to 5"" handling equipment. Tool Box Talk prior to L/D 5"" DP on deck.",0.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 11:00:00+00:00,2009-06-08 13:30:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"L/D on deck 5"" DP from 325m to surface.",2.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 13:30:00+00:00,2009-06-08 14:00:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"B/O EZSV plug RT, inspected, cleaned and L/D on deck.",0.5 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 14:00:00+00:00,2009-06-08 15:00:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"Changed to 5 1/2"" inserts in elevator. P/U and M/U Bull nose to 5 1/2"" stand. Changed to 5 1/2"" inserts in PS-30 slips.",1.0 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 15:00:00+00:00,2009-06-08 17:15:00+00:00,1590.0,m,fixed,plug abandon -- trip,ok,success,"RIH with Bull nose on 5 1/2"" DP from surface to 1590m MD, tagged 13 3/8"" EZSV plug with 5 ton at 1590m, pulled 5m. Meanwhile held Tool Box Talk prior to displace to 1,51 sg OBM from 1585m MD to surface.",2.25 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 17:15:00+00:00,2009-06-08 20:15:00+00:00,1585.0,m,fixed,plug abandon -- trip,ok,success,"Displaced Well, kill / choke line, chokemanifoild from 1,32 sg OBM to 1,51 sg OBM.",3.0 +15_9_F_10_2009_06_09.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-08T00:00:00+02:00,2009-06-09T00:00:00+02:00,2009-06-08 20:15:00+00:00,2009-06-08 22:00:00+00:00,687.0,m,fixed,plug abandon -- trip,ok,success,POOH with Bull nose from 1585m to 687m MD.,1.75 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-08 22:00:00+00:00,2009-06-08 23:00:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,POOH with Bull nose from 687m to surface.,1.0 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-08 23:00:00+00:00,2009-06-08 23:45:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,Cleared rigfloor. Removed PS-30 slips. Installed master bushing. Held Tool Box Talk.,0.75 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-08 23:45:00+00:00,2009-06-09 00:15:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,P/U Wear Bushing Running Tool from deck. Installed same with jet sub below.,0.5 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 00:15:00+00:00,2009-06-09 00:30:00+00:00,140.0,m,fixed,plug abandon -- trip,ok,success,"RIH with WB RT on 5 1/2"" HWDP / DP from surface to 140m.",0.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 00:30:00+00:00,2009-06-09 00:45:00+00:00,140.0,m,fixed,plug abandon -- trip,ok,success,"Jetted Well Head / Wear Bushing. 2600 l/min, 45 bar.",0.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 00:45:00+00:00,2009-06-09 01:00:00+00:00,140.0,m,fixed,plug abandon -- trip,ok,success,Connected RT to Wear Bushing according to Vetco procedures. Needed 50 ton to pull wear bushing free.,0.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 01:00:00+00:00,2009-06-09 02:00:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,POOH with Wear bushing from 140m.,1.0 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 02:00:00+00:00,2009-06-09 02:15:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"B/O Wear Bushing, racked last stand. Broke Jet sub off wear bushing RT. Scormarks outside wear bushing.",0.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 02:15:00+00:00,2009-06-09 04:00:00+00:00,140.0,m,fixed,plug abandon -- trip,ok,success,"Made up SRT with jet sub below. RIH to jet Well Head, pull MS-seal, jet again and POOH.",1.75 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 04:00:00+00:00,2009-06-09 05:30:00+00:00,140.0,m,fixed,plug abandon -- other,ok,success,"With closed annular, pulled MS-seal. 15 ton over pull. Pulled 1,5m no pressure on choke.",1.5 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 05:30:00+00:00,2009-06-09 05:45:00+00:00,138.5,m,fixed,plug abandon -- other,ok,success,"Opened annular, flow checked open well, well static.",0.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 05:45:00+00:00,2009-06-09 07:30:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"POOH with MS-seal from 138,5m to surface. Re-engaged RT in j-slot. Attempted to remove MS-seal from RT, no go. L/D RT and MS-seal.",1.75 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 07:30:00+00:00,2009-06-09 08:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"P/U wear Bushing RT, removed old WB, installed new.",0.5 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 08:00:00+00:00,2009-06-09 09:15:00+00:00,138.5,m,fixed,plug abandon -- other,ok,success,"RIH with wear bushing to 138,5m. Washed down 2775 l/min, 46 bar, 4 rpm. Set wear bushing according to Vetco procedures.",1.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 09:15:00+00:00,2009-06-09 10:15:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"POOH with wear bushing RT, re-set tool and L/D on deck.",1.0 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 10:15:00+00:00,2009-06-09 11:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Changed dies in AFT AR prior to collar run. Meanwhile cleaned rigfloor after wear bushing run.,0.75 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 11:00:00+00:00,2009-06-09 12:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"P/U cutting tool and tested same, knives activated at 20 strokes, 440 ltr / hrs, 10 bar. RIH 2 stands.",1.0 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 12:00:00+00:00,2009-06-09 12:15:00+00:00,80.0,m,fixed,plug abandon -- other,ok,success,Changed from Master bushing to PS-21 slips.,0.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 12:15:00+00:00,2009-06-09 17:00:00+00:00,1580.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 13 3/8"" casing cutters from 80m to 1580m MD.",4.75 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 17:00:00+00:00,2009-06-09 17:15:00+00:00,1580.0,m,fixed,plug abandon -- other,ok,success,"Took up/down weight, 116/105 ton. Free rotation weight, 110 ton, 4-6 kNm.",0.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 17:15:00+00:00,2009-06-09 17:30:00+00:00,1590.0,m,fixed,plug abandon -- other,ok,success,"Tagged 13 3/8"" EZSV plug, set down 3 ton, 1589,9m. MD",0.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 17:30:00+00:00,2009-06-09 18:00:00+00:00,1580.0,m,fixed,plug abandon -- other,ok,success,"Pulled 10 m. started pumps, 550 l/min, 62 bar. Stopped pumps.",0.5 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 18:00:00+00:00,2009-06-09 18:30:00+00:00,1580.0,m,fixed,plug abandon -- other,ok,success,"Started rotation, 100 rpm, 4-6 kNm, started pumps, 540 l/min, 60 bar. After 3-4 min, observed pressure drop from 60 bar to 18-19 bar. Continued for 2-3 min. Stopped rotation and pumps. Flow checked.",0.5 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 18:30:00+00:00,2009-06-09 19:00:00+00:00,1580.0,m,fixed,plug abandon -- other,ok,success,"Pulled 1,5m started pumps, 300 l/min, 18 bar. Slacked off string to 1580, took weight, 2 ton, pressure dropped to 6-8 bar.",0.5 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 19:00:00+00:00,2009-06-09 19:15:00+00:00,1580.0,m,fixed,plug abandon -- other,ok,success,"Pumped and displaced 4,7m3 1,71 sg slug.",0.25 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 19:15:00+00:00,2009-06-09 21:15:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"POOH with 13 3/8"" casing cutter from 1580m MD, to surface.",2.0 +15_9_F_10_2009_06_10.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-09T00:00:00+02:00,2009-06-10T00:00:00+02:00,2009-06-09 21:15:00+00:00,2009-06-09 22:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Changed saver sub in DDM.,0.75 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-09 22:00:00+00:00,2009-06-09 23:15:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Continue to change saver sub in DDM.,1.25 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-09 23:15:00+00:00,2009-06-10 01:15:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Broke off X/O above cutters.,2.0 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 01:15:00+00:00,2009-06-10 01:45:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,P/U and M/U wear Bushing RT.,0.5 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 01:45:00+00:00,2009-06-10 02:30:00+00:00,140.0,m,fixed,plug abandon -- other,ok,success,RIH with WB RT from surface to 140m.,0.75 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 02:30:00+00:00,2009-06-10 02:45:00+00:00,140.0,m,fixed,plug abandon -- other,ok,success,"Retreived wear bushing, 1-2 ton over pull.",0.25 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 02:45:00+00:00,2009-06-10 03:30:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,POOH with wear bushing from 140m to surface.,0.75 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 03:30:00+00:00,2009-06-10 04:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,L/D wear bushing and RT on deck.,0.5 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 04:00:00+00:00,2009-06-10 07:00:00+00:00,77.0,m,fixed,plug abandon -- trip,ok,success,"P/U and RIH with spear assembly. 2 stands of 8"" DC from set back and 3 singles from deck.",3.0 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 07:00:00+00:00,2009-06-10 07:30:00+00:00,77.0,m,fixed,interruption -- maintain,ok,success,"Serviced TDS, inspected for loose items prior to pulling casing.",0.5 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 07:30:00+00:00,2009-06-10 08:00:00+00:00,141.8,m,fixed,plug abandon -- trip,ok,success,"RIH to setting depth at 141,8m",0.5 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 08:00:00+00:00,2009-06-10 08:15:00+00:00,141.8,m,fixed,plug abandon -- other,ok,success,"Engaged spear in 13 3/8"" casing as per Smith procedure. Pulled casing free with 286 ton on weight indicator. 75 ton overpull.",0.25 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 08:15:00+00:00,2009-06-10 10:00:00+00:00,140.0,m,fixed,plug abandon -- other,ok,success,"Pulled up 2m, circulated out old mud as per mud eng. instructions. 3000 l/min, 63 bar.",1.75 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 10:00:00+00:00,2009-06-10 10:15:00+00:00,140.0,m,fixed,plug abandon -- other,ok,success,"Pumped and displaced 1m3 1,71 sg slug.",0.25 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 10:15:00+00:00,2009-06-10 12:00:00+00:00,1443.0,m,fixed,plug abandon -- trip,ok,success,"POOH with 5 1/2"" HWDP, 8"" DC and 13 3/8"" casing from 1580m to 1443m.",1.75 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 12:00:00+00:00,2009-06-10 12:15:00+00:00,1443.0,m,fixed,plug abandon -- trip,ok,success,"M/U TDS and pumped remaining 3,6m3 1,71 sg slug.",0.25 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 12:15:00+00:00,2009-06-10 12:30:00+00:00,1443.0,m,fixed,plug abandon -- other,ok,success,Held Tool Box Talk prior to rig up casing handling equipment.,0.25 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 12:30:00+00:00,2009-06-10 13:30:00+00:00,1440.0,m,fixed,plug abandon -- other,ok,success,Set hanger in slips. Released spear as per Smiths instruction.,1.0 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 13:30:00+00:00,2009-06-10 16:30:00+00:00,1440.0,m,fixed,drilling -- casing,ok,success,"Rigged up 13 3/8"" casing handling equipment.",3.0 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 16:30:00+00:00,2009-06-10 17:15:00+00:00,1440.0,m,fixed,drilling -- casing,ok,equipment failure,"Transport frame for 13 3/8"" casing tong could not run to well certer. Guides on weels too big. Trouble shot.",0.75 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 17:15:00+00:00,2009-06-10 20:45:00+00:00,1440.0,m,fixed,drilling -- casing,ok,equipment failure,"Disconnected guide wheels, grinded 1cm off guides.",3.5 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 20:45:00+00:00,2009-06-10 21:30:00+00:00,1440.0,m,fixed,drilling -- casing,ok,equipment failure,Installed wheels on weatherford casing tong. Adjusted and function tested tong.,0.75 +15_9_F_10_2009_06_11.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-10T00:00:00+02:00,2009-06-11T00:00:00+02:00,2009-06-10 21:30:00+00:00,2009-06-10 22:00:00+00:00,1435.0,m,fixed,plug abandon -- trip,ok,success,"Broke 13 3/8"" casing hanger, removed with crane. Broke out 1 more joint.,",0.5 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-10 22:00:00+00:00,2009-06-10 22:30:00+00:00,1399.0,m,fixed,plug abandon -- trip,ok,success,"Broke out 2 joints of 13 3/8"" casing. Trouble with catwalk conveyer.",0.5 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-10 22:30:00+00:00,2009-06-10 23:45:00+00:00,1399.0,m,fixed,interruption -- maintain,ok,equipment failure,Trouble shot catwalk conveyer.,1.25 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-10 23:45:00+00:00,2009-06-11 00:15:00+00:00,1399.0,m,fixed,plug abandon -- trip,ok,success,Fine tuned link tilts and Weatherford tong movements.,0.5 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 00:15:00+00:00,2009-06-11 04:00:00+00:00,1118.0,m,fixed,plug abandon -- trip,ok,success,"POOH and L/D 13 3/8"" casing on deck.",3.75 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 04:00:00+00:00,2009-06-11 05:00:00+00:00,1064.0,m,fixed,plug abandon -- trip,ok,success,"POOH and L/D 13 3/8"" casing from 1118m to 1064.",1.0 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 05:00:00+00:00,2009-06-11 05:15:00+00:00,1064.0,m,fixed,plug abandon -- trip,ok,success,"Held Tool Box Talk with oncoming crew prior to POOH with 13 3/8"" casing.",0.25 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 05:15:00+00:00,2009-06-11 16:15:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"POOH with 13 3/8"" casing from 1064m to surface.",11.0 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 16:15:00+00:00,2009-06-11 17:00:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,Rigged down casing equipment.,0.75 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 17:00:00+00:00,2009-06-11 17:15:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Held Tool Box Talk with oncoming crew prior to rig down casing equipment.,0.25 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 17:15:00+00:00,2009-06-11 20:30:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Rigged down casing equipment.,3.25 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 20:30:00+00:00,2009-06-11 20:45:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Held Tool Box Talk prior to run and set seat protector.,0.25 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 20:45:00+00:00,2009-06-11 21:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"P/U seat protector RT, installed seat protector.",0.25 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 21:00:00+00:00,2009-06-11 21:30:00+00:00,140.0,m,fixed,plug abandon -- trip,ok,success,"RIH with seat protector on 5 1/2"" HWDP / DP.",0.5 +15_9_F_10_2009_06_12.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-11T00:00:00+02:00,2009-06-12T00:00:00+02:00,2009-06-11 21:30:00+00:00,2009-06-11 22:00:00+00:00,140.0,m,fixed,plug abandon -- other,ok,success,Jetted well head. Set seat protector according to Vetco procedures.,0.5 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-11 22:00:00+00:00,2009-06-11 22:30:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"POOH with seal protector RT. Re-set NSP RT, L/D same on deck.",0.5 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-11 22:30:00+00:00,2009-06-11 22:45:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"Tool Box Talk prior to RIH with 3 1/2"" cement stinger on 5 1/2"" DP.",0.25 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-11 22:45:00+00:00,2009-06-11 23:15:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"Changed to 3 1/2"" inserts in elevator. Installed PS-21 slips.",0.5 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-11 23:15:00+00:00,2009-06-12 00:15:00+00:00,356.0,m,fixed,plug abandon -- trip,ok,success,Changed dies in iron roughneck and PS-21 slips.,1.0 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 00:15:00+00:00,2009-06-12 01:30:00+00:00,356.0,m,fixed,plug abandon -- trip,ok,success,"RIH with 3 1/2"" DP from surface to 356m",1.25 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 01:30:00+00:00,2009-06-12 02:15:00+00:00,356.0,m,fixed,plug abandon -- other,ok,success,"Changed from 3 1/2"" to 5 1/2"" pipe handling equipment.",0.75 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 02:15:00+00:00,2009-06-12 04:00:00+00:00,1481.0,m,fixed,plug abandon -- trip,ok,success,RIH with cement string from 356m to 1481m MD.,1.75 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 04:00:00+00:00,2009-06-12 04:15:00+00:00,1481.0,m,fixed,plug abandon -- other,ok,success,Held Tool Box Talk prior to spotting Hi-Vis pill.,0.25 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 04:15:00+00:00,2009-06-12 05:00:00+00:00,1481.0,m,fixed,plug abandon -- other,ok,success,"Broke circulation and verified steady parameters. 3040 l/min, 290 bar. RIH from 1480m to 1580m MD.",0.75 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 05:00:00+00:00,2009-06-12 05:30:00+00:00,1580.0,m,fixed,plug abandon -- other,ok,success,"Pumped and displaced 30m3 1,51 sg Hi-Vis pill. 3000 l/min, 267 bar.",0.5 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 05:30:00+00:00,2009-06-12 06:00:00+00:00,1485.0,m,fixed,plug abandon -- trip,ok,success,POOH from 1580m to 1485m MD.,0.5 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 06:00:00+00:00,2009-06-12 07:45:00+00:00,1485.0,m,fixed,plug abandon -- other,ok,success,"Circulated bottoms up at 1485m MD. 3000 l/min, 260 bar.",1.75 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 07:45:00+00:00,2009-06-12 08:00:00+00:00,1485.0,m,fixed,plug abandon -- other,ok,success,P/U and installed pump-in sub assembly.,0.25 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 08:00:00+00:00,2009-06-12 08:15:00+00:00,1485.0,m,fixed,plug abandon -- other,ok,success,"Pumped 15m3 1,70 sg spacer. 1330 l/min, 62 bar. Chased to rig floor with 800 ltrs. OBM.",0.25 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 08:15:00+00:00,2009-06-12 09:30:00+00:00,1485.0,m,fixed,plug abandon -- other,ok,operation failed,Troubleshot blockage from cement tank to surge tank.,1.25 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 09:30:00+00:00,2009-06-12 10:30:00+00:00,1485.0,m,fixed,plug abandon -- cement plug,ok,success,"Mixed and pumped 41,9m3 1,92 sg ""G"" cement slurry.",1.0 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 10:30:00+00:00,2009-06-12 10:45:00+00:00,1485.0,m,fixed,plug abandon -- other,ok,success,B/O and L/D pump-in sub assembly.,0.25 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 10:45:00+00:00,2009-06-12 12:00:00+00:00,1100.0,m,fixed,plug abandon -- trip,ok,success,POOH with cement string from 1485m to 1100m MD.,1.25 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 12:00:00+00:00,2009-06-12 12:30:00+00:00,1100.0,m,fixed,plug abandon -- other,ok,success,"Inserted 2 sponge balls and flushed string. 3200 l/min, 275 bar, 60 rpm, 2 kNm. Meanwhile filled trip tank.",0.5 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 12:30:00+00:00,2009-06-12 13:00:00+00:00,1100.0,m,fixed,plug abandon -- other,ok,success,"Pumped and displaced 4,7m3 1,71 sg slug.",0.5 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 13:00:00+00:00,2009-06-12 13:30:00+00:00,1100.0,m,fixed,plug abandon -- other,ok,success,"Held Tool Box Talk prior to L/D 5 1/2"" DP on deck. Meanwhile troubleshot HTS conveyor.",0.5 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 13:30:00+00:00,2009-06-12 15:45:00+00:00,629.0,m,fixed,plug abandon -- trip,ok,success,"POOH and L/D 5 1/2"" DP from 1100m to 629m MD.",2.25 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 15:45:00+00:00,2009-06-12 21:15:00+00:00,629.0,m,fixed,plug abandon -- wait,ok,success,Waited on cement to set up. meanwhile troubleshot malfunction on HTS conveyor belt.,5.5 +15_9_F_10_2009_06_13.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-12T00:00:00+02:00,2009-06-13T00:00:00+02:00,2009-06-12 21:15:00+00:00,2009-06-12 22:00:00+00:00,528.0,m,fixed,plug abandon -- trip,ok,success,"POOH and L/D 5 1/2"" DP from 629m to 528m MD.",0.75 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-12 22:00:00+00:00,2009-06-12 22:45:00+00:00,356.0,m,fixed,plug abandon -- trip,ok,success,"Continued POOH and L/D 5 1/2"" DP from 528m to 356m MD.",0.75 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-12 22:45:00+00:00,2009-06-12 23:30:00+00:00,356.0,m,fixed,plug abandon -- other,ok,success,"Held tool Box Talk. Changed from 5 1/2"" to 3 1/2"" handling equipment. Broke and L/D X/O's.",0.75 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-12 23:30:00+00:00,2009-06-13 01:00:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,"POOH with 3 1/2"" cement string from 356m to surface. Racked same in derrick.",1.5 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 01:00:00+00:00,2009-06-13 01:15:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"Cleaned and cleared rigfloor, held tool Box Talk prior to change handling equipment and RIH with jetting tool.",0.25 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 01:15:00+00:00,2009-06-13 01:30:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"Changed from 3 1/2"" to 5 1/2"" handling equipment.",0.25 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 01:30:00+00:00,2009-06-13 03:30:00+00:00,1100.0,m,fixed,plug abandon -- trip,ok,success,RIH with Bull nose and Jetting tool from surface to 1100m MD.,2.0 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 03:30:00+00:00,2009-06-13 04:00:00+00:00,1100.0,m,fixed,plug abandon -- wait,ok,success,Waited on cement to set up. Meanwhile performed rig maintenance.,0.5 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 04:00:00+00:00,2009-06-13 10:45:00+00:00,1100.0,m,fixed,drilling -- casing,ok,success,"Waited on cement. Meanwhile serviced AFT PRS, checked breakes and oil level.",6.75 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 10:45:00+00:00,2009-06-13 11:00:00+00:00,1100.0,m,fixed,plug abandon -- other,ok,success,"Broke circulation, 400 l/min, 12 bar.",0.25 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 11:00:00+00:00,2009-06-13 11:30:00+00:00,1100.0,m,fixed,plug abandon -- other,ok,success,"Lined up and performed line test, 98 bar, 10 min. Verified line up by applying 10 bar on line, and opened HCR and IBOP.",0.5 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 11:30:00+00:00,2009-06-13 12:15:00+00:00,1100.0,m,fixed,plug abandon -- cement plug,ok,success,"Pressure tested cement plug to 98 bar, 30 min. Pumped 1,21m3. Meanwhile held Tool Box Talk prior to displace well to sea water.",0.75 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 12:15:00+00:00,2009-06-13 12:30:00+00:00,1100.0,m,fixed,plug abandon -- cement plug,ok,success,"Bled off pressure. Got 1,15m3 in returns.",0.25 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 12:30:00+00:00,2009-06-13 13:30:00+00:00,1100.0,m,fixed,plug abandon -- other,ok,success,"Lined up and displaced surface lines to base oil. C & K manifolds, bleed off, poor boy de-gasser and trip tank.",1.0 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 13:30:00+00:00,2009-06-13 16:00:00+00:00,1100.0,m,fixed,plug abandon -- other,ok,success,"Displaced well to treated sea water as per pumping plan. 2500 l/min, 83 bar.",2.5 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 16:00:00+00:00,2009-06-13 18:15:00+00:00,148.0,m,fixed,plug abandon -- trip,ok,success,POOH with riser jetting tool from 110m to 148m,2.25 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 18:15:00+00:00,2009-06-13 19:00:00+00:00,148.0,m,fixed,plug abandon -- other,ok,success,"Flushed C & K manifoild with treated sea water. 650 l/min, 3 bar.",0.75 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 19:00:00+00:00,2009-06-13 19:15:00+00:00,148.0,m,fixed,plug abandon -- other,ok,success,"Pumped 15m3 Hi-Vis pill to displace riser. 3080 l/min, 43 bar.",0.25 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 19:15:00+00:00,2009-06-13 20:45:00+00:00,148.0,m,fixed,plug abandon -- other,ok,success,"Displaced Hi-Vis pill with sea water, and pumped til clean returns. 3475 l/min, 64 bar. Pulled 1 stand every 15 min, rotated 5-10 rpm.",1.5 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 20:45:00+00:00,2009-06-13 21:15:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"POOH from BOP to surface. Held Tool Box Talk. L/D 16"" jetting tool on deck.",0.5 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 21:15:00+00:00,2009-06-13 21:45:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Tool Box Talk. P/U and installed Seat protector RT.,0.5 +15_9_F_10_2009_06_14.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-13T00:00:00+02:00,2009-06-14T00:00:00+02:00,2009-06-13 21:45:00+00:00,2009-06-13 22:00:00+00:00,120.0,m,fixed,plug abandon -- trip,ok,success,RIH with seat protector RT from surface to 120m.,0.25 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-13 22:00:00+00:00,2009-06-13 22:30:00+00:00,148.0,m,fixed,plug abandon -- other,ok,success,"Continued to RIH from 120m to 148m. Connected seat protector. Jetted Well head. 2950 l/min, 33 bar.",0.5 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-13 22:30:00+00:00,2009-06-13 22:45:00+00:00,0.0,m,fixed,plug abandon -- trip,ok,success,POOH with seat protector from 148m to surface.,0.25 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-13 22:45:00+00:00,2009-06-13 23:30:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"Disconnected Bull nose, jet sub and seat protector from RT and L/D RT.",0.75 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-13 23:30:00+00:00,2009-06-14 00:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"Tool Box Talk. Made up side entry sub assembly, closed annular, blew air down choke line to drain BOP.",0.5 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 00:00:00+00:00,2009-06-14 00:30:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Tool Box Talk and preparations for nippling down diverter.,0.5 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 00:30:00+00:00,2009-06-14 02:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Nippled down diverter.,1.5 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 02:00:00+00:00,2009-06-14 03:15:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Nippled down bell niple.,1.25 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 03:15:00+00:00,2009-06-14 04:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Nipled down and skidded BOP to test stump.,0.75 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 04:00:00+00:00,2009-06-14 05:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Completed nippling down and skidded BOP to test stump.,1.0 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 05:00:00+00:00,2009-06-14 05:15:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Held Tool Box Talk prior to connecting Claxton tool.,0.25 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 05:15:00+00:00,2009-06-14 06:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Removed master bushing, ran Claxton tool through, installed master bushing, connected stand of DP.",1.25 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 06:30:00+00:00,2009-06-14 08:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,M/U Claxton tool to BOP joint. Meanwhile prepared tention system for dis-assembly.,1.5 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 08:00:00+00:00,2009-06-14 08:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Removed scaffold from BOP joint.,0.5 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 08:30:00+00:00,2009-06-14 08:45:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Transferred tension from cylinders to TDS. Informed production to shut in.,0.25 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 08:45:00+00:00,2009-06-14 10:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Nippled down tension cylinders. Meanwhile ran guide wire and hot stab.,1.75 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 10:30:00+00:00,2009-06-14 11:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Moved moonpool hatches from BOP joint.,0.5 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 11:00:00+00:00,2009-06-14 12:15:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Unlock TBC. Primary release ineffective. Unlocked TBC secondary release.,1.25 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 12:15:00+00:00,2009-06-14 12:45:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Retreive hot stab and guide wire.,0.5 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 12:45:00+00:00,2009-06-14 13:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"P/U 2m and installed debris cap. Continued P/U until Claxton tool at rotary table. Racked 1 stand 5 1/2"" DP.",0.25 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 13:00:00+00:00,2009-06-14 13:45:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Pulled BOP joint to rotary level.,0.75 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 13:45:00+00:00,2009-06-14 14:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Held Tool Box Talk prior to install spider.,0.25 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 14:00:00+00:00,2009-06-14 15:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Installed HPDR spider.,1.0 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 15:00:00+00:00,2009-06-14 17:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Removed fairing and broke flange connection. Meanwhile cleaned in shakers and re-assembled pump 1.,2.0 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 17:00:00+00:00,2009-06-14 18:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Disconnected at bottom of BOP joint, L/D same on deck.",1.5 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 18:30:00+00:00,2009-06-14 20:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"P/U splash zone joint, set in spider, disconnected and L/D on deck.",2.0 +15_9_F_10_2009_06_15.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-14T00:00:00+02:00,2009-06-15T00:00:00+02:00,2009-06-14 20:30:00+00:00,2009-06-14 22:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"POOH with HPDR, L/D on deck.",1.5 +15_9_F_10_2009_06_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-15T00:00:00+02:00,2009-06-16T00:00:00+02:00,2009-06-14 22:00:00+00:00,2009-06-15 02:30:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,"Continue POOH with HPDR, L/D on deck.",4.5 +15_9_F_10_2009_06_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-15T00:00:00+02:00,2009-06-16T00:00:00+02:00,2009-06-15 02:30:00+00:00,2009-06-15 04:00:00+00:00,0.0,m,fixed,drilling -- bop/wellhead equipment,ok,success,Cleaned and cleared rigfloor. Closed hatches on lower deck. Removed scaffolding. Prepared to run corrotion cap.,1.5 +15_9_F_10_2009_06_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-15T00:00:00+02:00,2009-06-16T00:00:00+02:00,2009-06-15 04:00:00+00:00,2009-06-15 07:00:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,"Cleared rigfloor for excess equipment. Attempted to inspect well head, lost communication with camera. +Meanwhile performed general rig maintenance. Prepared for skidding.",3.0 +15_9_F_10_2009_06_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-15T00:00:00+02:00,2009-06-16T00:00:00+02:00,2009-06-15 07:00:00+00:00,2009-06-15 11:30:00+00:00,0.0,m,fixed,interruption -- maintain,ok,success,"Changed blower hose, cleaned shakers, pits and broke riser doubles. +Meanwhile repaired camera on ROV.",4.5 +15_9_F_10_2009_06_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-15T00:00:00+02:00,2009-06-16T00:00:00+02:00,2009-06-15 11:30:00+00:00,2009-06-15 13:00:00+00:00,0.0,m,fixed,drilling -- other,ok,success,"ROV inspected Well Head with camera. +Meanwhile continued to change blower hose and general cleaning.",1.5 +15_9_F_10_2009_06_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-15T00:00:00+02:00,2009-06-16T00:00:00+02:00,2009-06-15 13:00:00+00:00,2009-06-15 16:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,Ran and installed corrosion cap and pumped inhibitor. Cut hose and retreived mini reel and tugger to surface.,3.0 +15_9_F_10_2009_06_16.xml,NO 15/9-F-10,NO 15/9-F-10,2009-06-15T00:00:00+02:00,2009-06-16T00:00:00+02:00,2009-06-15 16:00:00+00:00,2009-06-15 17:00:00+00:00,0.0,m,fixed,plug abandon -- other,ok,success,"Installed hatch covers in moonpool and removed bridge from cantilever to prosess module. +***End of operation for F - 10.***",1.0